CASE STUDY # 140
1. Headline: Process modifications in a machine shop results
in savings.
2. Background: See below
3. Cleaner Production Principle: process modification
4. Description of Cleaner Production Application: A six tank
metal surface preparation (phosphating) and cleaning
process, a filtration system and a residuals concentration
process replaces a manual process, using acetone, for
removing surface oils from metal parts. The wiped parts
had been subsequently cleaned in three rinse tanks. The
new process uses counterflow to efficiently utilize the
rinse waters. The residuals are concentrated by liquid
evaporation and sludge concentration, using steam heat
from the boiler in the winter and a new gas boiler in the
summer. A distillation unit permits additional savings
through acetone and other solvent recovery and reuse.
Material/Energy Balance and Substitutions
FEEDSTOCKS: Water, acetone, chemicals
WASTES: Wastewaters, acetone
MEDIUM: Liquid
5. Economics
CAPITAL COST:
$38,967.68
OPERATION/MAINTENANCE: $500/yr
gas per boiler
MONTHS TO RECOVER: Not
reported
DISPOSAL & FEEDSTOCK:
$14,418/yr
6. Advantages
FEEDSTOCK REDUCTION: 45% reduction in acetone, 96% in
water, and 50% in chemicals
WASTE PRODUCTION: Reduced to less than 500 lbs/yr
IMPACT: The new metal fabrication system addresses
previous operational problems, reduces material costs, oil
accumulation, labor requirements, and residual waste
disposal costs. Hazardous sludge generation is reduced to
less than one 55 gallon drum.
7. Constraints: No information provided.
8. Contact and Citation: "Case Summaries of Waste Reduction
by Industries in the Southeast", Schecter, Roger N., Hunt,
Gary, July, 1989, Page 40.
9. Keywords: United States, USA, metal, machine shop,
process modification, cleaning, surface preparation,
filtration, rinsing, distillation, solvent, acetone, ISIC
3499.
10. Reviewer's Comments: This case study part of a core
collection of case studies from North Carolina, USA and
was originally abstracted for the US Environmental
Protection Agency's Pollution Prevention Information
Clearinghouse. It underwent a UNEP IE funded technical
review in 1994 for quality and completeness. It was
edited for the ICPIC diskette in July 1995.
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