Ohio Environmental Protection Agency Pollution Prevention Section Division Of Hazardous Waste Management SEPTEMBER 1992 --------------------------------------------- Acknowledgements This document was prepared under a federal fiscal year 1992 Resource Conservation and Recovery Act (RCRA) grant from U.S. EPA to Ohio EPA, Division of Hazardous Waste Management. We are grateful for the assistance of all the companies that shared their success stories with us and the individuals responsible for submitting the information and answering our many questions. We would also like to thank those who referred us to companies that had successfully implemented pollution prevention/waste minimization in their facilities. Pollution Prevention Section Division of Hazardous Waste Management Ohio Environmental Protection Agency Columbus, Ohio 614/644-3469 September 1992 --------------------------------------------- INTRODUCTION AND SUMMARY Pollution prevention case studies provide a valuable reservoir of information to business, government and the public. By detailing specific actions taken by facilities, case studies provide examples to other companies of changes they can implement to reduce their own pollution generation. Case studies also demonstrate that waste minimization/pollution prevention works. It reduces waste generation while providing numerous benefits to a company, including cost savings, improved worker protection and public relations, reduced liability and environmental protection. As specified in the Resource Conservation and Recovery Act (RCRA) grant to the Division of Hazardous Waste Management (DHWM), for fiscal year 1992, the Ohio EPA developed a Hazardous Waste Minimization and Pollution Prevention Case Study Form based upon U.S. EPA's Pollution Prevention Case Study Format. This form was widely distributed in order to obtain the thirty-one hazardous waste minimization and pollution prevention case studies in this report. In response to U.S. EPA's interest in focusing on the Great Lakes, the Lake Erie basin of Ohio was used for the geographic focus for this report. Keywords at the end of each case study in this report facilitate indexing for easy referral for specific purposes, waste streams, pollution prevention activities and other issues. The case studies come from a variety of industries and cover a variety of processes. Each company included in its submission one or two SIC codes that best describe the industry segment or segments referenced by the case study, as listed below in Table 1. Table 1. [see original hard copy of document] Over forty projects are discussed in the case studies, some involving more than one activity and some involving both source reduction and recycling. The majority of the activities involve source reduction practices. Many of the source reduction activities affected degreasing or cleaning operations. The chemical mentioned most often was 1,1,1-trichloroethane (TCA). The use of TCA was reduced in some instances and eliminated entirely in others. The industries cited a number of benefits gained and the public, improved worked environment, improved employee and public relations, reduced requirements and reduced liabilities. One industry, Perfection Finishers, Inc., stated that the decision to eliminate use of TCA was made in part because the solvent was increasingly becoming a target of health agencies and the Ohio EPA. It took several of the industries some time and several tries to find an appropriate substitute for this solvent. Substitutions in cleaning and degreasing operations were also found by three companies for chlorinated solvent blends, tetrachloroethylene and chlorinated hydrocarbons. Painting processes were affected by source reduction almost as much as degreasing and cleaning were. All nine companies that changed a painting operation through source reduction practices made a raw material substitution to a less toxic or hazardous paint. Four of these were to powder coatings. The Automatic Welding and Manufacturing Company, one of the companies that made both raw material and equipment changes, began using a high solids paint and airless paint guns instead of conventional guns. This not only generated less sludge, but also increased production rates and decreased energy usage. Diebold, Inc., found a paint supplier that would provide small amounts of custom paint, reducing the quantity of unused paint. Other source reduction activities range from very large projects to smaller projects. For example, BP Chemical, Inc., decided to build a new facility to reduce NOx emissions rather than implement a great number of changes in an old facility. Several changes at the Eveready Battery Company were smaller in scope. Eveready is in the process of changing to a water based adhesive in order to eliminate the use of TCA in an adhesive. The number of mineral spirit tanks and the solvent and the solvent changing frequencies have been reduced, and squirt and spray bottles containing solvent have been eliminated. Improved operating practices such as these were implemented in several other companies to reduce their waste. Kovatch Castings Company reduced TCA emissions by ensuring that a drum of TCA remained covered when not in use, and by limiting employee access to the solvent. Improved housekeeping at the Lincoln Electric Company facilitated recycling of barium and manganese. Plasticolors, Inc., improved production scheduling at its facility so that different colors of product were processed in a specific sequence. Source reduction at other companies was achieved through process and equipment changes and raw material substitution. Often these changes occurred in combinations or in conjunction with recycling practices. Dietrich Industries, Inc., implemented both mechanical changes to a washer and ultrafiltration and reuse of spent chemical solution. This combination has significantly lowered disposal costs and reduced chemical use. Like most of the recycling activities described in this report, Dietrich's recycling is performed onsite. In one example of offsite recycling, Walbridge Coating Company sends a zinc/nickel sludge to another company for feeder stock, and in return receives the mixed metals carbonate generated from this material for use as a raw material in one of their own processes. There is great variety in the recycling practices in this report. Some affect waste water discharges, some metal waste, some solvent or coating waste. Most were implemented with low capital costs, although even the more costly recycling activities tended to lead to cost savings. Other benefits of the recycling activities include improved quality of parts, reduced hazardous waste transportation and disposal costs, reduced liability, energy and resource conservation and improved public relations. Some activities were more difficult to implement than others, requiring the assistance of several other companies or a great deal of trial and error before material could be properly reclaimed. All companies were requested to list obstacles, problems and known constraints. Problems encountered at the beginning stages of implementation included high capital costs, the difficulty of finding replacement materials that worked as well as original materials and the time necessary to "fine-tune" new processes and train personnel to use them. Once changes were implemented and employee resistance overcome, some companies found that new methods needed more attention than old methods or had inherent problems that might limit use. In some instances, specific detail has been provided. Companies that used offsite recycling were concerned about finding and keeping a constant market for the recycled material. One very specific barrier was mentioned by the Luke Engineering and Manufacturing Company, which has a company goal to eliminate the use of chlorinated hydrocarbons. It must degrease some parts with TCA because of military specifications. Several case studies refer to the U.S. EPA 33/50 Program. This is a voluntary pollution prevention initiative to reduce national pollution releases and off-site transfers of seventeen toxic chemicals by 33% by the end of 1992 and 50% by the end of 1995. U.S. EPA is asking companies to examine their own industrial processes to identify and implement cost-effective pollution prevention practices for these chemicals. These case studies document the efforts of Ohio companies to benefit both the environment and themselves. They have overcome obstacles and barriers to achieve this, and are willing to let others benefit from their experiences. We believe these companies are helping to set the standard for pollution prevention and waste minimization in Ohio. They should be applauded for their outstanding efforts. HOW CASE STUDIES WERE OBTAINED The Pollution Prevention Section (PPS) of Ohio EPA obtained these case studies from February through July, 1992. A variety of approaches was used to attempt to obtain as many case studies as possible. These included: (1) mass mailings of a letter and case study form to all hazardous waste generators and Toxics Release Inventory reporters (approximately 3,000 mailings); (2) a mailing with the Ohio Toxics Release Inventory form for 1991 reports; (3) telephone calls to facilities that were known to the Pollution Prevention Section to have some activity that might have been useful for a case study; (4) about 50 personalized letters to manufacturers; (5) advertising through business organization newsletters, including those of the Ohio Chamber of Commerce, the Printing Industry of Ohio and the Ohio Chemical Council; and (6) advertising in the Northeast Industrial Waste Exchange "Listings Catalog" and two Ohio EPA newsletters ("New(s) Source" and "Airlines"). A tracking system was established to follow the requests for case study information and produce revisions. Ohio EPA initially solicited case studies using a complete, revised copy of U.S. EPA's Pollution Prevention Case Study form (see Appendix A). It was eight pages long and was seen by facilities as too time consuming and difficult to complete. The initial mailing received very limited response. An abbreviated form was substituted (see Appendix B). The deadline for submissions was extended, and the staff of the Ohio EPA PPS called many facilities individually and requested case studies. Many of the contacts from the facilities expressed an interest in the project but stated that they simply did not have the time to prepare a submission. This problem was intensified by July as many contacts said they were too busy because they were attempting to complete the U.S. EPA Form R, which they had just received. In an effort to encourage facilities to submit their success stories, contacts were told that submission could be made over the phone or in a report format. PPS staff wrote or re- wrote these submissions in accordance with the abbreviated format. The combination of a limited response to requests and the rejection of some case studies received led to the eventual number of case studies in this report that was less than the original goal of 50. The Pollution Prevention Section rejected several case studies that were not appropriate for this report, such as those that did not include hazardous waste minimization or toxics pollution prevention. Some dealt only with solid waste. A few companies called the PPS after submitting a case study and requested that it not be used because upper management was reluctant to have the information published. Many of the case studies were either too vague or not sufficiently quantified to be usable, and the contacts were unable or unwilling to provide more detailed information. Other contacts were quite helpful and provided additional detail over the phone or by a follow up letter to PPS. All case study suppliers were sent draft copies of the final version of their facility's case study. Ohio EPA requested permission to revise and use the case studies in this report, and permission was granted. All companies voluntarily provided this information. Mention of a company in this report does imply endorsement by the Ohio EPA. [ POSSIBLE TYPO ERROR IN ORIGINAL: SHOULD THE LAST SENTENCE MAYBE SAY "DOES NOT IMPLY ENDORSEMENT" ? ] Ohio EPA will use these case studies to publicize the accomplishments of Ohio businesses in waste minimization and pollution prevention. Among other uses, they will be submitted to the U.S. EPA for inclusion in the case studies found in the Pollution Prevention Electronic Information Exchange System (PIES) of the Pollution Prevention Information Clearinghouse (PPIC). For more information, contact the persons listed with each case study, or contact the Pollution Prevention Section, Division of Hazardous Waste Management, Ohio EPA, P.O. Box 1049, Columbus, Ohio 43266-0149, 614/644-3469. [ POSSIBLE TYPO ERROR IN ORIGINAL: P.O. BOX IS 1049, ZIP CODE EXTENSION IS 0149 -- THESE 4 DIGITS SHOULD MATCH! ] POLLUTION PREVENTION CASE STUDIES Adelphia, Incorporated Cleveland 1.0 Headline A paint process modification was implemented to switch from solvent based to water based paint, reducing the amount of air emissions. A non-hazardous water based cleaner is now being used for degreasing. 2.0 SIC Code 2851 3.0 Name and Location of Company Adelphia, Inc. 15657 Brookpark Road Cleveland, Ohio 44142 4.0 Clean Technology Category Process and equipment modifications were implemented to reduce air emissions and hazardous waste generation. 