Case Study #247
1. Headline: Indonesia Cleaner Industrial Production Program
(ICIP): Cleaner Production Assessment for a Flexible
Packaging Manufacturer
2. Background:
Executive Summary
A Cleaner production assessment was conducted by ICIP in a
facility that manufactures flexible packaging. The purpose
of the assessment was to identify cleaner production
options that would reduce the quantity of toxic materials,
other raw materials, and energy used in the manufacturing
process; demonstrate the economic and environmental value
of a cleaner production assessment; and improve
manufacturing competitiveness and product quality. The
assessment was done by a team of US-based cleaner
production experts, US process specialists, and Indonesian
consultants.
The team identified 9 cleaner production options that
could save the facility Rp. 2.14 billion/year for an
implementation cost of Rp. 95.7 million. Both the cylinder-
making and printing areas of the facility were found to
have significant cleaner production opportunities. If
implemented, the opportunities will save and estimated
3,780,000 meters of printed substrate; 23,010 kg of ink;
35,700 liters each of toluene and ethyl acetate; and 1,450
kg of copper, nickel and chrome.
Most significantly, the implementation of these
opportunities would lead to a dramatic reduction in
rejects, especially of cylinders. For example, 150
cylinders per month (30% of total cylinder production) are
placed on the press and fail before 4,000 meters of
substrate are printed. The reduction of the reject rate
alone will save press downtime, process materials, and
environmental releases, and will increase profitability
without a need for increased sales.
Facility Background
The facility is a medium-sized flexible packing
manufacturer. The plant started operations in 1986 and
presently employs 300 workers, operating in three shifts,
five days per week. Occasionally the plant will be
operated more than five days per week when required by
production demands. Product output is about 50 million
meters of printed packaging annually. For its monthly
production, this facility uses an estimated 5 tons of
paper, 20 tons of aluminum sheet, 100 tons of extruded
plastic, 18,000 liters of ethyl acetate, 16,000 liters of
toluene, and 25 tons of ink of various colors.
3. Cleaner Production Principle: The assessment identified
various cleaner production applications including: process
modification, good housekeeping, new technology,
recycling, and material substitution.
4. Description of Cleaner Production Application:
Process Description
The process of producing flexible packaging can be divided
into five main processes. These are: 1) cylinder making;
2) image creation; 3) printing; 4) laminating; and 5)
slitting. The cylinder making process prepares a steel
tube to accept an etched image that will eventually
transfer ink to a substrate during the printing process.
The process involves electroplating the tube with nickel,
then copper, transferring an image to the surface of the
tube, and finally chrome electroplating to protect the
image from abrasion during the printing process. Numerous
polishing steps, both by hand and by automatic polishing
machines, are required throughout the process.
After reproducing the image on the surface of the
cylinder, the etched image is corrected and "proofed" by
actually printing a sample. At any stage a defect may be
detected, requiring grinding, polishing, etching or
dechroming to correct the problem. Some cylinders are
produced from a bare steel surface, while others are
produced by removing an image from a previously used
cylinder through dechroming, etching and grinding.
After proofing, the etched cylinder is placed in a
printing press and flooded with a solvent-based ink. A
different color (up to seven colors) is used for each
cylinder. The ink is transferred to the substrate
(polypropylene, OPP, polyethylene, or low-density
polyethylene) by rotating the cylinder through the ink
"fountain", wiping away the excess with a "doctor blade",
and then rotating the cylinder against the substrate. Some
products go through a laminating process that is done on
separate equipment. The final product is sized acceding to
customer needs by slitting large multiple-image rolls of
printed, laminated material to smaller rolls that may be
only one image wide.
Environmental Problems
There are three main types of contaminants form this
facility that adversely impact the environment. They are:
1) vapors which are released from chemical solutions for
cylinder making and dechroming, solvent adhesive, and ink;
2) liquid chemicals and heavy metals that are discharged
from spent cylinder making solutions, spent ink, and spent
solvent; and 3) solid waste which includes copper dust,
sludge, spent film from the cylinder-making process;
excess substrate from slitting, printing and laminating
and bobbin cutting.
Cleaner Production Opportunities
The assessment identified 9 cleaner production
opportunities that address the problems identified above.
Listed below are the opportunities recommended for this
facility and the environmental and financial benefits and
financial costs of each.
