IMPROVED STENCILING AND MARKING SYSTEM
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Overview: | The Improved Stenciling and Marking
System can generate and print labels, markings, signs, instruction plates
etc., on a variety of engineered adhesive-backed materials without
generating any hazardous wastes or volatile organic compound (VOC)
emissions. The traditional method of marking equipment requires the
use of a stencil cutout, followed by masking material and paint. This
method generates paint and paint wastes (spray cans, tape, rags, and
solvent, etc.) that must generally be disposed of as hazardous waste.
The system generates durable stencils and signs via a computer-driven graphics output device that prints and cuts vinyl and film material to marking operation specifications. Most desktop computers with the necessary capabilities can run the software. According to the manufacturers, vinyl stencils have an outdoor durability of up to 7 years, and the image has a guaranteed outdoor life of 3 to 5 years. In contrast, spray-painted, stenciled markings must be reapplied every 18 months. These systems can be used to provide all the marking, stenciling, and sign making for an activity or ship. Examples of applications include aircraft labels, support equipment (part numbers, operational instructions) automotive decals, and facility directional signs. A Navy Environmental Leadership Program (NELP) Preproduction Initiative Demonstration evaluated the viability of two systems (The Roland Color Camm Pro and the Gerber Edge) for Navy applications. In this project NAS North Island prototyped the equipment and three other sites, NS Mayport, Naval Air Station Joint Reserve Base (NASJRB) New Orleans, and NAS Brunswick, provided input. The Roland Color Camm Pro (Pc-60) is a one-piece device that prints and cuts stencils. The Gerber Edge and GSx Cutter is a unit composed of two separate components; the edge, which prints the stencil, and the cutter. Consumables used by both the Roland and Gerber units include vinyl (adhesive-backed), transfer tape (used to assist in transferring an adhesive-backed stencil onto the desired surface), and application fluid (applied to the surface being stenciled to enhance proper positioning of the stencil). The results of the demonstrations indicated that:
For more information regarding these tests, refer to Test Directive NAWCADLKE-PVTD-SE-980001. *This information is contained in the latest update of NAVAIR 17-1-125, Support Equipment Cleaning, Preservation and Corrosion Control Manual, dated 15 March 2000. | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Compliance Benefit: | Switching from traditional paint stenciling to
an Improved Stenciling and Marking System will result in reduced hazardous waste
generation and disposal costs, which contribute to compliance under RCRA (40 CFR 262)
and Executive Order 13148. It will also help facilities to meet the Federal
acquisition and waste prevention requirements of EO 13101. Furthermore, non-paint-based
stenciling and marking may help a facility to reduce its reporting requirements
under SARA Title III (40 CFR 355, 370, 372).
In addition, by reducing HAP and VOC emissions related to solvent use, a facility will be more likely to meet the emissions limits of an air permit issued in accordance with 40 CFR 70 and 71 or related state requirements. The switch may also decrease the need for a facility to obtain an air permit in the first place. The compliance benefits listed here are only meant to be used as general guidelines and are not meant to be strictly interpreted. Actual compliance benefits will vary depending on the factors involved, e.g., the amount of workload involved. | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Materials Compatibility: |
No material
compatibility issues were identified. | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Safety and Health: | The use of the system
contributed to a healthier work environment for personnel by removing
exposure to solvents and paints and potential cut hazards presented by the
traditional method. Consult your local industrial health specialist
and your local health and safety personnel prior to implementing this
technology. | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Benefits: |
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Disadvantages: | No disadvantages were
identified. | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Economic Analysis: |
The information provided
below was generated under the NELP-PreProduction Initiative.
Assumptions:
Cost Comparison for Spray Paint with Stencil Cutouts vs. NELP Method Previous Method: Spray Paint with Stencil Cutouts
Labor Waste Disposal
Cost Analysis Summary (Per Year)
*Roland = (10 x $11,609.33) - [$7,470.00 + (10 x $3,691.48)] ; Gerber = (10 x $11,609.33) - [$22,136.26 + (10 x $4,251.78)] | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
NSN/MSDS: | None identified. | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Approving Authority: | Appropriate authority for making process changes should
always be sought and obtained prior to procuring or implementing any of the technology
identified herein. | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Points of Contact: | For more information | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Vendors: | This is not meant to be a
complete list, as there may be other suppliers of this type of
equipment.
Tonas Graphics | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Related Links: |
Do You Mark Equipment And
Paint Signs?, Navy Environmental Quality Initiative (EQI)
Improved Stenciling and Marking System | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Sources: | Mr. Tom Rua, NAWC
Lakehurst. Pollution Prevention Equipment Program, 1998 Preproduction Initiative Final Report, Improved Stenciling and marking System, NAS NORTH ISLAND, CA, 13 December 2000, Naval Air Warfare Center, Lakehurst, NJ. Preproduction Initiative - NELP, Improved Stenciling and Marking system, Cost Analysis Report. JG-PP Information Sheet for: Low-Voc Identification Marking, March 2000. Paper, "Technology Survey for Alternatives to Solvent-Based Ink Stenciling for Identification Marking, NDCEE, October 29, 1997 and July 16, 1998. | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
Supplemental: |
Picture of Improved Stenciling and Marking System![]() |