5.0 Case Study Summary Adelphia, Incorporated, coats products for industries. In 1989, Adelphia started changing as many paints as possible from solvent based material to water based material. This has reduced the plant's air emissions substantially. In addition, it has completely eliminated one solvent. Adelphia is currently using a non-hazardous, water soluble cleaner for degreasing of parts before painting. This has reduced the amount of hazardous waste generation. This new process works better than the old method of hot caustic cleaning. Adelphia is currently using an acid detergent. They are also experimenting with a new product for use on their phosphate line, which would replace a caustic cleaner. This product is a non- hazardous organic acid. 6.0 Economics The economic benefits include the decreased amount of hazardous waste. This has lowered hazardous waste disposal costs. At this time no further information is available. 7.0 Cleaner Production Benefits The Adelphia facility in Cleveland has reduced air emissions from the use of water based paints. The total amount of hazardous waste generated will continue to decrease because the degreasing operation is using a water based degreaser. 8.0 Obstacles, Problems and/or Known Constraints None mentioned 9.0 Date Case Study was Performed 1989-1992 10.0 Contacts with Citations Adelphia, Inc. 15657 Brookpark Road Cleveland, Ohio 44142 Mr. Fred Payton, Plant Manager 216/267-0570 11.0 Keywords 503 Halogenated (e.g., chlorinated) solvents 800 Organic gases 2030 Degreasing 2097 Painting 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 1008 Treatment/disposal costs avoided ---------------------------------------------------------- Air Products and Chemicals, Inc. Cleveland 1.0 Headline Seal pot water is recovered and reused in another process, reducing wastewater discharges. 2.0 SIC Code 2821 3.0 Name and Location of Company Air Products and Chemicals, Inc. 6626 Union Avenue Cleveland, Ohio 44105 4.0 Clean Technology Category A simple process modification was made which took a waste stream from one process and put it into a raw material supply for another process. 5.0 Case Study Summary Two primary processes exist at the Air Products and Chemicals Incorporated facility in Cleveland. The first is a batch polymerization of vinyl acetate to form a solid polymer and the second is a continuous polyvinyl acetate emulsion process. The pollution prevention example involves a modification to each process. This modification reduced vinyl acetate containing waste water discharges to the local publicly owned treatment work (POTW) by approximately 56%. The batch process reactor has a seal pot used to eliminate vapor emissions of vinyl acetate. The seal pot has a continuous water purge. Before the process change, this water was sent directly to the POTW during a batch. No water is required when the reactor is idle. Two of the raw materials for the continuous emulsion process are water and vinyl acetate. The process change routed the batch process seal pot water directly to the continuous process as a raw material feed where the vinyl acetate is converted to a saleable product. The change had no impact on the production rates for either process and had no adverse impacts on product quality. The facility in Cleveland, which is usually in operation five days per week, produces approximately 28 million pounds of vinyl acetate based polymers annually. Superfund Amendments and Reauthorization Act (SARA) Toxics Release Inventory (TRI) reportable emissions for calendar year 1990 for the facility were 19,650 pounds. The pollution source reduction described above was completed in October of 1991. The quantitative information is based on engineering estimates. The only materials required to complete the change were readily available piping and valves. 6.0 Economics The entire process change cost less than $1000 to install. Standard stainless steel tubing and valves were used. Approximately $2000 per year will be saved in operational costs as a result of implementing the process change. The payback period will be approximately six months. 7.0 Cleaner Production Benefits The pollution source reduction provides economic benefits as described above as well as improved public relations through reduced TRI reportable emissions. 8.0 Obstacles, Problems and/or Known Constraints No significant problems or obstacles were encountered. 9.0 Date Case Study was Performed The opportunity for the pollution source reduction was identified in August 1991 and was fully implemented in October 1991. 10.0 Contacts with Citations Air Products and Chemicals, Inc. 6626 Union Avenue Cleveland, Ohio 44105-1384 Mr. Douglas Miller, Plant Manager 216/883-7494 11.0 Keywords Other liquid waste 2049 Emulsification 2110 Polymerization 02 Process modification or substitution 04 Process raw materials modification or substitution 1002 Annual cost savings 1003 Capital costs 1005 Payback period ---------------------------------------------------------- Automatic Welding and Manufacturing Company Ashland 1.0 Headline Through the equipment change of updating paint guns to airless guns, and the substitution of high solids paints, hazardous waste generation has been reduced. All paint thinner is recycled and reused on site, with any residual thinner disposed of as hazardous waste. 2.0 SIC Code 3499 3.0 Name and Location of Company Automatic Welding and Manufacturing 532 County Road 1600 Ashland, Ohio 44805 4.0 Clean Technology Category Process equipment modifications and raw material substitution in the painting operations were implemented to reduce the amount of hazardous waste generated. Paint thinner is recycled and reused on site, also reducing the amount of hazardous waste generated. 5.0 Case Study Summary As a "job-shop" fabricator. Automatic Welding and Manufacturing Company builds a variety of products based on customer specification. Hazardous waste is generated in the paint areas. Painting was originally done with conventional paint guns and high volatile organic compound paint. This generated a large amount of paint sludge which was classified as a hazardous waste. Paint guns were replaced with airless guns, and use of high solids paint was implemented. These changes reduced the amount of sludge generated. Some hazardous waste is generated as residual paint thinner, but most thinner is recycled on site and reused. Production rates have increased because less time is spent in the paint booths to do the same work. Energy usage has decreased because the new guns are airless. Training of employees was necessary not only to enable them to use the new equipment, but also to foster an attitude of pollution prevention. Automatic Welding and Manufacturing employs approximately eighty- five people. The scale of operation depends on customer requirements. When painting, the facility uses about 100 gallons of paint a day. The plant has achieved approximately 80% of the project that was initially planned. A limited number of conventional paint guns are still in use. Little equipment had to be special ordered, because almost everything was readily available through vendors. 6.0 Economics Approximately $20,000 has been invested at this point. Operational and maintenance costs have not been evaluated, but a payback time of one year is expected. 7.0 Cleaner Production Benefits Automatic Welding and Manufacturing has realized economic benefits through reduced hazardous waste treatment costs. Improved public relations are expected. Liability has been reduced. Changes in the painting processes have enabled the company to change from a small quantity generator to a conditionally exempt small quantity generator, and have made compliance more attainable. 8.0 Obstacles, Problems and/or Known Constraints The only difficulty involved in implementing the pollution prevention techniques was the time factor involved in training employees to use the new equipment and fostering an attitude among the employees that would encourage good implementation of these changes. 9.0 Date Case Study was Performed Changes in the painting process began in January 1992, and are not yet complete. 10.0 Contacts with Citations Automatic Welding and Manufacturing 532 County Road 1600 Ashland, Ohio 44805 Mr. Wayne Wilfong 419/281-2808 No external material was used except for vendor information. 11.0 Keywords 604 Organic paint sludge 511 Paint thinner or distillates 2097 Painting 01 Equipment or technology modifications 02 Process modification or substitution 04 Process raw materials modification or substitution 07 On-site recycling or recovery for reuse 1002 Annual cost savings 1005 Payback period Regulatory incentives ---------------------------------------------------------- BP Chemicals, Incorporated Lima 1.0 Headline Replacing an old facility with a new facility will reduce air emissions by approximately 2,000 tons a year of NOx, recover the nitrogen oxides and turn them into a sellable product. 2.0 SIC Code 2819 3.0 Name and Location of Company BP Chemicals, Inc. Ft. Amanda and Adgate Road P.O. Box 628 Lima, Ohio 45802 4.0 Clean Technology Category Process and equipment modifications are being implemented to recover NOx from air emissions. 5.0 Case Study Summary BP Chemicals-Lima currently owns and operates a nitric acid production facility at Ft. Amanda and Adgate Roads. The current nitric acid production facility has been in operation since 1955, and continues to produce nitric acid within customer specifications. The operating rate of the current plant exceeds the nameplate capacity of 180 tons per day by roughly 10%. Over the past several years, due to improvements to the process, production records have been set due to high customer demands. Uses of nitric acid include fertilizers, metals treatment, dye/pigment production, explosives and wastewater treatment. The existing plant is currently permitted as an air point source under the Ohio Air Pollution Control Regulations. The average emission rate as stated in the permit is 425 pounds per hour of NOx. The plant is equipped with a fume burner as a control device which chemically oxidizes nitrogen dioxide to nitric oxide. During the startup period, the plant has received complaints of a visible red plume when the fume burner is brought on-line. Although nitric acid plants are listed in federal regulations as subject to New Source Performance Standards (NSPS), this particular plant has been grandfathered and is not subject to those regulations. The federal NSPS standard for nitric acid plants is three pounds per ton of acid. The current plant in Lima operates at 57 pounds per ton of acid. BP Chemicals performed an economic evaluation to assess the feasibility of constructing a new nitric acid plant to replace the existing plant. The economic evaluation indicated that the construction of a new plant could be a profitable venture. In addition, the opportunity to carry out a major environmental upgrade at the BP-Lima facilities was an important consideration in the project. The project was approved and funds were allocated for the new facility. The new nitric acid production facility has been designed to integrate the latest technology with respect to product recovery and reduction of by-products. Techniques which are incorporated into the design include higher pressures, the use of chilled water and modified absorber design, all of which improve recovery of nitrogen oxides to nitric acid. In addition to the emissions reduction gained through the inherent efficiency of the process, a NOx abatement system was also included in the design. The abatement system will use the most current commercially available technology for NOx reduction. Selective catalytic reduction was chosen as the best available control technology. This technology utilizes a catalyst bed to react ammonia and NOx. The products of this reaction are intermediate salts which decompose into elemental nitrogen and water which exit through the vent stack. The new plant will result in a 95% reduction of NOx versus the old plant. Improved production methods such as those mentioned above account for 80% of the reduction while the selective catalytic reduction unit accounts for the remaining 15%. As evidenced by these figures, the bulk of the reduction is being gained through the design and operation of a highly efficient production facility. Water discharges from the current as well as the new nitric acid plant consist solely of clean water streams (cooling water, boiler feed water, and steam condensate). The new plant will produce 270 tons per day of nitric acid which is a 50% increase in production over the current plant. The water use and discharge, however, will remain the same due to improvements in heat recovery. Heat generated in the process is used to produce steam which is used elsewhere in the plant. Improvements in heat recovery allow the generation of more steam, while cooling water use is decreased. The emission reduction from the new plant will make a significant reduction in the air emissions inventory of the BP-Lima plant and in Allen County. The shutdown of the old plant and subsequent startup of the new plant will result in a 45% reduction in NOx emissions from the BP-Lima complex. This reduction corresponds to a 22% decrease in NOx emissions in Allen County. The emissions reduction is approximately 2000 tons per year or 4,000,000 pounds per year. The concept of waste reduction and pollution prevention has been actively practiced at BP Chemicals-Lima. Research efforts have been conducted both on and offsite to improve process operation by producing more product per unit of raw material and less waste. In addition to these efforts, the BP-Lima management is actively committed to waste reduction across each media. Several critical operating parameters have been compiled since the startup of the nitric acid plant. The attached Figure 1 depicts the wastewater generation per unit of production at the plant at the Lima site. As can be seen, wastewater generation per pound of product has dropped roughly 40% over the last thirty years. Figure 2 shows the raw material requirement in terms of pound of propylene required for each pound of acrylonitrile produced. The lower this ratio, the less unreacted propylene that is discharged in the waste gas stream. The ratio has also dropped by roughly 40% over the last thirty years. Air emissions at the Lima site have received a good deal of attention in terms of reduction efforts. Figures 3 and 4 depict the reported emissions from the BP-Lima plant site. Figure 3 shows the reduction of the Superfund Amendments and Reauthorization Act Toxic Chemical Release air emissions which are reported annually. These air emissions have been reduced by more than half since the reporting was put into effect. Figure 4 shows the emissions levels of the criteria pollutants from the BP-Lima site. From 1987 to 1989, a reduction of 50,000,000 pounds per year of carbon monoxide and hydrocarbon emissions has been achieved. Following these two pollutants, the next largest criteria pollutant is NOx. The new plant will reduce the existing emission level by 4,000,000 pounds. BP Chemicals will continue to pursue these reductions and reduce the waste generation through source control and waste minimization. 