Case Study # 82
1. Headline: Different technical measures were taken to
reduce the polymer residues in the process waste water
from a chemical process industry that manufactures
acrylate dispersions used as binding agents in water-based
inks.
2. Background: Rohm and Haas Nordic is a chemical process
industry that manufactures acrylate dispersions which are
used as binding agents in water-based inks. Rohm and Haas
as an international company has a central programme that
includes a "Waste Reduction Policy". The programme
originated from the rather strict environmental demands
placed on Rohm and Haas in the United States by the
American environmental authorities. Another contributing
factor to the formulation of the central environmental
programme was the bad will which the international
chemical industry got after several serious accidents.
The company's products are classified based on their
hazardousness and restrictions have been established for
each class. Other areas of emphasis include the intention
to limit landfilling, the requirement of catchment dams
to protect against discharges directly to fresh water,
and groundwater analysis to discover leakages. The company
also has the goal of reducing the polymer content in the
waste water (white water). The internal programme of
environmental measures is to some extent considerably more
far-reaching than the Swedish authorities requirements.
The company is part of the multinational concern Rohm and
Haas Co. The plant in Landskrona has about 50 employees
and the turnover in 1993 was US$ 26.9 million. Some 50
different products were manufactured with a total weight
of 27,500 tons. Case study was performed in 1990.
3. Cleaner Production Principle: Process modification
4. Description of Cleaner Production Application:
Process/equipment modification: The polymer binding
agents are made in batches, one product a time. The
production time for a product can be up to 24 hours. The
process stages during the manufacturing of polymer
products before accomplished changes of equipment:
In the pre-emulsifying tank the base chemicals,
principally acrylate monomers, are mixed with additive
chemicals for emulsifying the monomers. The mixture is
transferred to a reactor vessel where polymerization
takes place after the addition of catalysts and
activators. Then the product is tapped to a mixing vessel
where the final consistency is achieved. At this stage,
neutralization and preserving also takes place. The
product is then filtered to remove larger particles. The
final polymer product is a 50% water dispersion and is
pumped to a storage tank from which it is delivered either
in bulk or in a barrel or container.
The quality demands on the products are high. Therefore a
thorough cleaning of the process equipment after every
manufactured batch is necessary. The generated process
waste water is centrally collected in a sludge tank.
Certain treatment is carried out such as pH-adjustment and
test of the water which must be free from monomers before
discharge to the municipal waste water treatment facility.
Earlier reactor vessels in glass enamelled steel were
replaced with stainless steel reactor vessels which also
had a 50% larger volume. The increased capacity in
relation to each produced batch reduced the need for
cleaning. The surrounding equipment was also changed;
among other things, modern control equipment was added
permitting an increased automatic control as well as a
more effective and water saving high pressure wash of the
reactor. After emptying the reactor, the first rinse water
was transferred from the rotating nozzles to be used as
dilution water in the blending tank. These various
measures have lessened the role of the reactor as a
source of product loss as well as reduced the need for
cleaning.
The filtering of a product is done at several different
stages in the process. The product loss was greatest in
the filtering which takes place between the blending tank
and storage tank. The filters were replaced with others
with smaller volume. As a result product loss could be
reduced from the earlier 40 kg to 2-3 kg at every filter
replacement. It has been estimated that product loss
during the filter replacement amounted to around 100 tons
(50% polymer product). The quantity has now been reduced
by 80%. Dedicated pipelines have been installed to all
storage tanks for finished products. In this way, there is
no need to empty the system between every bulk unloading.
The dedicated pipelines system also makes it possible to
limit the product loss, cleaning needs and water
consumption. The preventive measures will save nearly 160
tons of polymers (50 % polymer product) which otherwise
would have left the facility with the waste water. A
waste reduction audit showed that this amount corresponds
to 30 percent of the total product loss.
Losses arose earlier in the transport pipeline between the
plant and the tank farm when product in the pipes was
rinsed away. The losses have been about 40 tons of
polymers a year (50% polymer product). To take care of
this loss a new line with the possibility for spiking was
installed. Spiking involves emptying a system by pushing a
plug of foamed plastic through with compressed air. The
spiking system reduced the product loss by up to 90% as
well as the water consumption and the amount of polymers
in the white water could be reduced.
