INTERNATIONAL CLEANER PRODUCTION INFORMATION CLEARINGHOUSE

CASE STUDY # 146

1. Headline: Ultrasonic reactor cleaner reduces waste

generation and cuts energy costs are reduced.

2. Background: See below.

3. Cleaner Production Principle: process modification

4. Description of Cleaner Production Application: A Chemdet

Sonic Cleaning system is now used at 3-M to clean batch

reactors, replacing the old process of filling the reactor

with caustic or solvent and boiling the solution for one

or two days. Cleaning chemicals are pumped under pressure

through a twin-nozzled rotating spray head to break down

the waste. Then, caustic or solvent is sprayed under 600

lb pressure to complete the dissolution and flush the

vessel clean.

Material/Energy Balance and Substitution

FEEDSTOCKS: Solvent, caustic

WASTES: Spent solvent, caustic, containing adhesives,

resins, polymers

MEDIUM: Liquid

5. Economics

CAPITAL COST: $36,000

OPERATION/MAINTENANCE: Reduction in labor costs not

reported

MONTHS TO RECOVER: Savings realized in first year

DISPOSAL & FEEDSTOCK: $575,000 in first year, from labor,

materials and machine costs

6. Advantages

FEEDSTOCK REDUCTION: Reduced requirements for solvent and

caustic not reported

WASTE PRODUCTION: 1,000 tons/yr of water pollutants were

eliminated

IMPACT/PROBLEMS: Installation of the Chemdet system for

cleaning the reactors has eliminated the need to fill the

4,000-8,000 gallon reactors with solvent and caustic,

which greatly reduces the amount of spent solvent

generated. Significant savings were realized in the first

year.

7. Constraints: No information provided.

8. Contact and Citation: "Catalogue of Successful Hazardous

Waste Reduction/Recycling Projects", Energy Pathways Inc.

and Pollution Probe Foundation, prepared for Industrial

Programs Branch, Conservation & Protection Environment

Canada, March, 1987, page 19.

9. Keywords: United States, USA, chemical, process

modification, ultrasonic cleaning, ISIC 3700, solvent,

caustic.

10. Reviewer's Comments: This case study was originally

abstracted for the US EPA's Pollution Prevention

Information Clearinghouse from the Canadian publication

"Catalogue of Successful Hazardous Waste

Reduction/Recycling Projects." It underwent a UNEP IE

funded technical review in 1994 for quality and

completeness. It was edited for the ICPIC diskette in

July 1995.

( Docno unep05: 450-003-A-337 )