6.0 Economics The decision to commit the capital funds to construct a new facility was based on economic analysis. Despite the enormous environmental benefit, a voluntary project of this magnitude must be economically sound with respect to cost and payback. The economic analysis showed that the current market conditions and expected revenue could support the decision to build a new facility. Allocation of $17,000,000 for the new plant was made. Three major factors which made the project profitable were the current market conditions, increase in production, and decrease in the unit production costs. The economic payback period is calculated at between three to four years. 7.0 Cleaner Production Benefits The primary benefits from the completion of this project are economic and environmental. Economic benefits include increased profitability and higher plant reliability. Economic benefits to the community include increased spending for goods and services by BP Chemicals throughout the local economy during the construction, and an improvement of the infrastructure of the BP Chemicals facility which is a major employer in the community. Environmental benefits include the reduction in NOx emissions by 4,000,000 pounds. 8.0 Obstacles, Problems and/or Known Constraints No technical obstacles are anticipated in the construction and implementation of the new plant. This is primarily due to the use of proven technology in order to achieve the emission reduction. 9.0 Date Case Study was Performed Construction of the plant is currently underway. Start-up is scheduled for the fourth quarter of 1992. 10.0 Contacts with Citations BP Chemicals, Inc. Ft. Amanda and Adgate Road Lima, Ohio 45804 11.0 Keywords 400 Inorganic gases 2014 Chemical manufacturing 01 Equipment or technology modification 02 Process modification or substitution 1002 Annual cost savings 1003 Capital costs 1005 Payback period [four pages of graphs, Figures 1 through 4] ---------------------------------------------------------- City Machine and Wheel Company Stow 1.0 Headline A conventional wet paint coating operation was changed to a dry powder, state-of-the-art coating system. 2.0 SIC Code 3499 3.0 Name and Location of Company City Machine and Wheel Company 1676 Commerce Drive Stow, Ohio 44224 4.0 Clean Technology Category A process modification, equipment modification and raw material substitution occurred when City Machine and Wheel Company (CMW) completely changed over to a dry powder system. 5.0 Case Study Summary CMW employs an average of 105 people with as many as 136 during their peak season. The majority of the work is welding, painting and mounting tires on wheels for lawn and garden and recreational vehicle industries. With the process change CMW will have some changes in their regulatory compliance. They will no longer have to report under current regulations and will no longer have to file a report using an EPA form R. Wastewater discharge from the prewash system goes to the Akron publicly owned treatment work and is periodically tested by the Summit County Environmental Services. CMW will weld, paint, and mount approximately 1,500,000 wheels in 1992. The addition of the powder paint line system has eliminated hazardous waste generation. The powder paint line system is new technology that is commercially available, although it has been tailored specifically to the needs of CMW and their industry. The previous system used a one-time spray. All overspray was hazardous waste paint sludge. Liquid paint was replaced with dry powder which can be reused and does not require solvents for cleanup. Xylene recycling was eliminated from the old system. A reclamation system for used paint enables powder to be reused. The wet painting system was a chain on edge conveyor system which held one part per spindle. The paint spray boot consisted of a trip switch actuated spray gun table to follow the parts being painted. Eight spray guns were attached to cover all sizes of wheels. The cure oven was an electric infra-red oven, which was very costly to run. All parts were hand cleaned before being placed on the line. Paint was sprayed onto the parts, and overspray from the painting operation was caught in a waterfall booth where the paint was detackified and separated from the water. This operation could paint a maximum of approximately 7,000 parts per 24-hour time period. Emissions to the atmosphere occurred during the painting operation in the paintbooth, and in the cure oven as the parts were cured. Cleanup was done with xylene which was recycled according to EPA regulations. Components of the leftover paint sludge had to be reported under Form R of the Toxics Release Inventory, and the sludge was very costly to dispose of. All paint was low volatile organic compound paint. Xylene, used as a paint thinner, was reported to the EPA using Form R. The new powder paint line system is a conveyor system able to hold multiple parts and sizes together. The parts pass through an electrostatic charged cloud of paint powder which is attracted to the metal part. All paint which does not adhere is reclaimed and can be reused, eliminating paint sludge and hazardous waste. The wheels pass through a five-stage wash system which cleans and treats the steel surface minutes before painting. The parts are cured in a gas fired oven which is more cost efficient to operate. This operation has a maximum of approximately 13,000 parts per eighteen hour time period. All hydrocarbon solvent air emissions were eliminated with this new process. Cleanup is simply done with a broom, a shop vac and water. The leftover scrap paint is non-hazardous and non-regulated material. The only monitoring now required is due to the addition of the wash system. CMW must be within environmental standards for wastewater when it cleans out the holding tank. Before the wet paint line system was put into place the hazardous waste generated was 85,100 pounds per year. No hazardous waste is generated with the new painting process. The training and supervision of this area with the new system is more critical than with the previous system. The final end product quality has improved. The housekeeping and cleanup under the new project is far easier compared to the previous wet paints. Housekeeping has gone from washing parts in solvents to using a squeegee and water for cleanup. 6.0 Economics The cost to install the powder paint line system was approximately $500,000. The cost savings have been calculated at about 20% on utilities. The payback period for this system is estimated to be two years. 7.0 Cleaner Production Benefits With the addition of the powder paint line system, CMW has eliminated hazardous waste disposal costs and recycling costs. Together these costs average $52,000 per year. EPA regulatory paperwork and reporting time will be eliminated. Shutting down the paint line to clean out the waterfall spray booth is no longer necessary. This will add two to three more shifts of production time per month. CMW has improved public relations by eliminating hydrocarbon air emissions into the atmosphere. In addition, CMW will have reduced liabilities concerning the shipment of hazardous waste off-site. With the installation of this system, production planning was made easier because of the capability of CMW to paint larger volumes of parts of the same color regardless of size. In the past, the wet system was very limited as to what could be done with different part sizes or configurations requiring a new setup for each. The need for a hazardous waste storage area has been eliminated along with all paperwork requirements. 8.0 Obstacles, Problems and/or Known Constraints Few obstacles were encountered during startup and construction of the system. Since the technology was new to everyone at CMW, employees needed time to learn how to operate the new system. The only real obstacle encountered during the first ten months of operation was a high buildup of zinc in the holding tanks of the prewash system. With the help of Summit County Environmental Service contacts, CMW is currently in the process of correcting the problem at the time of this report. 9.0 Date Case Study was Performed The powder paint line went into limited testing production in June of 1991. Total production went into effect as of October of 1991. 10.0 Contacts with Citations City Machine and Wheel Company 1676 Commerce Drive Stow, Ohio 44224 Mr. David Sebastian 216/688-7756 11.0 Keywords 503 Halogenated solvents 511 Paint thinner or petroleum distillates 604 Organic paint or ink sludge 800 Organic gases 2097 Painting 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 1002 Annual cost savings 1003 Capital costs 1005 Payback period Regulatory incentives ---------------------------------------------------------- Cleveland Wood Products Cleveland 1.0 Headline Source reduction techniques reduced volatile organic compound emission from a painting operation. 2.0 SIC Code 3991 3.0 Name and Location of Company Cleveland Wood Products 3881 West 150th Street Cleveland, Ohio 44111 4.0 Clean Technology Category Process and equipment modifications and a raw material substitution were implemented to reduce the amount of volatile organic compound (VOC) emissions from a painting operation. 5.0 Case Study Summary Cleveland Wood Products is a small company with less than 100 employees that designs and manufactures brushes for the vacuum cleaner industry. Eighty-five percent of the brushrolls produced are wooden and require spray painting prior to bristling. In January of 1987, Cleveland Wood Products began evaluating their paint spraying operation in order to reduce liability insurance premiums. The company realized that it could potentially reduce air pollutants and eliminate the risk of spills to prevent environmental problems by switching paint systems. The old paint system was electrostatic lacquer and was mixed on site. It was Cleveland Wood Product's desire to convert to water based paints to eliminate VOC pollution. However, water based paint suitable for wood was not available to meet the company's requirements. As an interim move to reduce VOC emissions, Cleveland Wood Products converted to enamel spray in 1988. A new stainless steel air operated enclosed paint delivery system was installed using closed drums with air operated mixer paddles. The paint vendor delivered a small quantity of paint every third day, eliminating on-site storage. Pre-mixed paint eliminated thinners and possibilities of accidental spills. The use of enamel also significantly reduced the amount of VOC's emitted. At the same time three paint manufacturers were asked to develop a usable water based paint for wood. Initially the major paint manufacturers did not address the company's need for a water based paint because of their small size and the limited potential for wood applications. Throughout 1989 and 1990, water based paints were sampled but failed because of an inability to cover or dry to touch in a short amount of time. In late 1991, a modification of Cleveland Wood Products automatic paint line was made which directed overspray onto the product instead of onto the filters. This was a significant quality, cost improvement. An acceptable water based paint was approved on May 1, 1992, and went into use by July 1992. Emissions from this paint are significantly below all EPA VOC emission standards. 6.0 Economics Water based paints cost more per gallon, but pieces painted per gallon has increased. 7.0 Cleaner Production Benefits The net result of this effort is protection of the environment as well as cost reductions enhancing the company's competitive position. It has also spawned awareness and organized efforts to further reduce the source of waste throughout Cleveland Wood Product's operation. Efforts are not only supported but encouraged by all employees. In addition, facilities and equipment are cleaner and easier to maintain. 8.0 Obstacles, Problems and/or Known Constraints None mentioned 9.0 Date Case Study was Performed 1989-1992 10.0 Contacts with Citations Cleveland Wood Products 3881 West 150th Street Cleveland, Ohio 44111 Mr. Ronald R. Varesco, General Manager 216/252-1190 11.0 Keywords 511 Paint thinner or petroleum distillates 604 Organic paint or ink sludge 800 Organic gases 2097 Painting 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 09 Management strategies 1002 Annual cost savings ---------------------------------------------------------- Copeland Corporation Wapakoneta 1.0 Headline Replacement of 1,1,1-trichloroethane cleaning solvent with a petroleum distillates product and replacement of xylene based paint with powder coating has resulted in substantial cost savings. 