INTERNATIONAL CLEANER PRODUCTION INFORMATION CLEARINGHOUSE

CASE STUDY # 163

1. Headline: Water Reduction and Wastewater Treatment in an

Electroplating Plant of Printed Circuit Boards

2. Background: See Below

3. Cleaner Production Principle: process modification

4. Description of Cleaner Production Application:

Technology Principle: This technology involves using

electrolysis and ion exchange to remove copper, spray

rinsing to reduce water usage, and treatment of

wastewater by neutralization and ultrafiltration.

Process and Waste Information: The process consists of

four lines, two of which contain an acidic copper bath, a

lead/tin bath, and spray or cascade rinse baths. The

third line is a stain bath with NH4OH and the rinse water

is returned to the bath. The fourth line is a mechanical

brush line, releasing heavy metal particles. Before 1980,

wastewater was sewered without treatment. It contained

5-8 mg/l of heavy metals, totally 160 kg/yr. Concentrates

were disposed as chemical waste by specialized companies.

In the new process, water reduction is achieved by

changing the rinse baths to cascade rinse baths, using

water from the cascade rinses for spray rinsing. The

spray water is transported to a wastewater treatment

installation.

The treatment begins by electrolytically recovering

copper. Copper particles from a mechanical brush line are

first dissolved by acids. Concentrations are decreased

from 300-400 ppm to approximately 10 ppm. A further

decrease in copper concentration is achieved by an ion

exchanger, reducing the copper content to less than 1 ppm.

Water containing heavy metals (only copper) in low

concentrations undergoes neutralization and

ultrafiltration. The sludge and concentrates are chemical

waste and disposed of by specialized companies. Water not

containing heavy metals is released without treatment.

Water use decreased by 15,000 m3/yr and 100-200 kg/yr of

sludge is produced. No new feedstocks were introduced and

no effects on product quality were reported.

Scale of Operation: The facility produces 100 m2/day of

printed circuitry and employees 5 people in the

electroplating department.

Stage of Development: The technology is fully

implemented.

Level of Commercialization: All equipment is widely

available.

Material/Energy Balances and Substitutions:

Material Category Quantity Before

Quantity After Waste Generation

(kg/yr):

Copper 160

1

Heavy metals unknown

negligible

Sludge 0 100-200

Feedstock Use: N/A N/A

Water Use (m3/yr): 25,000 10,000

Energy Use: N/A negligible

5. Economics

Investment Costs: Investment costs were Dfl 350,000 for

1980. Capital costs were 35,000 Dfl/yr.

Operational & Maintenance Costs: Costs were 9,000 Dfl/yr

for chemicals and 3,000 Dfl/yr for manpower.

Payback Time: The investment will not be paid back since

annual costs (Dfl 47,000) outweigh savings (Dfl 6,000 on

copper).

6. Advantages: Demands by water regulation authorities

prompted use of the measures. The facility now meets the

regulatory standards. Water usage has decreased by 15,000

m3/yr and copper levels in the wastewater have decreased

from 160 kg/yr to 1 kg/yr. Savings on copper were Dfl

6,000.

7. Constraints: It took 7-8 months (1.5 man-years) to

properly regulate the ultrafiltration system. No other

problems were encountered.

8. Contacts

Citation: Wastewater problems in the metal industry:

results of interviews in 48 companies). Dr. Ir W.H.

Rulkens, TNO, Maatschappelijke Technologie, postbus 342,

7300 AH Apeldoorn, Netherlands. TEL:(055)773344.

Industry/Program Contact and Address:

H.W. du Mortier

VOM

Jan van Eycklaan 2

Postbus 120

3720 AC Bilthoven

Netherlands

TEL: 31-30-287111

FAX: 31-30-287674

9. Keywords: the Netherlands, printed circuit board,

electroplating, ISIC 2113, electrolysis, ion exchange,

copper, ultrafiltration, heavy metal, rinsing, sludge.

10. Reviewer's Comments: This case study was originally

compiled by the UNEP IE Working Group on Metal Finishing.

It underwent a UNEP IE funded technical review in 1994 for

quality and completeness. It was edited for the ICPIC

diskette in July 1995.

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