CASE STUDY # 161
1. Headline: Use of Acid Purification Unit on Concentrated
High Temperature Pickling Liquor Reduces Iron
Concentration
2. Background: See below.
3. Cleaner Production Principle: new technology and process
modification
4. Description of Cleaner Production Application: This
technology involves the use of an acid purification unit
(APU) consisting of filters and an ion exchanger to reduce
iron content of the pickle acid.
Case Study Summary
Process and Waste Information: In the original pickling
process, no purification of the acidic liquor was
undertaken. The liquid was discarded in a continuous
"bleeding" process after the "bleed" was neutralized with
lime.
The new process involves use of equipment consisting of
three basic pieces and one optional piece: an Eco-Tec Acid
Purification Unit AP30-24 HT cartridge filter and ion
exchanger, a feed pump, an Eco-Tec sand filter and an
optional 400 gallon (1100 liter) water supply tank. The
pickle acid is pumped from the reservoir tank through a
media filter to remove dirt and oil particles. The acid
then passes through a second filter (0.5 m) to remove very
fine particulate and filter media from reaching the resin
bed in an ion exchange unit. The following stage contains
three steps per cycle: the water displacement stage, the
byproduct (iron) removal stage, and the produce (acid)
return stage.
The water displacement phase allows the pickle acid into
the resin bed, displacing the water from the previous
cycle. This water can be reused by sending it to the
water supply tank, or sent to drain. This stage lasts
approximately one minute.
The by product stage allows the pickle acid to continue
its flow through the resin bed trapping the sulfate ions
and allowing the iron to pass through and sent to drain.
This phase also takes about one minute.
The product return phase stops the flow of acid from the
reservoir and starts a counterflow of water from a
pressurized source (main water line or water supply tank
pump). The water picks up the sulfate ions and returns
them to the tank of sulfuric acid. This stage takes about
two minutes.
This three phase cycle continues automatically until the
dirt build-up in the media filter causes the process to
automatically shut down. A back flush procedure is
necessary to clean the filter before restarting the
system again. Backflushing time is approximately one
hour.
Using the new process results in the reduction of the iron
content of the acid solution from an initial 7.7% to a
steady 2-3% during the latter half of the test period. An
89% decrease in use of sulfuric acid and lime also
resulted. No new materials are introduced in the process.
Since pickling uniformity is a product quality
improvement, product quality is at least as good as before
using the APU, but this was not quantified.
Stage of Development: The installation is fully
implemented. Data are derived from the last month of
testing.
Level of Commercialization: The installation is fully
commercially available. The vendor seems well equipped
and experienced in construction and maintenance of the
equipment.
Material/Energy Balances and Substitutions:
Material Category Quantity Before Quantity
After
Waste Generation: N/A N/A
Feedstock Use:
Sulfuric acid 629,089 67,558
(lbs/yr)
Lime (tons/yr) 252 28
(Computed)
Water Use: N/A
N/A Energy Use: N/A
N/A
5. Economics
Investment Costs: Investment costs were as follows:
Design and supply of equipment
$84,000.00 Equipment installation
$10,000.00 Start-up, supplies, etc.
$ 2,500.00
Total
$94,000.00
These costs do not include the test program or the
management personnel costs for the project.
Operational & Maintenance Costs: These costs are
estimated at $2500/yr.
Payback Time: Payback time was calculated as 2.33 years.
Annual savings on chemicals were calculated as $43,937.
Not included in the calculations are an estimated $8,000
saved annually on sludge hauling.
6. Advantages: Annual savings on chemicals were $25,942 for
sulfuric acid and $17,995 for lime, or a total of $43,937.
An estimated $8,000 were saved on sludge hauling. The
project demonstrated that sulfuric acid used in preparing
steel strip for electrogalvanizing could be reclaimed for
continuous use.
7. Constraints: Except for some start-up problems, no other
problems seem to have been encountered.
8. Contacts
Name & Location of Company
Metal Koting
Continuous Colour Coat Ltd.
1430 Martin Grove Road
Rexdale Ontario M9W 4Y1
Canada
TEL 1 416 743-7980
Mr. M. Schulz
Head Training Section
Environment Canada
3439 River Road South
Ottawa, Ontario K1 OH3
Canada
TEL: 1 613 991-1954
FAX: 1 613 991-1635
9. Keywords: Canada, metal, iron and steel, pickling, new
technology, acid purification, ion exchange, pickle acid,
sulfate, acid.
10. Reviewer's Comments: This case study was originally
compiled by the UNEP IE Working Group on Metal Finishing.
It underwent a UNEP IE funded technical review in 1994 for
quality and completeness. It was edited for the ICPIC
diskette in July 1995.
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