2.0 SIC Code 3585 3.0 Name and Location of Company Copeland Corporation 751 Industrial Drive Wapakoneta, Ohio 45895 4.0 Clean Technology Category Equipment and process modifications were implemented to replace 1,1,1-trichloroethane with a petroleum based product and switch from a xylene based paint to a powder coating. 5.0 Case Study Summary At the Wapakoneta plant, Copeland Corporation remanufactures and assembles new compressors for residential air-conditioning systems. The materials used for the compressors are cold rolled steel and salvaged parts from field failure compressors. Before the process change the field compressors were cut open and disassembled. The electric motors were removed and cold cleaned in trichloroethane to remove burnt oils and residues. After being assembled and welded, the cold roll steel shells were spray painted with a xylene based paint for a finished coat. Since the process change, electric motors from field failure compressors are cold cleaned in a petroleum based product. This change was made in February 1990. In addition, a powder coating system was installed to finish coat the compressors. This system was installed in March of 1990. Copeland had a quality concern regarding the residue that has to be removed from compressor parts prior to assembling. Residue lodged in electric motors could cause the motor to short out and fail early. All cleaning compounds must be compatible with freon which is used in compressor systems. Solvent based paints caused problems with uniform coverage and had very low salt spray corrosion protection. Powder coating is applied automatically for a more uniform coverage and salt spray corrosion is far superior to solvent based paints. 6.0 Economics A total of $251,000 per year is saved in material, maintenance and waste disposal costs. The cost to change from solvent based paint to powder coating was $95,000. 7.0 Cleaner Production Benefits Improvements in health and safety are important to Copeland. Operators are no longer working with fumes from 1,1,1- trichloroethane. The petroleum based product is non-hazardous and had no odor. Operators no longer have to work with fumes from xylene solvent based paint. Liability from handling storage and disposal of paint related waste has been eliminated. The powder coating is applied automatically. The waste from the petroleum based product is used in a fuels blend program. Since Copeland started powder coating they have eliminated approximately 124 barrels of paint related waste per year. Air emissions from xylene based paint have been eliminated. This is reflected in Copeland's air permits, their Form R's, and Community Right to Know Releases. Emissions from the powder system are limited to natural gas combustion. 8.0 Obstacles, Problems and/or Known Constraints Copeland tried a citrus based product to clean their electric motors; however, the fruit smell made the operator nauseous. the petroleum based product has no odor. 9.0 Date Case Study was Performed 1989-1992 10.0 Contacts with Citations Copeland Corporation 751 Industrial Drive Wapakoneta, Ohio 45895-0428 Mr. Ken Fisher, Environmental Coordinator 419/738-9234 11.0 Keywords 502 Halogenated (e.g., chlorinated) solvents 511 Paint thinner and petroleum distillates 800 Organic gases 2079 Metal cleaning 2097 Painting 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 1002 Annual cost savings 1003 Capital costs 1008 Treatment/disposal cost avoided Worker protection Regulatory incentives ---------------------------------------------------------- Crown Equipment Corporation New Bremen 1.0 Headline 1,1,1-trichloroethane has been replaced with an aqueous cleaning solution. 2.0 SIC Code 3537 3.0 Name and Location of Company Crown Equipment Corporation 40 South Washington Street New Bremen, Ohio 45869 4.0 Clean Technology Category This project involved a material substitution and equipment and process modifications. The organic solvent 1,1,1-trichloroethane was replaced with aqueous cleaning compounds. 5.0 Case Study Summary Industrial manufacturing plants have for years relied on the use of various solvents for cleaning miscellaneous metal parts. The organic solvent 1,1,1-trichloroethane has been the solvent of choice for many because of its low toxicity and high flash point characteristics. Only recently has this solvent been added to the list of those chemicals known to deplete the ozone layer. Crown Equipment Corporation, a manufacturer of electric lift trucks and antenna rotators, first substituted a water based cleaning compound in cold cleaning (dip) operations. Two large vapor degreasers were then removed and replaced with a series of agitating wash tanks. This central cleaning system employs a wash, rinse, rust inhibiting and drying stage to clean parts. Crown has not had to change production rates as a result of the new process. New waste streams generated consist of 900 gallons of oily wastewater that is treated on site. Energy usage cannot be quantified at this time. It is expected to rise, however, as a result of the additional heating requirements. In 1988, 208,000 pounds of 1,1,1-trichloroethane were used in cold cleaning degreasing and the operation of two vapor degreasers. Following implementation of this project, 1,1,1- trichloroethane was eliminated. The agitating technology utilized for this project was commercially available. The central cleaning system was purchased "off the shelf". The chemistry was customized to meet the cleaning requirements that Crown required and to provide adequate rust protection. 6.0 Economics Capital costs for the purchase of the central cleaning equipment was $78,000. This included all equipment necessary to provide the same cleaning capacity and production rates as before. Operation and maintenance costs remain the same for the new equipment as compared to vapor degreasing. Approximately eighty additional work hours were required to install the new equipment. The payback period for the entire project is ten months. This figure is based on the purchase of 17,175 gallons of 1,1,1- trichloroethane in 1989. By eliminating cold cleaning with this solvent, a reduction in solvent usage of approximately 35% was realized with no capital investment. The cost of purchasing the 1,1,1-trichloroethane in 1989 was $103,000. The purchase of the central washing equipment was $78,000 with an additional $3,000 in chemical costs. 7.0 Cleaner Production Benefits This project has produced various benefits for Crown including cost savings, improved public relations, improved employee relations and pollution reduction. It has reduced regulatory requirements through a reduction in hazardous waste materials sent out for disposal. Non-hazardous waste streams that had previously been contaminated by the solvent are no longer rendered hazardous by such contamination. This project has allowed Crown to drop 1,1,1-trichloroethane from its Superfund Amendments and Reauthorization Act reporting requirements, and reduced the liability for Crown in sending the listed wastes to disposal facilities. Since this material has been removed from the manufacturing area, employees no longer have the potential for exposure. In addition, the spill response group had one less chemical of concern. This project has been reviewed by other industrial manufacturers who are interested in removing solvent degreasing operations. 8.0 Obstacles, Problems and/or Known Constraints The biggest obstacle Crown faced was providing the capital outlay required to purchase the equipment. This was especially difficult since the economy and Crown were in a recession during the planning stages of this project. This project also required extensive investigation into alternative cleaning processes and equipment. It required a review of the numbers, types and metallurgy of the parts being cleaned. A great deal of bench testing of the various parts was performed prior to deciding on the best equipment to purchase. 9.0 Date Case Study was Performed The project was begun in August 1990 with investigations and bench testing. Equipment purchasing occurred in November 1991. The completed project has been evaluated for six months as of May 1992. 10.0 Contacts with Citations Implementing industry: Crown Equipment Corporation 40 South Washington Street New Bremen, Ohio 45869 Mr. Brian J. Duffy, Environmental Manager 419/629-2311 11.0 Keywords 502 Halogenated (e.g., chlorinated) solvents 1014 Degreasing 2136 Vapor degreasing 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 1002 Annual cost savings 1003 Capital costs 1008 Treatment/disposal cost avoided Worker protection Regulatory incentives ---------------------------------------------------------- Diebold, Incorporated Canton 1.0 Headline A paint substitution has significantly reduced the use of chemicals in the EPA 33/50 Program for this company. 2.0 SIC Code 3499 3.0 Name and Location of Company Diebold, Incorporated 818 Mulberry Road Canton, Ohio 44707-3256 4.0 Clean Technology Category Diebold Incorporated has significantly reduced the use of 33/50 Program solvents through the implementation of material substitution. 5.0 Case Study Summary Diebold manufactures, sells and installs a variety of products. A change in production at Diebold's main plant in 1991 reduced the volume of paint they would normally use in certain high- volume colors. Their high-solids baked enamel paint supplier subsequently requested that Diebold find a new supplier. Their old supplier could not make an acceptable profit with a reduced volume of standard colors and over thirty colors in one to twenty gallon batches. Diebold was concerned with maintaining quality and cost factors while reducing the use of toxics in their paint systems. They discovered a company that specializes in Diebold's paint market. More importantly, this company could supply most of the colors needed without the use of solvents listed in the EPA 33/50 Program. Another desirable characteristic of Diebold's new paint supplier's coating system was that the clean-up solvent for their high-solids coating contained no 33/50 solvents. These were two convincing selling points for Diebold. The supplier was also willing to make up special colors in increments of one gallon, which reduced Diebold's inventory. 6.0 Economics The price of paint with the new supplier is the same as it was before. Diebold can now purchase the paint in smaller quantities, for exactly what they need, as compared to five gallon drums with their old supplier. This has reduced the quantity of unused paint that is disposed of, thereby reducing hazardous waste disposal costs. The true environmental impact of switching paint suppliers is a further reduction in the use of toxic chemicals with no increase in costs. 7.0 Cleaner Production Benefits Diebold has seen an economic benefit in reduced hazardous waste disposal costs and has further reduced the use of toxic chemicals. 8.0 Obstacles, Problems and/or Known Constraints None observed 9.0 Date Case Study was Performed 1989-1992 10.0 Contacts with Citations Diebold, Incorporated 818 Mulberry Road Canton, Ohio 44707-3256 Mr. David Rinehart 216/588-3704 11.0 Keywords 509 Organic paint, ink lacquer, or varnish 2097 Painting 02 Process raw materials modification or substitution Treatment or disposal cost reduced ---------------------------------------------------------- Dietrich Industries, Incorporated Warren 1.0 Headline Mechanical modifications to a washer and the use of ultrafiltration technology has resulted in a substantial decrease in hazardous waste disposal costs and a decrease in chemical costs. 2.0 SIC Code 3490 3.0 Name and Location of Company Dietrich Industries, Inc. 1985 North River Road Warren, Ohio 44483 4.0 Clean Technology Category Implementation of process and equipment modifications has resulted in substantial cost savings. 