Summary of Recommended Cleaner Production Opportunities
Cylinder making--
1. Change concentrations maintain baths, improve
storage-- reduces releases of chrome nickel, and
copper to the environment, with an implementation
cost of Rp 12.9 million per year and a financial
savings of Rp 1.5 billion per year. An immediate
payback period.
2. Replace toluene with alkaline cleaner--
eliminates the releases of toluene to water at a cost
of Rp 4.5 million to implement Rp 5.9 million/year,
with a financial savings of Rp 16.9 million per year
with a pay back period od 5.3 months.
3. Recover copper fines eliminates copper releases
from this source at a cost of Rp 110,000 per year and
a financial savings of Rp 325,000 per year and a pay
back period of 4 months.
Printing--
1. Recover ink form cans- reduces ink consumption
between 3840 and 5760 kg/year. No implementation
costs and a financial benefit of Rp 30.7 to 46
million/year. With an immediate payback.
2. Computerized ink inventory and use color
matching system reduces waste ink reduces rejects due
to poor ink quality. Implementation costs of Rp 91
millon and financial benefits os Rp 138 million per
year with a pay back period of 8 months.
3. Zahn cup clean-up reduces solvent use by 90% and
reduces solvent releases. Costs of Rp 22,000 and
financial benefits of 167 million per year and an
immediate pay back period.
4. Modify doctor blade settings reduces releases of
chrome due to need for rework. No implementation
cost and a financial benefit of Rp 88 million / year
and an immediate payback
5. Improve temporary fluid storage reduces of and
exposure to evaporated solvents. Implementation
costs of Rp 22,000 and financial benefits of Rp 43.6
million per year and an immediate pay back period.
Engraving-- Indexing film to cylinder key reduces
substrate loss. Implementation costs of Rp 220,000 with
financial benefits of 160 million per year and an
immediate payback period.
Total implementation costs of opportunities estimated at
Rp 95.7 million (one-time costs); Rp 18.9 million per year
and financial benefits estimated a Rp 2.14 billion to 2.16
billion per year.
Cylinder Making-- The current composition of the three
plating baths causes many defects on the finished
cylinders. Of the total 500 cylinders that are chrome
plated every month, about 50% must be replated. This is
due to improper plating bath composition, maintenance,
dechroming, and grinding procedures. Taking measures to
improved this process will benefit the entire production
process, improving quality of the finished product and
reducing waste. The actions that should be taken to reduce
the number of defects on the cylinders include:
1) Change the concentrations of the sulfuric acid and
alter the components in the nickel, acid copper and chrome
baths. For a nominal cost, these measures will reduce
problems such as cracking, corrosion, hardness, and lack
of brightness on the cylinders.
2) Maintain the acid copper, chrome, and nickel process
solutions according to standard practice. Currently, the
solutions are changed with a high frequency. The acid
copper solution should last several years rather than two
weeks and the chrome and nickel solutions should seldom
require replacement.
3) During dechroming, maintain the hydrochloric acid
concentration at 10% by volume and plug the cylinders to
prevent HCL attack of the exposed steel on the interior of
the cylinder.
4) Improve storage conditions by drying cylinders and
placing them in a plastic bag with silica gel to prevent
corrosion in storage. It is estimated that 100 cylinders
per month must be rechromed because of corrosion from the
HCL bath and from the humid conditions.
Total saving from these changes could reach RP. 1.5
billion/year form reduced press downtime and less need for
rework. Increases in annual operating cost are Rp. 12.8
million/year. The payback period for these changes is 3.5
days.
Cleaning-- Toluene is currently used to clean the
cylinders. This system should be replaced with an alkaline
cleaning system which will improve cleaning and reduce the
need for toluene. The cost of a new cleaning system is Rp.
4,500,000. Annual savings are Rp. 10,920,000. The payback
period is 5.3 months.
Copper Recovery-- The grinding operation has and output of
solid copper fines that are currently directed outside to
the drainage ditch, where they have collected to some
depth. To eliminate copper releases, the fines in the
drainage ditch should be scooped out, washed and sold as
scrap. A porous bag should be attached to the grinder
output pipe to collect all fines in the future. Net
savings are Rp. 215000/year and the payback period is 4
months.
