INTERNATIONAL CLEANER PRODUCTION INFORMATION CLEARINGHOUSE

CASE STUDY #10 1. Headline: Waste reduction in steelwork painting 2. Background: In the 'Ostrowiec' Steelworks the manufacture of steel products is carried out using production-line methods. The final operations required for almost all products are surface treatment and painting. In the Machinery Building Department these operations are carried out with shot-blasting machines and manually operated spray booths. The original painting method was air-atomized spraying which has the lowest transfer efficiency of the coating methods and yields large quantities of waste. The 'Ostrowiec' Steelworks consist of eleven Departments, the main production departments are Steelworks, Processing, Steel, Construction, Machinery Building and the Foundry. 3. Cleaner Production Principle: Process modification 4. Description of Cleaner Production Application: A pollution prevention audit was carried out to improve the environment and efficiency and working conditions in the painting areas. The objective of this program was to reduce the quantity of wastes and costs of painting by a combination of improvements to the technology and good housekeeping. The overall aim was to improve the quality of coating, to reduce the amount of paint raw material and to reduce the quantities of wastes. The existing painting method was compared with two more advanced painting technologies. The transfer efficiency for the different methods are as follows: air-atomized spray (conventional) 30-50% airless spray 65-70% pressure atomized electrostatic spray 85-95% In conventional spraying compressed air is used both to atomize the paint and carry it to the surface to be painted. With airless spraying the paint is pumped under high pressure to a small jet where the high velocity is sufficient to induce atomization. The lack of any expanding compressed air stream eliminates unwanted spray mist, reduces the loss of paint by overspray and most of the paint adheres to the work surface. With pressure atomized electrostatic spray, paint is delivered at high pressure as before, but is fed to a insulated nozzle. An electrostatic charge of about 100kV is applied to this nozzle. The charging of the paint particles assists the atomization and causes them to repel each other. Additionally the charged paint moves along the field lines to the earthed work piece. As the electrostatic field lines envelop the object the paint particles cannot fly straight past, but 'wrap' themselves uniformly around the surface. It is this effect that gives high paint efficiency and reduces waste. Note that electrostatic hand spray guns require a small mains transformer and a very reduced current to avoid accidental electrical shock. Tests carried out with the two improved painting methods showed the following results: Comparison of raw material consumption and waste quantities of the different methods: Air-atomized Airless Pressure spray spray atomized electrostatic spray Paints 8.0 m3 6.8 m3 5.6 m3 Solvents 6.5 m3 1.6 m3 1.6 m3 Wastes 2,400 kg 1,400 kg 500 kg 5. Economics: (Estimates, based on Trials) Airless spray Pressure atomized electrostatic spray Cost saving US$/year Total savings 38,500 39,400 Capital investment US$4,800 US$13,000 Payback period1.5 months 4 months 6. Advantages: Reduction of high disposal costs. Reduced running costs. Decreased financial liability by generating a smaller quantity of hazardous wastes. Improved public perception and acceptance in the business community. Also indicated were potential reductions in the effluent concentrations of about 45% for sludge and 75% for organic solvents. 7. Constraints: N/A 8. Contacts:Mrs Lucyna Chrzanowska Steelworks 'Ostrowiec' ul Swietokrzyska 8 27-400 Ostrowiec Swietokrzyski Poland Tel: +48 472 528 81 Fax: +48 472 512 34 Telex: 0612581 hn pl 9. Keywords: Poland, metal, iron and steel, painting, process modification, electrostatic spray, airless spray, raw material saving 10. Reviewer comments: This case study was originally published in the UNEP IE document "Cleaner Production Worldwide". In the process of preparing the document the case study underwent a technical review.