5.0 Case Study Summary Dietrich Industries Incorporated's Warren facility is a metal fabricating and steel processing facility. They produce steel sheets and blanks for uses in appliances to automobiles. They supply fabricated steel products for the mining industry, and steel stampings for various other uses. In 1988, a steel stamping (no further description can be given for proprietary reasons) was to be produced in this facility. As they began to produce large quantities of this stamping, some problems were being reported by customers. The major concern was the inability to achieve proper paint adhesion to the part. The decision was made to begin washing the parts before shipment to the customer. In 1988, the plant began fabrication of a prototype washer that fit their particular needs. As the demand for these stampings escalated, the washer could not meet production levels necessary to supply their customers. A second washer of a new design was constructed to meet the increased demand. By 1989, this washer, too, fell short of their needs. A third washer of even larger capacity was constructed and supplied all of their customers until 1990, when a concerted effort was made to increase capacity while decreasing the cost to produce the part. A new washer was contracted for fabrication. This washer was to include everything that had been learned from the previous washers. The new washer was constructed from stainless steel to their specifications. The three stage, belt type spray washer was delivered in 1990. Changes in the EPA's regulations created problems for the customer. The demand skyrocketed for cleaner parts which could be painted with a water based paint. The facility now had the capacity to produce ample parts but the quality was unacceptable. research into the paintability problem showed that iron phosphatizing would promote better adhesion of the paint. The facility wanted to utilize the existing washer with iron phosphate. Several large corporations in the coil coating industry were contacted to provide a combination cleaner/iron phosphatizing chemical. The first batch of the new process, with iron phosphatizing/cleaning, then rinse and seal, was disastrous. Within two weeks the bath had to be dumped. This cost $4,200. The expense was caused by the contamination of the chemical bath caused by drag out from the part and the conveyor belt. The need to reduce this expense marked the beginning of their eventual goal of finding a near zero discharge system. Initially, the main concern was to eliminate the chemical crossover between the tanks of different chemicals. Air blow-off knives were designed to shed the liquid from the parts and belt carrying them, and the single continuous belt was broken into three distinct sections, one for each chemical solution. These modifications incurred costs for parts of $15,000. The facility originally intended to use waste treatment to produce a waste water acceptable by the county sanitary engineer. The process water would be collected, pH corrected, precipitated and released to a sanitary sewer. This is the normally accepted method to meet local sanitary sewer regulations, but the cost of city water and sewerage was unacceptable to meet long term goals. Conventional waste treatment would be a daily expense with no means to recover the investment. The idea of disposing of the chemical solution, 97% of which was water, at high cost, caused concern. This water could be reused for the following chemical bath. They began to research methods for recovering their waste water solution. Potential recovery systems from deionization to microfiltration were discussed. Experts on each system were consulted, and it was decided that the most suitable and cost effective method to achieve the plant's goal was ultrafiltration. The decision was made to purchase a unit capable of processing two to ten gallons per minute. This unit would incur a capital expenditure of $36,000. It is Dietrich's opinion that the use of ultrafiltration technology may be the least expensive option to minimize liquid pollution source production. Ultrafiltration allows for the reuse of a spent iron phosphate bath for make-up water. Figure 1 shows the mechanism that allows ultrafiltration to work as a self cleaning system. As the contaminated feed flows along the membrane walls, it scrubs the particles too large to penetrate to the exit of the cartridge. The contaminated flow is returned to the process tank for circulation to the cartridge again. The clean permeate that passed through the membrane is returned for reuse in the washer. The ultrafiltration system was installed and soon the operator was able to keep the bath at very consistent levels. The unit was installed as shown in Figure 2. The return line from the unit does not enter stage 1 directly. This is to prevent stagnation of stage 2. The quality of the parts began to rise dramatically upon start-up. The next steps taken were to determine the effectiveness of the system and to log the amount of each chemical being used. Table 1 shows the type, amount and cost of each chemical used. The significant decrease in cost between charge #2 and #3 was due to the addition of ultrafiltration. 6.0 Economics The process changes described above have achieved an 84% reduction in chemical costs, while reducing the quantity of water pollution by 88% from the original method. These reductions are due to mechanical modifications to the washer and the addition of ultrafiltration to process the chemical solutions being used. The total cost savings on an annual basis is $132,000. This figure does not include the increased freedom from liabilities of massive disposal of waste material. A more vivid picture of the amount of chemical savings is shown in Figure 3. An overall reduction of 90% in the consumption of iron phosphate is the pronounced difference. The slight increase in sealer use was caused by the increase in production. The most dramatic increase is in the use of booster chemicals. The booster is being utilized more since the entire iron phosphate package is not needed. Figure 4 depicts the reduction in chemical costs. The modifications show a 50% reduction compared to the original configuration. The addition of ultrafiltration produced an 80% reduction in chemical costs in the same comparison. Figure 5 shows the bottom line, the actual cost of the chemicals to produce 100 parts. The simple modifications netted a 63% reduction of cost alone. The recycling of the chemical solution added another 57% savings. The total reduction in chemical costs was an impressive 84%. The amount of process water that must be disposed of has made the largest impact on overall cost of processing parts. The anticipated amount of waste water prior to modification was 64,800 gallons. The actual amount of process water disposed of was 3,600 gallons at a cost of $2,880. The facility is presently accumulating an average of forty gallons of sludge per month. This is quite small in comparison to the original 2,700 gallons disposed every two weeks. The washer in its original configuration would have consumed $26,112 of chemicals annually. In its present configuration it is projected to consume less than $5,000 of chemicals based on the same production level. The amount of chemical costs are dwarfed by the savings through source reduction of liquid waste. The projected cost of waste water disposal in the washer's original state would have been $112,320. The present system, a nearly closed loop, will require as little as $1,000 for disposal of tramp oil and sludge annually. The total capital expenditure for the modification and addition of ultrafiltration was under $60,000 including labor. This relatively simple application of current technology produces an annual savings in excess of $132,000. 7.0 Cleaner Production Benefits The reuse of the iron phosphate bath after it has passed through the membrane in the ultrafiltration technology saves massive disposal costs. The reuse is also responsible for the following items: * City water costs are reduced due to less need for make-up water. * Chemical costs are reduced through reuse of the bath already saturated with phosphoric acid. * Sludge build up removal costs are reduced due to continuous filtering. * Other liquid wastes can be processed by ultrafiltration with only minimal flushing of the system. * Minimal floor space is required because the ultrafiltration unit can be remotely located. * Maintenance cost is reduced since the ultrafilter helps hold the bath at a consistent concentration requiring less operator attention. * The part quality is greatly improved due to the consistency of the bath. 8.0 Obstacles, Problems and/or Known Constraints No problems existed except that the operators needed sufficient time to learn to operate the bath. 9.0 Date Case Study was Performed 1988-1992 10.0 Contacts with Citations Dietrich Industries, Inc. P.O. Box 68 Blairsville, PA 15717 Mr. Robert O. Beckwith, Corporate Project Engineer 412/676-4782 11.0 Keywords Other waste water 2079 Metal cleaning 01 Equipment or technology modification 02 Process modification or substitution 07 Onsite recycling or recovery for reuse 11 Wastewater reduction 1002 Annual cost savings 1003 Capital costs 1008 Treatment/disposal cost avoided [Figure 1, Figure 2, Table 1, Figure 3, Figure 4, Figure 5] [each on a full page] ---------------------------------------------------------- Eveready Battery Company Fremont 1.0 Headline Process and equipment modifications were implemented to achieve solvent minimization and elimination of 1,1,1-trichloroethane used in adhesives. 2.0 SIC Code 3692 and 3691 3.0 Name and Location of Company Eveready Battery Company, Inc. 1501 West State Street Fremont, Ohio 43420 4.0 Clean Technology Category Process and equipment modifications were implemented to reduce the amount of solvents used and eliminate the use of 1,1,1- trichloroethane used in adhesives. 5.0 Case Study Summary Eveready Battery Company has had an active solvent Emissions Tracking and Solvent Minimization / Elimination program at all of their plants for many years. The Fremont facility, which manufactures carbon-zinc flashlight and lantern batteries, has completed trials of a water based adhesive in order to eliminate the use of 1,1,1-trichloroethane from a labeling adhesive. The plant has ordered production quantities of the water based adhesive, and began its use exclusively by the end of September, 1992, as inventories of the old adhesive were used up. The number of mineral spirit tanks and the solvent changing frequencies have been reduced along with the elimination of squirt and spray bottles containing solvent. Process wastes are recycled whenever possible at the Fremont facility. Scrap mix can usually go back into the mix room for blending with fresh product. Scrap cans are returned to the vendor who melts them down for reprocessing. Lithographed steel from lantern-battery jackets is sold as scrap metal. Cardboard from packaging is sent to a local recycling center. Currently, the Fremont facility is recycling approximately 90% of their wastes for which they have identified outlets. 6.0 Economics No cost savings are noted; tangibles and intangibles seemed to have balanced out. 7.0 Cleaner Production Benefits Use of 1,1,1-trichloroethane has been eliminated in the production process. 8.0 Obstacles, Problems and/or Known Constraints Natural resistance to change by employees disappeared quickly, especially after the new adhesive formula worked more effectively. 9.0 Date Case Study was Performed 1989-1992 10.0 Contacts with Citations Eveready Battery Company, Inc. 1501 West State Street Fremont, Ohio 43420 Mr. Steve Lolli, Plant Environmental Coordinator 419/334-6595 or 419/332-6401 11.0 Keywords 502 Halogenated (e.g., chlorinated) solvents 2018 Cleaning 2062 Gluing 04 Process raw materials modification or substitution 1008 Treatment/disposal cost avoided ---------------------------------------------------------- General Metals Powder Company Akron 1.0 Headline Waste water is purified and reused in a production process. 2.0 SIC Code 3499 3.0 Name and Location of Company General Metals Powder Company 130 Elinor Avenue Akron, OH 44310 4.0 Clean Technology Category The installation of ion exchange columns and the subsequent modification of their regenerating process allowed General Metals Powder Company (GEMPCO) to concentrate and reuse copper laden rinse waters. 5.0 Case Study Summary GEMPCO produces copper powder through electrolytic deposition of copper in an acidic solution, and uses it in a powdered metallurgical process to manufacture friction linings for clutch plates and brake plates. Wastewater from the powder production process contains solid copper particles and dissolved copper ions and would be considered a toxic waste. This waste stream, which was previously disposed of on the company property, is the subject of this case study. Disposal of this waste was stopped in 1986, and a process of purifying the wastes was initiated by diverting the waste water through an ion exchange resin that would remove the copper. GEMPCO began to regenerate the resin with sulfuric acid and reuse the copper laden regenerate solution as electrolyte in the copper slurry production. However, this regenerate solution had a high concentration of sodium which inhibited the production of the copper slurry. The company that engineered and installed the ion exchange equipment considered their work complete, leaving GEMPCO with a process which cleaned the waste water but left a regenerate solution unsuitable for reuse in the electrolytic deposition process. Company personnel working on the system devised an electro- winning process to remove the sodium from the regenerate solution, making it acceptable for reuse in production. Now GEMPCO had a system that could provide a usable regenerate solution and an effluent acceptable for its sewer permit. Since the regenerate solution had to be stripped of sodium in a batch process, the amount of regenerate solution GEMPCO could use was restricted by the rate of electrolyte consumption required by the slurry production. This affected how often the ion exchange resins were regenerated. GEMPCO was generating more electrolyte from the ion exchange than it could use, so it delayed the frequency of regeneration of the resin. This lowered the efficiency of the ion exchange and produced waste water with too much copper in it to be in compliance with sewer permit levels. GEMPCO's system worked but it needed improvements to meet the sewer permit limits on a regular basis. GEMPCO hired a company that had been through a similar experience. They analyzed GEMPCO's system and recommended changes that got GEMPCO more capacity from the ion exchange resin. GEMPCO stopped the conversion of resin to a sodium state for copper absorption since it was unnecessary. These measures doubled the life of the ion exchange resins. Now GEMPCO had a system that worked and brought the company well below the permit levels for copper. GEMPCO's permit level was cut in half from four parts per million to two parts per million and the company is still in compliance. All of this work put more of a demand on the company's utilities. GEMPCO is using more electricity for the electro-winning process and more water and chemicals to generate de-ionized water. Currently GEMPCO has not increased its production rates or saved any money by using regenerate solution for electrolyte. The average amount of water going to the sanitary sewer system is twenty gallons per minute or 10,000 gallons per day. Currently GEMPCO is in full compliance with its sewer use permit and is not generating any hazardous waste from this process. The effluent flow rates are estimated. GEMPCO states that this technology is currently available. However, of the two companies that provided information and equipment, the first company left GEMPCO with a system that did not work and ruined GEMPCO's production process. The second company helped GEMPCO solve its problems. 