More deliveries in bulk are now done with a corresponding
reduction in tapping from barrels and other containers.
This reduces the need for cleaning and water consumption.
In 1987 the distribution between the different forms of
delivery was 72% by bulk, 21% by barrel, and 7% by other
types of containers. The corresponding values for 1993
were 75% by bulk, 5% by barrel, and 20% by other types of
containers.
Earlier, the process water inhalted polymer products. An
installation of ultrafiltration equipment has now made it
possible to separate all polymer residues from the waste
water. The dry substance content is 40% for the recycled
polymer material.
Furthermore, the recovered product has a sufficiently high
quality and could be used as a simple binding agent.
Process and Waste Information: Rohm and Haas Nordiska AB
is a chemical process industry that manufactures acrylate
dispersions which are used as binding agents in water-
based inks. The environmental load was concentrated to
the process waste water which contained polymer residues;
the so called white water. A change of reactor vessels
lessened the role of the reactors as a source of product
loss as well as reduced the need for cleaning.
As a result of the new filters with smaller volume the
product loss could be reduced from the earlier 40 kg to
2-3 kg at every filter replacement. Dedicated pipelines to
every storage tank for finished products made it possible
to eliminate 160 tons of polymers from the process waste
water. The cleaning needs and water consumption could also
be reduced and there is no need to empty the system
between every bulk unloading. Ultrafiltration is used to
separate the polymer residues from the process water. The
recovered product has a dry content of 40% and such a
sufficiently high quality that it could be used as a
simple binding agent.
Scale of Operation: The plant has 50 employees and the
turnover in 1993 was US$ 26.9 million. Some 50 products
were manufactured with a total weight of 27,500 tons.
Year Process waste water Production Total dry content
in the waste water**
(tons) (tons) (kg/ton produced)
1986 156 12,000 12.7
1987 180 15,400 11.8
1990 250 26,400 9.5
1991/92* - - 6.6
1993 - 27,500 6.0
* Calculated from one year ahead from the middle of 1991
** Before ultrafiltration
The technology is fully implemented and commercially
available.
Material/Energy Balances and Substitution:
Material Category Quantity Before Quantity After
1986 1993
Waste Generation 12.7 kg/ton 6.0 kg/ton
Feedstock Use N/A N/A
Water Use N/A reduced
Energy Use equivalent
5. Economics
Investment costs include the installation of the dedicated
pipeline system within the tank farm: US$ 253,000, and the
installation of spiking system: US$ 16,900.
Payback Time: Based on the sales value the payback time
was 1.1 years for the tank farm and three to four months
for the dedicated pipelines system
6. Advantages
Reduction of the loss of finished products, reduced need
for cleaning and reduced volume of polymers in the process
waste water were obtained. The recovered product had a
sufficiently high quality and could be used as a simple
binding agent. The driving force behind the accomplished
changes at the company was a central programme which Rohm
and Haas had as a multinational company that included a
"Waste Reduction Policy". The programme originated from
the rather strict environmental demands placed on Rohm and
Haas in the United States by the American environmental
authorities. Another contributing force was the badwill
which the international chemical industry got after
several serious accidents.
7. Constraints: Not reported.
8. Contacts
Lars Siljebratt & Claes Nilon
Foundation of TEM
Asumsgatan 38 275 37
Sjobo Sweden
TEL: +46-(0)416-273 00
FAX: +46-(0)416-273 12
Rohm and Haas Nordiska AB
Ringvogen 163
Box 45
261 22 Landskrona
Sweden
Tel: +46-(0)418-240 90
9. Keywords: Sweden, chemicals, acrylate, process
modification, ink, water-based inks, polymers, binding
agent, spiking system, ultrafiltration.
10. This case study was translated from Swedish and submitted
by the Swedish Foundation of TEM to UNEP IE. It was
edited by UNEP IE in July 1995, but has not undergone a
formal technical review.