CASE STUDY # 184
1. Headline: Reduction in the Oil Consumption in the
Synthetic Fiber Industry
2. Background: See below.
3. Cleaner Production Principle: Process modification
4. Description of Cleaner Production Application: This
technology involves equipment modification to reduce oil
consumption and hot air temperature.
Case Study Summary
Process and Waste Information: In the finishing steps of
manufacture of dissolving grade pulp, at Harihar
Polyfiber, the pulp is dewatered, flash dried, baled and
packed. The mechanical dewatering was done to about 38%
of dry content then the pulp was dried further to 70% of
dry content using hot air at 300 Degrees C, generated by
burning fuel oil.
In order to reduce the oil consumption and temperature of
the hot air, two dewatering booster presses were installed
in series after the existing dewatering presses running in
parallel. This improved the dryness of pulp to +50% and
the temperature of the hot air could be brought down to
200 Degrees C.
State of Development: The clean technology is fully
implemented.
Level of Commercialization: The clean technology is fully
commercialized.
Balances and Substitutions: Improvement in dryness
content of pulp by 50% and temperature of hot air is
reduced from 300 Degrees C to 200 Degrees C.
6. Advantages: Economic benefits were a savings of Rs. 3.5
million/year by reducing fuel oil consumption by about 14
kg/tonne of pulp. Furthermore, an improvement in pulp
quality resulted by avoiding the "burnouts" due to higher
temperatures of hot air. Environmental benefits include
reduction in fuel oil consumption.
7. Constraints: No information provided.
8. Contacts and Citation
Types of Source Material: Unpublished.
Citation and Industry/Program Contact and Address: Mr.
Shailendra Jain, Senior Executive President, Harihar
Polyfibers (GRASIM), Karnataka, India.
9. Keywords: India, textile, synthetic fiber, process
modification, ISIC 2299, oil, energy saving.
10. Reviewer's Comments: This case study was originally
compiled by the UNEP Working Group of Textiles. It
underwent a UNEP IE funded technical review in 1994 for
quality and completeness. It was edited for the ICPIC
diskette in July of 1995.
( Docno UNEP 11: DOCUMENT NOT AVAILABLE 11-27 )