6.0 Economics GEMPCO has spent $400,000 to achieve its current state of compliance. Items purchased include a filter press, a sand filter, two 27 cubic foot ion exchange columns, 1,600 gallon and 500 gallon plastic tanks, five chemical metering pumps, two centrifugal process pumps, two diaphragm pumps, a control panel with a microprocessor, approximately forty PVC diaphragm valves pneumatically operated, PVC plumbing and secondary containment diking for all of this equipment. GEMPCO feels that if it had contracted with the second company from the beginning, the system would have cost $250,000 required less space and been less complicated. GEMPCO has hired a full time salaried employee to be responsible for all the water processing. It also requires twenty-five percent of a union operator's daily work and ten percent of a union maintenance person's time. This equipment does not save GEMPCO any money. It is estimated that GEMPCO is spending $15,000 a year in utilities and chemicals for this equipment. 7.0 Cleaner Production Benefits This process keeps the company in compliance with its permit and allows GEMPCO to stay in business. 8.0 Obstacles, Problems and/or Known Constraints The obstacle that limits GEMPCO the most and causes the greatest potential for problems is the quality and quantity of ion exchange regenerated solution. GEMPCO is constantly juggling the scheduling of production and the regeneration schedule to stay in compliance and not create more regenerate solution than GEMPCO can use. The operation of this equipment always poses the potential to disrupt operations and cause problems with the product GEMPCO produces. 9.0 Date Case Study was Performed The initial work on this project was started in 1986 and was completed in 1987. The second stage of improvements occurred in 1990. 10.0 Contacts with Citations General Metals Powder Company 130 Elinor Avenue Akron, OH 44310 Mr. Brian Kramer, Plant Engineer 216/633-1226 11.0 Keywords 117 Other inorganic liquid 2067 Ion exchange 2083 Metal recovery 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 07 Onsite recycling or recovery for reuse Regulatory incentives ---------------------------------------------------------- Gerity-Schultz Corporation Toledo 1.0 Headline Soluble quench oil has been replaced by synthetic oil. 2.0 SIC Code 3369 3.0 Name and Location of Company Gerity Schultz Corporation 1810 Clinton Street Toledo, Ohio 43607 4.0 Clean Technology Category Gerity Schultz Corporation has substituted synthetic oil for soluble oil in the quench pits. The synthetic oil in the pits lasts for two years or longer; the soluble oil was replaced about every two months. This substitution has resulted in a large reduction of disposable waste. 5.0 Case Study Summary Gerity Schultz is a zinc die casting facility. The castings are quenched in pits under the die casting machines in a water and oil mixture called quench oil. In the original process, hydraulic oils and lubricating oils (tramp oils) which drip into the pits, along with some quench oil, overflowed into city drains. This kept the quench oil fresh and emulsified. However, Gerity Schultz was required to pay the city a $2,000 per month surcharge for this oil drainage. Eventually the city prohibited this kind of oil drainage, so the facility plugged these drains. Because of this the tramp oil caused the soluble oil to go out of emulsion and the oil became rancid in about two months. The company decided to find a substitute for the quench oil. Each pit contains approximately 1,200 to 1,400 gallons of quench oil consisting of 2 to 4% oil and 96 to 98% water. There are approximately eight pits in operation at any one time. Synthetic oils were available at the time the facility was looking for a substitute. It was necessary to find one which was compatible with zinc. The first choice caused "stearate" growths on zinc castings under certain conditions. Since then the facility has changed to a different synthetic oil. 6.0 Economics Soluble oil sells for about $2.50 per gallon; synthetic oil costs about $5.00 per gallon. Gerity Schultz originally flowed the quench oil through filters and separators (both soluble and synthetic). Now the facility filters the synthetic quench through an $8,500 ultra-filter. The ultra-filter could not be used with the soluble oil. It takes about sixteen man hours to drain and steam clean a quench pit. In the past, when they used soluble oil, Gerity Schultz cleaned the pits about every two months. Now the pits need to be cleaned about every two years. Biocides which cost $150 per gallon are added to the quench pits every few months, or as needed, at about 1 pint per every 1200 gallons. Basing the payback period simply on oil costs, the payback time is only about four months. The soluble oil costs $2.50 per gallon and the synthetic oil costs $5.00 per gallon, but the soluble oil only lasted approximately two months. 7.0 Cleaner Production Benefits Gerity Schultz now spends less money for quench oil and no longer has to pay the $2,000 per month for oil discharge to city sewers. Public relations have improved and liabilities have been reduced as Gerity Schultz no longer dispenses quench oil into city drains. 8.0 Obstacles, Problems and/or Known Constraints None mentioned 9.0 Date Case Study was Performed Gerity Schultz first began using synthetic oil in the spring of 1989. 10.0 Contacts with Citations Gerity Schultz Corporation 1810 Clinton Street Toledo, Ohio 43607 Mr. Jim Ochs 419/244-4971 11.0 Keywords 506 Waste oil 2035 Die casting 04 Process raw materials modification or substitution 1002 Annual cost savings ---------------------------------------------------------- Gerity Schultz Corporation Toledo 1.0 Headline Ethylene glycol hydraulic fluid, a Section 313 toxic material, was replaced by a non-toxic material. 2.0 SIC Code 3369 3.0 Name and Location of Company Gerity Schultz Corporation 1810 Clinton Street Toledo, Ohio 43607 4.0 Clean Technology Category Using material substitution, diethylene glycol, a non-toxic material, replaced ethylene glycol, a toxic material, as a hydraulic fluid. 5.0 Case Study Summary Gerity Schultz is a zinc die casting facility that uses hydraulic systems to open and close dies. When a suitable substitute hydraulic fluid was found, the switch was made from a toxic to a non-toxic hydraulic fluid. 6.0 Economics The change was made more for safety and environmental reasons rather than for economic reasons. However, a cost savings of about $0.80 per gallon was realized. 7.0 Cleaner Production Benefits There is less danger of injuries to workers due to ingestion, inhalation or skin contact. 8.0 Obstacles, Problems and/or Known Constraints None mentioned 9.0 Date Case Study was Performed Diethylene glycol was substituted for ethylene glycol in 1989. 10.0 Contacts with Citations Gerity Schultz Corporation 1810 Clinton Street Toledo, Ohio 43607 Mr. Jim Ochs 419/244-4971 11.0 Keywords 609 Other organic sludge 2035 Die casting 04 Process raw materials modification or substitution 1002 Annual cost savings ---------------------------------------------------------- Guardian Automotive Products Upper Sandusky 1.0 Headline 1,1,1-trichloroethane was almost completely replaced by a solvent which has a lower evaporation rate and is less environmentally damaging. 2.0 SIC Code 3231 3.0 Name and Location of Company Guardian Automotive Products State Route 67 South P.O. Box 336 Upper Sandusky, Ohio 43351 4.0 Clean Technology Category The technology used in this study was a material substitution. The use of the solvent 1,1,1-trichloroethane was reduced almost completely by replacing it with another solvent. The replacement solvent is equally effective as a cleaner but has a lower evaporation rate than the 1,1,1-trichloroethane, thus reducing the amount of raw materials purchased and amount of waste disposed of. 5.0 Case Study Summary Guardian Automotive Products manufactures laminated windshields for the automotive industry. The solvent is used in a silkscreening process in which Guardian applies a decorative paint band around the outer edge of the windshield. In some cases the screen will become clogged or cause misprints. In these situations, the solvent is used to clean on-line problems. The production levels during and after the substitution remained the same with only minor fluctuations in productions due to product demand. The waste stream produced from this process has been dramatically impacted with a reduction in off site disposal of 18,150 pounds of 1,1,1-trichloroethane waste in 1990 to 7,425 pounds in 1991. This reduction is expected to continue into 1992 with the phasing out of this solvent. The purchase of raw materials is also down dramatically from 118,800 pounds in 1990 to 10,800 pounds in 1991. This will also be impacted as the solvent is phased out. The current status of this case study is complete, as the initial project was to reduce the use of 1,1,1-trichloroethane. This has been in effect since November of 1990. An additional step will be taken in the future to eliminate the solvent completely. The technology necessary to complete this project was readily available and no process changes or equipment changes were needed. 6.0 Economics Investment costs for this project were reflected in a massive raw material reduction which resulted in a substantial savings in the cost of materials. Operational and maintenance costs for the project remained the same. 7.0 Cleaner Production Benefits The economic benefit realized by this project is the reduction of the use of a highly volatile solvent which was producing large quantities of fugitive emissions. An additional benefit is the great reduction in the amount of waste which is transported off site for disposal. 8.0 Obstacles, Problems and/or Known Constraints The only obstacle that was encountered during the project was difficulty in finding a solvent to clean the silkscreens that would not damage the screen. Most solvents that were experimented with were either ineffective or damaged the screens as they cleaned them. The replacement solvent does not clean as aggressively or dry as quickly as the 1,1,1-trichloroethane, but is as effective in protecting the screen. 9.0 Date Case Study was Performed This project was initiated in mid-1990 and was implemented on November 1, 1990. 10.0 Contacts with Citations Guardian Automotive Products RR#5, State Route 67 South P.O. Box 336 Upper Sandusky, Ohio 43351 Mr. Jeffrey D. Warner, Environmental Technician 419/294-4921 11.0 Keywords 502 Halogenated solvents 800 Organic gases 2018 Cleaning Silkscreening 04 Process raw materials modification or substitution 1002 Cost savings ---------------------------------------------------------- Kovatch Castings Company Uniontown 1.0 Headline Manufacturing costs have been lowered through source reduction and recycling of 1,1,1-trichloroethane. 2.0 SIC Code 3324 3.0 Name and Location of Company Kovatch Castings Company 3743 Tabs Drive Uniontown, Ohio 44685 4.0 Clean Technology Category Use and loss through emissions of 1,1,1-trichloroethane at Kovatch Castings Company have been reduced through improved housekeeping measures and management skills. The solvent still in use is reclaimed off-site and reused by Kovatch. 5.0 Case Study Summary Kovatch is a ferrous and non-ferrous investment foundry. Part of the operation is to remove the silicone mold spray from the wax patterns with 1,1,1-trichloroethane. Although usage has never been high, Kovatch has implemented changes to reduce use of the solvent and reclaim and reuse it, and is investigating replacement products. Wax patterns are degreased in 1,1,1-trichloroethane in the "shell room" and coated repeatedly with a ceramic shell material. When the shell material is dry, the wax pattern is melted out, leaving a hollow ceramic shell. This shell is fired in an oven, then removed to have the molten metal poured into it. When the metal has cooled, the shell is broken away, revealing the metal casting that was formed in wax. The 1,1,1-trichloroethane is used at room temperature in its natural liquid state. The wax patterns are dipped several times in the solvent until all traces of the silicone mold release spray are removed. When the silicone builds up in the solvent to a level that makes cleaning ineffective, the solvent is pumped out into empty fifty-five gallon drums and clean solvent is pumped into the cleaning tank. The used solvent is then stored on site for less than ninety days, then transported to the recycler following the proper state and federal regulations. The cleaning tank holds approximately twenty-five gallons and is changed about every two to three weeks, or as needed, depending on production. As the reclamation process only yields about 75%, the remaining 25% must be made up with prime material at a higher cost. Through the use of proper management skills and improved housekeeping, use of 1,1,1-trichloroethane has dropped from 880 gallons in 1990 to 605 gallons in 1991. A projected usage for 1992 is about 550 gallons. This decrease is due to two primary changes. A fifty-five gallon drum of the solvent that was previously left uncovered at times is now always kept covered when not in use, reducing emissions. Although the solvent was purchased only for cleaning the wax patterns, people from other departments would take small amounts from the shell room for use in cleaning other rooms. This practice was stopped, and non- hazardous cleaners are used for cleaning in these areas. Kovatch is concerned that off-site reclamation will not continue to the be the best solution because the cost of reclamation continues to increase and because 1,1,1-trichloroethane will eventually be banned. Kovatch is trying different replacement solutions that are environmentally sound. Traditionally, the best degreaser for the investment industry is liquid freon with a thin layer of water on top to prevent losses through evaporation. Because of the known problems with freon, the company has used 1,1,1-trichloroethane. A citrus derivative has been tried in years past with no success. If a detergent based cleaner is found to successfully clean the wax patterns, a rinse station possibly will have to be built and two additional stages added to the process, a rinse and a dry. This might be difficult, as the wax starts to soften and possibly deform at temperatures as low as 95 degrees Fahrenheit. This will be detrimental to the process because the dimensional tolerances on many of the waxes can be as close as + or - 0.005 inches. 