Ink Waste-- When a new can of ink is opened at the press,
it is divided up and diluted with solvent. The empty ink
can is then put aside next to the cleaning tank and filled
with waste solvents. The cans still contain some ink which
can be recovered and used on the press. This will reduce
ink consumption, saving between Rp. 30.7 and 46 million
each year.
Improve Ink Management-- The flow of ink through this
facility is complicated and inefficient. There is little
inventory control and many cans of ink remain in the
warehouse for several years, often becoming unusable.
Excess ink at the printing presses often remains unused
and evaporates. A computer system should be installed to
track shelf inventory and ink usage. A color matching
system and a new spectrometer would also enable the ink
manager to do color matching more efficiently. These
recommendations reduce the amount of ink returned to the
supplier or thrown away. Installation and training costs
are Rp. 91,000,000; annual ink savings are Rp.
138,000,000. The payback period is 8 months.
Solvent Use-- The viscosity of ink in the fountain is
monitored regularly using a Zahn cup. The Zahn cup is
washed after checking the viscosity. To do this, the
operator soaks the Zahn cup in fresh solvent. This solvent
is considered waste solvent after 3 Zahn cup cleanings. To
reduce the solvent used in the process by 90%, the
facility could use a triple counter rinse system which
would ensure that solvent was thrown out only after it was
no longer usable. The system could save the facility Rp.
167,132,160/year. Installation costs are less than Rp.
22,000.
Doctor blades-- Doctor blades are used to remove excess
ink form the cylinder before the impression is made on the
substrate. The facility could change the material of the
doctor blade from stainless to carbon steel, ensure that
it is mounted properly, and set the blade at a steeper
angle to reduce the entrapment of particles under the
blade. With these changes, the doctor blade will perform
better, keeping impurities from getting on to the print
surface of the cylinder and reducing the production of
waste. Savings are expected to be Rp. 88,200,000/year.
Reduce Solvent Losses in Temporary Ink Storage-- Several
ink cans reside in temporary storage near the presses at
any given time. Many of these are left with pouring holes
open or are cut to expose half the lid. This results in
evaporation of the inks, exposing workers to harmful
fumes. All ink cans in temporary storage should be sealed
when not in use, and durable plastic lids can be used for
the doctor blade cleaning drums. The savings from reducing
solvent evaporation can reach Rp. 43,649,000 per year.
Implementation cost is Rp. 22,000 to install new lids.
Indexing Film to Cylinder Keyway-- Typically, several
cylinders are used (one for each color) during any given
printing run. The cylinders must be properly aligned to
ensure that colors are overlayed correctly. The current
method used to position the cylinders does not index the
beginning of the film to a constant point on the cylinder
and successive cylinders on the press are in alignment at
the beginning of a run only by chance. This random
orientation of a set of cylinders causes mis-registration
at the beginning of a run wasting substrate, ink, and
press time. A pointer mounted in a fixed relation to the
collar can be used to position the film on the cylinder at
a constant point. Implementation cost is Rp. 220,000 and
savings are Rp. 160 million per year.
Conclusion
Many of the product quality and environmental problems of
this facility stem from problems in making and storing the
cylinders used in the printing process. Improving this
process to reduce rejects will significantly improve the
quality of the product, save the facility a substantial
amount of money each year, and reduce the impact of this
facility on the environment.
5. Economics: See above.
6. Advantages: See above.
7. Constraints: See above.
8. Contacts:
Indonesia Cleaner Industrial Production programme
Mashill Tower 20th floor
Jl. Jend. Sudirman Kav. 25
Jakarta 12920
Indonesia
TEL: (62 21) 5267681
(62 21) 5267682
(62 21) 5267683
(62 21) 5267684
FAX: (62 21) 5267680
Internet: icip@indo.net.id
9. Keywords: USAID, Indonesia, packaging, flexible
packaging, material substitution, process modification,
good housekeeping, recycling, ICIP, electroplating,
plating, iron and steel, heavy metal, chrome, nickel,
copper, solvent, toluene, acid, alkaline cleaning
10. Reviewer's comments: This case study was carried out in a
developing country in which EP3 has an established
programme. It was submitted to UNEP IE and edited for the
ICPIC diskette in August 1995. It has not undergone a
formal technical review.