INTERNATIONAL CLEANER PRODUCTION INFORMATION CLEARINGHOUSE

CASE STUDY #51

1. Headline: Reducing waste in polyester production

2. Background: Synthetic fibre (polyester) plays an important

role in the textile industry in Indonesia. The first step in

polyester production is the production of chips through a

polymerization process in which raw materials -including

ethylene glycol, terephtalic acid, additives and a catalyst -

are combined. This process produces two types of wastes:

liquid waste that is treated in the wastewater treatment

plant; and solid waste, known as RG-Residue. Before the

implementation of cleaner production technologies, the RG-

Residues were disposed of by incineration.

Seven boilers provide power for the process. Of these, three

use heat recovered from the diesel engines, two industrial diesel

oil, one natural gas and one diesel fuel.

P.T.TIFICO was founded in 1973 with two shareholders, Teijin

Ltd and Toyo Menka Kaisha (Japan); the company went public in

1980. P.T.TIFICO consists of 14 departments, including one

dedicated to safety and environmental concerns. P.T.TIFICO

produces staple fibre and filament yarn polyester.

3. Cleaner Production Principle: Material substitution

4. Description of Cleaner Production Application: Cleaner

production initiatives at P.T.TIFICO included the reuse of RG-

Residue, substitution of industrial diesel oil with natural

gas, industrial water recirculation and heat recovery. These

cleaner production initiatives have increased process

efficiency.

Reuse of RG-Residue: The RG-Residue was previously disposed

of in an incinerator with a 1.5 ton/day capacity. This

process was costly and produced substantial air pollution. It

was therefore decided to evaluate the reuse of RG-Residue as

an additive in the production of carpet sheet for roofing.

The additive was found to improve the characteristics of the

carpet sheet, and incineration was stopped. This reduced air

pollution substantially and produced economies in savings on

incinerator fuel which decreased production costs. The plant

produces about 35 tons a month of RG-Residue but since demand

exceeds production there are no storage problems.

Natural gas utilization: One boiler running off industrial

diesel fuel oil was converted to run off natural gas,

reducing air pollution and energy costs.

Industrial water recycling: In the wastewater treatment

plant, liquid wastes are treated by activated sludge. Before

treatment, chemical oxygen demand (COD) levels were 10 000-12

000 parts per million (ppm). Following treatment, COD levels

were reduced to 20-40 ppm, a level which easily meets the

government standard for wastewater of 200 ppm (class II).

Approximately 32 per cent of the wastewater is now reused in

the process, reducing the need for fresh water by about 2450

liters/minute.

Exhaust gas recovery: Waste heat from the diesel engine is

used to produce 12 tons/hour of steam.

5. Economics:

Natural gas utilization US$/year

Net savings 387 000

Capital investment 637 700

Payback period 1.7

years

Industrial water recycling

Net savings 53 408

Capital investment 12 074

Payback period 3 months

Exhaust gas boiler

Net savings 601 843

Capital investment 1 105

990

Payback period 1.84

years

Reuse of RG-Residue

energy savings 390

labor savings 1 100

sales of wastes 5 530

Total 7 020

6. Advantages: N/A

7. Constraints: N/A

8. Contacts:Djahri Arsyad

Tatsushito Maeda

P.T.TIFICO

PO Box 485

Tangerang 15001

Indonesia

Phone: +62 21 553 1649

Fax: +62 21 553 1646

9. Keywords:Indonesia, textile, polyester, material

substitution, RG-residue, COD

10. Reviewer comments: This case study was originally

published in the UNEP IE document "Cleaner Production in the

ASIA and Pacific Economic Coorporation (APEC) Region. In the

process of preparing the document the case study underwent a

technical review.