6.0 Economics There have been no investment costs or payback period for the reduced use or reclamation of the 1,1,1-trichloroethane. A 45% reduction of material costs for recycling was realized due to a change from one service center to another, with no degradation of either product or service. Although Kovatch has realized cost savings from changes made, a detailed cost/savings analysis has not been performed. 7.0 Cleaner Production Benefits In addition to cost savings, Kovatch has benefitted from improved worker safety from implementation of pollution prevention. They expect benefits in both these areas to increase when 1,1,1- trichloroethane has been completely replaced. 8.0 Obstacles, Problems and/or Known Constraints The only problems foreseen with the replacement of the 1,1,1- trichloroethane is the addition of rinse and drying stations. They must be monitored very carefully because o temperature instability of the wax patterns. The quality control on this procedure must have some type of computer controlled processing and monitoring system to verify on a continual basis the temperature of the rinse water and the drying air. 9.0 Date Case Study was Performed There are no known dates to this study as it has been an ongoing study since the incorporation of Kovatch over fourteen years ago. 10.0 Contacts with Citations Kovatch Castings Co. 3743 Tabs Drive Uniontown, Ohio 44685 Mr. Michael Sparrow, Chief Engineer 216/896-9944 11.0 Keywords 502 Halogenated solvents 800 Organic gases 2030 Degreasing 05 Better housekeeping 09 Management strategies Offsite reclamation for onsite reuse 1002 Annual cost savings Worker protection ---------------------------------------------------------- The Lincoln Electric Company Cleveland 1.0 Headline A variety of source reduction activities have resulted in cost savings, reduced emissions and a safer work environment for the employees. 2.0 SIC Code 2899 3.0 Name and Location of Company The Lincoln Electric Company 22801 St. Clair Avenue Cleveland, Ohio 44117-1199 4.0 Clean Technology Category Material and product substitutions have been used to reduce the quantity of 1,1,1-trichloroethane used in paints, coatings and metal cleaning operations. Housekeeping and recycling practices at Lincoln Electric have resulted in the reduction of releases of barium compounds. Modification of processing techniques allowed for the capture and re-use of manganese ore that had previously been disposed of. An ion-exchange system strips the copper from plating streams for sale to a copper reclaimer. 5.0 Case Study Summary The Lincoln Electric Company manufactures arc welding products and industrial motors. The Lincoln Electric Company has committed to participate in the 33/50 Program and plans to try to eliminate the use of 1,1,1-trichloroethane in 1992. The use of 1,1,1-trichloroethane has been reduced from 912,000 pounds in 1987 to 473,000 in 1991, through material and product substitutions. Three colors of spray paints are used: red, grey and black. The reduction of 1,1,1-trichloroethane usage from 1987 to the present has been achieved by substituting powder coatings for red and black spray paints, and by installing water based washer systems instead of vapor degreasers for pre-cleaning parts. At the present time the grey spray paints used in the facility are being converted to powder coatings. The process will also eliminate several of the remaining vapor degreasers. This change will improve part quality significantly. The amount of 1,1,1- trichloroethane eliminated is approximately 50,000 per year. The dip paints use 1,1,1-trichloroethane as a solvent. Lincoln is investigating water based dip paints which will eliminate the solvent based systems currently in use. The elimination of these dip paints will reduce the use of this solvent by 160,000 pounds. Currently, vapor degreasers are used to clean parts in process, in maintenance areas and prior to painting in some manufacturing areas. Vapor degreasers will be eliminated by installing water based washers. The project has approached the vapor degreaser elimination problem by bringing in-house several types of water based cleaning machines. The cleaning machines are combined with a number of chemical cleaners for evaluation by the research and development section. Lincoln is hoping to achieve the right combination of cleaners and equipment for plant purposes, thus eliminating the use of 1,1,1-trichloroethane in the plant by 1992. Lincoln Electric has reduced barium releases from 14,700 pounds in 1988, to 800 pounds in 1991. This reduction of barium releases has been achieved through a greater emphasis on housekeeping and recycling practices. Specialty chemicals are formulated and processed for incorporation into welding consumables manufactured at Lincoln Electric. Formerly, offspec materials (floor sweepings, etc.) were collected for disposal. Specialty chemicals are now processed in confined rooms so that no contamination occurs. As these processes develop, fugitive losses, baghouse collected materials and other process losses are collected and reused in product formulations. Manganese releases at Lincoln Electric have been reduced from 2,924,863 pounds in 1988, to 14,147 pounds in 1991. This material represented 62% of Lincoln Electric Superfund Amendments and Reauthorization Act (SARA) Toxics Release Inventory (TRI) reported emissions in 1987 and 1988. Lincoln Electric modified process techniques to capture and reuse material that previously had been disposed of. Additionally, process development changes now allow material that was off-spec in size to be re-used in its products. The program to contain manganese and develop higher processing efficiencies focused on the addition of a recirculation loop in the processing system. This has allowed the feeding back of previously wasted materials into the front end of the process. Better housekeeping has further reduced waste generation in this process. Lincoln Electric Company also manufactures printed circuit boards for their welding machine product line. Recently a new water treatment plant was installed to treat the waste by-products from the plating processes associated with the production of printed circuit boards. Conventional water treatment processes used to treat similar waste streams at Lincoln generate 2,000 tons of landfillable waste a year. This amounts to an annual disposal cost of $75,000. Lincoln has installed an ion-exchange system which strips the copper from the plating streams, collects and concentrates it and finally plates the copper out into foil sheets. The foil sheets are sold to a copper reclaimer. With the process modification, no solid wastes are generated for disposal in a landfill. 6.0 Economics The investment cost for substituting powder coatings for red and black spray paints and installing water based washer systems was approximately $4,000,000. The cost of converting to grey powder coatings is $3,500,000 and will save approximately $750,000 per year. The cost of the water based washer project is estimated to be $750,000. Operational and maintenance costs and payback times for the reduction of 1,1,1-trichloroethane are not available. The reduction in releases of barium compounds did not involve a substantial outlay of money. The cost of properly training employees on better housekeeping practices was the principal expense. The payback period was three months. Full cost savings are not available at this time. The program to contain manganese cost approximately $12,500 to implement and saves $70,000 per year. The cost of the ion-exchange system which strips copper from the plating stream is approximately $300,000. With an annual savings in disposal costs of $75,000, the payback period for the new system is approximately four years. 7.0 Cleaner Production Benefits The primary benefit of the elimination of 1,1,1-trichloroethane is that the material is no longer used in the work environment which improves the quality of the work environment. Second, it has improved the quality of the products and done so at a lower operating cost. Production waste is considered a foundry sand now that it is no longer contaminated with barium. Approximately $80,000 to $85,000 will be saved per year due to decreased disposal costs now that this waste is reclassified. The primary benefit of the reduction of the manganese waste material is that the emissions from the Lincoln Electric facility of manganese compounds and its SARA TRI release totals have been significantly reduced. Also, lower amounts of manganese need to be purchased. 8.0 Obstacles, Problems and/or Known Constraints The 1,1,1-trichloroethane reduction program is extremely complex and requires the cooperation of the Quality Assurance, Machine Research and Development, Methods and Plant Engineering Departments. Prior to implementing new ideas, Lincoln must verify that the quality is as good as or better than the previous product and the results can be achieved at a lower total cost. The difficulties involved with making the barium reduction program a success were the research and development efforts required to reformulate some of the products to accept recycled materials. Another obstacle was the process management of equipment scheduling burden to allow certain chemical types to be manufactured at one time in the process. 9.0 Date Case Study was Performed 1987-1992 10.0 Contacts with Citations The Lincoln Electric Company 22801 St. Clair Avenue Cleveland, Ohio 44117-1199 Mr. John Petkovsek, Plant Environmental Engineer 216/481-8100 11.0 Keywords 502 Halogenated solvents Other inorganic solids, metal compounds 2015 Chemical processes, other 2020 Coating 2079 Metal cleaning 2097 Painting 2136 Vapor degreasing 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 05 Better housekeeping 07 Onsite recycling or recovery for reuse 1002 Annual cost savings Improved quality Worker protection ---------------------------------------------------------- Luke Engineering and Manufacturing Company Wadsworth 1.0 Headline The use of 1,1,1-trichloroethane is being reduced and eventually eliminated by replacement with biodegradable, water-based alkaline cleaners. 2.0 SIC Code 3471 3.0 Name and Location of Company Luke Engineering and Manufacturing P.O. Box 478 456 South Blvd. Wadsworth, Ohio 44281 4.0 Clean Technology Category The goal of Luke Engineering and Manufacturing Company is to eventually eliminate the use of chlorinated hydrocarbons by replacing them with biodegradable water based alkaline cleaners. 5.0 Case Study Summary This company is a job aluminum finishing operation. Its primary business is hard anodizing, serving a broad industrial base, including automotive, aerospace, defense, rail, tire, electronic, medical and other industries. In order to prepare parts for finishing, the metal must be prepared to present a clean surface as free as possible from any machining lubricants, oxides, scales, etc. This procedure has historically been started with a solvent cleaning to eliminate surface oil, grease and dirt. Luke Engineering and Manufacturing is currently moving as many of its jobs as possible to an agitated wash and rinse station to accomplish this. To date, approximately fifteen jobs have been switched to this type of cleaning. These fifteen jobs amount to about 30% of the company's sales volume. The company is moving to this process one customer at a time in order to ascertain the extent and types of other problems which occur. All the equipment and materials used are readily available. 6.0 Economics At this time, Luke Engineering and Manufacturing has not developed a complete cost analysis on how these changes are affecting their operation. Their preliminary analysis would seem to indicate a slight labor increase and a savings in the alkaline cleaner over the chlorinated solvent. The equipment, much of which the company built itself, had a capital cost of about $7,500. 7.0 Cleaner Production Benefits The benefits to be gained, other than regulatory relief, will be determined over a period of time. 8.0 Obstacles, Problems and/or Known Constraints One of the barriers faced presently is a requirement for the degreasing of parts prior to and after the operation with 1,1,1- trichloroethane. This is a government weapons specification requirement. The company has approached the customer about removing this requirement, but to date has received no relief. 9.0 Date Case Study was Performed The company has been involved in this project for about nine months. 