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Solvent Alternatives Guide
Brushing

Case Studies

A 3M electronics products plant was using ammonium persulfate, phosphoric acid, and sulfuric acid to clean copper sheeting. This cleaning method generated 40,000 lb/yr of hazardous liquid waste. The plant switched to a rotating brush cleaning system that scrubbed the copper sheeting with pumice. The abrasive cleaning method generates a nonhazardous waste sludge that can be disposed of in a conventional landfill. The new cleaning system cost $59,000. The initial cost was recovered in the third year of operation.

3M Company. Waste Stopper: Pumice on Copper. Environmental Engineering and Pollution Control Dept., Saint Paul, MN.


Cenex, in Inver Grove Heights, MN, recycles approximately 110,000 30- and 55-gallon drums as part of their lubricant distribution business. Drums are typically reused (and repainted) 5 or 6 times. Cenex switched from a hot caustic paint removal system to a mechanical paint removal system utilizing metal and nylon brushes. Cenex eliminated 164,000 lb/yr of caustic waste generation. The brushing unit generates approximately 12,000 lb/yr of nonhazardous paint chip waste. The brushing unit cost $110,000 initially and replacement brushes cost $25,000 annually. Waste disposal costs have been reduced from $55,000/yr to $900/yr. Maintenance downtime is now 4 days/yr instead of 16 days/yr. Cenex also saves $6,000/yr on the cost of sodium hydroxide. NET SAVINGS: $35,000/YR + 12 DAYS/YR DOWNTIME.

Pagel, Paul. 1993. Brushing Replaces Sodium Hydroxide for Paint Removal. MnTAP SOURCE, 8(2):1, Minnesota technical Assistance Program.


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Last Update: 29 December 1998
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