CASE STUDY #51
1. Headline: Reducing waste in polyester production
2. Background: Synthetic fibre (polyester) plays an important
role in the textile industry in Indonesia. The first step in
polyester production is the production of chips through a
polymerization process in which raw materials -including
ethylene glycol, terephtalic acid, additives and a catalyst -
are combined. This process produces two types of wastes:
liquid waste that is treated in the wastewater treatment
plant; and solid waste, known as RG-Residue. Before the
implementation of cleaner production technologies, the RG-
Residues were disposed of by incineration.
Seven boilers provide power for the process. Of these, three
use heat recovered from the diesel engines, two industrial diesel
oil, one natural gas and one diesel fuel.
P.T.TIFICO was founded in 1973 with two shareholders, Teijin
Ltd and Toyo Menka Kaisha (Japan); the company went public in
1980. P.T.TIFICO consists of 14 departments, including one
dedicated to safety and environmental concerns. P.T.TIFICO
produces staple fibre and filament yarn polyester.
3. Cleaner Production Principle: Material substitution
4. Description of Cleaner Production Application: Cleaner
production initiatives at P.T.TIFICO included the reuse of RG-
Residue, substitution of industrial diesel oil with natural
gas, industrial water recirculation and heat recovery. These
cleaner production initiatives have increased process
efficiency.
Reuse of RG-Residue: The RG-Residue was previously disposed
of in an incinerator with a 1.5 ton/day capacity. This
process was costly and produced substantial air pollution. It
was therefore decided to evaluate the reuse of RG-Residue as
an additive in the production of carpet sheet for roofing.
The additive was found to improve the characteristics of the
carpet sheet, and incineration was stopped. This reduced air
pollution substantially and produced economies in savings on
incinerator fuel which decreased production costs. The plant
produces about 35 tons a month of RG-Residue but since demand
exceeds production there are no storage problems.
Natural gas utilization: One boiler running off industrial
diesel fuel oil was converted to run off natural gas,
reducing air pollution and energy costs.
Industrial water recycling: In the wastewater treatment
plant, liquid wastes are treated by activated sludge. Before
treatment, chemical oxygen demand (COD) levels were 10 000-12
000 parts per million (ppm). Following treatment, COD levels
were reduced to 20-40 ppm, a level which easily meets the
government standard for wastewater of 200 ppm (class II).
Approximately 32 per cent of the wastewater is now reused in
the process, reducing the need for fresh water by about 2450
liters/minute.
Exhaust gas recovery: Waste heat from the diesel engine is
used to produce 12 tons/hour of steam.
5. Economics:
Natural gas utilization US$/year
Net savings 387 000
Capital investment 637 700
Payback period 1.7
years
Industrial water recycling
Net savings 53 408
Capital investment 12 074
Payback period 3 months
Exhaust gas boiler
Net savings 601 843
Capital investment 1 105
990
Payback period 1.84
years
Reuse of RG-Residue
energy savings 390
labor savings 1 100
sales of wastes 5 530
Total 7 020
6. Advantages: N/A
7. Constraints: N/A
8. Contacts:Djahri Arsyad
Tatsushito Maeda
P.T.TIFICO
PO Box 485
Tangerang 15001
Indonesia
Phone: +62 21 553 1649
Fax: +62 21 553 1646
9. Keywords:Indonesia, textile, polyester, material
substitution, RG-residue, COD
10. Reviewer comments: This case study was originally
published in the UNEP IE document "Cleaner Production in the
ASIA and Pacific Economic Coorporation (APEC) Region. In the
process of preparing the document the case study underwent a
technical review.