10.0 Contacts with Citations Luke Engineering and Manufacturing P.O. Box 478 456 South Blvd. Wadsworth, Ohio 44281 Mr. F. P. Hayduk 216/335-1502 Information was supplied through vendor data. 11.0 Keywords 502 Halogenated solvents 2079 Metal Cleaning 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution Regulatory incentives ---------------------------------------------------------- Manufacturers Enameling Corporation Toledo 1.0 Headline All possible painting jobs have been converted from liquid to powder paint. 2.0 SIC Code 3479 and 3079 3.0 Name and Location of Company Manufacturers Enameling Corporation 400 South Westwood Avenue Toledo, Ohio 43609-1599 4.0 Clean Technology Category Process and equipment modification were made and material substitutions were implemented to reduce volatile organic compound (VOC) emissions from application of liquid paints. This was achieved substitution with powder paints where possible. 5.0 Case Study Summary The Manufacturers Enameling Corporation performs contract liquid and powder paint finishing as a sub-contractor to original equipment manufacturer vendors to the automotive companies. It is a family-owned company, has been operating since 1946, and presently bills approximately $5,000,000 per year with 80 employees. The company has been a pioneer in over chrome- painting, powder finishing over liquid priming, robot spraying, aqueous cleaning of plastics and hi-density conveyor racking. Manufacturers Enameling has been spraying powder paints since 1975 on refrigeration parts, and on class A exterior automotive parts since 1978. Initially this was done only to achieve the superior corrosion resistance of powders, but since 1987 a concentrated effort has been made to convert every possible job from liquid to powder to reduce VOC emissions. Incidental benefits to this are greater ease of application of the powder, favorable economics even without powder recovery, the ability to handle parts immediately after cool-down from the ovens, and pack ship and machine without any dwell time for oxidation curing. These steps are necessary with some liquid paints. On a material volume basis, about 30% of the company's paints are powder. Total paint usage is 30-40,000 gallons per year. Spraying 30% of 35,000 gallons without solvents, as is possible with powder, results in approximately an 80,000 pound per year reduction in VOC emissions. Application of liquid and powder paints by robot spraying is a "home grown" process at Manufacturers Enameling Corporation. It is a mature technique, in use in production for over fifteen years. Powder paint application is readily available from a wide choice of suppliers. Features which allow for quick interchangeability to liquid spraying are not available due to the nature of powder paint, as scrupulous clean-up is necessary to prevent color contamination in subsequent paint jobs. 6.0 Economics Operational and maintenance cost comparisons are difficult without calculating the costs for doing liquid and powder application separately. For a primary analysis, the mentioned solvent would cost $20-30,000 annually, plus probably a similar amount for cleanup solvents and disposal. Per-piece cost on two representative high-volume production parts is illustrative: * aluminum 6-cylinder intake manifold * material cost for liquid primer and liquid finish - $0.45 * material cost for liquid primer and powder finish - $0.26 (57% of previous) * luggage rack longitudinal molding * material cost for liquid primer and liquid finish - $0.099 * material cost for liquid primer and powder finish - $0.053 (53% of previous) 7.0 Cleaner Production Benefits VOC savings in the above two examples are: * manifold * VOC emission for liquid primer and liquid topcoat - 0.065 pounds per piece * VOC emission for liquid primer and powder topcoat - 0.011 pounds per piece (16% of previous) * longitudinal molding * VOC emission for liquid primer and liquid topcoat - 0.02 pounds per piece * VOC emission for liquid primer and powder topcoat - 0.0042 pounds per piece (20% of previous) 8.0 Obstacles, Problems and/or Known Constraints Powder paints have disadvantages which accompany their use in all situations and preclude their use completely in others. Disadvantages are: * single-coat limitation; * no tinting capability, making exact color matching difficult; * scrupulous booth cleanup is necessary to prevent "polka dots" in subsequent paint jobs (either liquid or powder); * rejects past two times must either be stripped, which is difficult with powder, or must be recoated with two-part epoxy primer plus a liquid paint which duplicates the color and performance characteristics; * if attempting to reclaim powder for class A re-use, clean room atmosphere in spraying room is mandatory. Sieving will not remove all foreign matter. Applications which preclude the use of powder are: * zinc rich (ZRC-type coatings); * wash primer or spot repair prime; * hi-heat aluminum; * plastics, except certain types of heat-resisting material, when heated or conductive primed prior to coating. Gloss match to metal parts painted with the same material may not be acceptable, because slow heatup rate of plastic in heavy sections will increase final gloss of the finish; * CARC epoxy and urethane (military specification for vehicles); * glamour metallic; * painting of assembled machines or vehicles. 9.0 Date Case Study was Performed 1987-1992 10.0 Contacts with Citations Manufacturers Enameling Corporation 400 South Westwood Avenue Toledo, Ohio 43609-1599 Mr. Richard A. Dooley 419/385-2545 11.0 Keywords 500 Organic liquids 800 Organic gases 2097 Painting 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 07 Onsite recycling or recovery for reuse 1002 Annual cost savings 1008 Treatment/disposal cost avoided ---------------------------------------------------------- Neo-Wood Products Tiffin 1.0 Headline Nitrocellulose lacquer overspray dust is redissolved in a lacquer thinner solvent blend for reclamation and reuse. 2.0 SIC Code 2511 3.0 Name and Location of Company Neo-Wood Products Tiffin Plant 447 Wall Street Seneca County Tiffin, Ohio 44883 4.0 Clean Technology Category The process consists of redissolving dried overspray powder from wood furniture finishing. The recycling of this material enhances housekeeping and fire safety. 5.0 Case Study Summary Neo-Wood Products manufactures wood furniture. Waste is generated in paint booths where nitrocellulose lacquer is sprayed on wood furniture. Overspray dust is collected on filters and swept from the floors and walls of the booths. The collected dust is blended into a solvent which duplicates the solvent in the original lacquer. The reclaimed lacquer is strained to remove insoluble particles and pieces of filter media before use. During 1991, approximately 3,400 pounds of dust was reclaimed, which is equivalent to 5,000 gallons of 10% by weight solids lacquer. A new raw material, the dust solvent blend, was formulated by the lacquer supplier for this process. The dust is collected in the normal course of daily cleanup and stored in covered metal containers until dissolved. The daily average collection of dust for 1991 was 13.5 pounds or 19.4 gallons of reclaimed lacquer per day. This operation eliminates the need for hazardous waste disposal of lacquer dust. This technique has been in continuous use since 1986 in this plant. The quantitative information is based on the quality of dust reclamation solvent used as reported to Ohio EPA for 1991. The process was not commercially available at the time of inception. The procedure was developed "in-house" using equipment on hand. The solvent blend for this procedure was designed specifically for this purpose. 6.0 Economics Capital cost of equipment used for this recovery project was $1,000. Both items listed below were purchased used. * 1 each - mixer, Shar Dispenser, 10 horsepower * 1 each - mix tank, 200 gallon, steel The operational and maintenance costs are unavailable, but are not significant. Payback time was never calculated. 7.0 Cleaner Production Benefits Benefits gained from this pollution prevention technique include: * Elimination of disposal problems associated with a highly flammable dust and the attendant costs. * Encouragement of better housekeeping in the spray booths. 8.0 Obstacles, Problems and/or Known Constraints This technique works best with dust from lacquer that does not contain flattering agents, i.e., zinc steorate or amorphous silica, which are very difficult to resuspend after drying. The reclaimed lacquer is higher in volatile organic compound content than the virgin lacquer, therefore is less desirable from an emission perspective. 9.0 Date Case Study was Performed This technique was developed in 1986. The procedures and equipment as they are now have been in place since 1990. 10.0 Contacts with Citations Neo-Wood Products Tiffin Plant 447 Wall Street Seneca County Tiffin, Ohio 44883 Mr. Gary Larsen 419/447-9700 11.0 Keywords 711 Other nonhalogenated organic solids 2020 Coating 2094 Paint spray cleanup 05 Better housekeeping 07 Onsite recycling and recovery for reuse 09 Management strategies 1008 Treatment/disposal cost avoided ---------------------------------------------------------- Perfection Finishers, Incorporated Wauseon 1.0 Headline This facility has eliminated the use of 1,1,1-trichloroethane as a degreaser and switched to a biodegradable citrus based cleaning compound made from orange peels. 2.0 SIC Code 3741 3.0 Name and Location of Company Perfection Finishers, Inc. 1151 North Ottokee Street Wauseon, Ohio 43567 4.0 Clean Technology Category Material substitution and process and equipment modifications were implemented to eliminate the use of 1,1,1-trichloroethane in degreasing operations. A biodegradable citrus cleaning compound is now used. 5.0 Case Study Summary Perfection Finishers, Incorporated performs plating, painting, finishing and decorating operations on glass, plastic and metal. Approximately one year ago, Perfection Finishers started looking for ways to eliminate its vapor degreasers which used 1,1,1- trichloroethane. The reasoning for the change was that the chemical was increasingly becoming a target of health agencies and the Ohio EPA and has a negative effect on stratospheric ozone. The company read about a new cleaner/degreaser that was made from orange peels. This material is a commercial grade cleaning compound and is listed as biodegradable. A local distributor of this product was contacted and consulted. A power spray line was set up to try to degrease parts in the production line using this new system. This process took about six months to "de-bug". As of February, 1991, 1,1,1-trichloroethane has been completely replaced and is no longer stored or used at this facility. Currently, Perfection Finishers is experimenting with ways to save paint solvents by the incorporation of new painting methods and equipment. They are also experimenting with water based paints in the attempt to reduce volatile organic compounds. 6.0 Economics Company savings have been substantial since the switch from using 1,1,1-trichloroethane to a citrus based degreasing product. Past production practices required the use of approximately 55 gallons of 1,1,1-trichloroethane per day. Because Perfection Finishers is a small company, it is difficult to make changes even though they may result in cost savings. This change in the production line not only helped the cost of operation, it has helped to prevent the release of 35 tons of 1,1,1-trichloroethane. The company approximates cost savings of this program to be in the neighborhood of $40-50,000 a year. For a company this size, this is a substantial cost savings. 7.0 Cleaner Production Benefits This facility will eliminate the use of 1,1,1-trichloroethane emissions by 51,000 pounds per year. 8.0 Obstacles, Problems and/or Known Constraints None mentioned 9.0 Date Case Study was Performed 1991-1992 10.0 Contacts with Citations Perfection Finishers, Inc. 1151 North Ottokee Street Wauseon, Ohio 43567 Mr. Karl Shook, Plant Manager 419/337-8015 11.0 Keywords 502 Halogenated solvents 2136 Vapor degreasers 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 1002 Annual cost savings 1008 Treatment/disposal cost avoided ---------------------------------------------------------- Plasticolors, Incorporated Ashtabula 1.0 Headline This company has developed and implemented a waste minimization program which reduced waste generation by 43% during its first plan year. 2.0 SIC Code 2851 3.0 Name and Location of Company Plasticolors, Inc. 2600 Michigan Avenue Ashtabula, Ohio 44004 4.0 Clean Technology Category Process raw materials modification and process modifications were undertaken by Plasticolors, Incorporated, to implement their goal of waste minimization. 5.0 Case Study Summary Plasticolors, Inc. manufactures dispersions, additives and colorants. In early 1990, the company began a waste minimization program to reduce the amount of waste generated and to reuse materials when possible without affecting product quality. The amount of resinous and water waste generated during the twelve months prior to their waste minimization program (WASTEMIN) was 556,100 pounds. During their first plan year it was 315,478 pounds, a reduction of 43%. Overall production during this time decreased by 17%. In addition, 12,227 pounds of solid waste (office/computer paper and cardboard) was sent out for recycling rather than a landfill where it had previously been sent. All areas of Plasticolors' operation have been involved in the WASTEMIN project. All employees have received various degrees of training and education regarding the proper segregation, collection, reuse and/or disposal of residual materials and their associated costs. Segregation and separation of flammable materials from combustible materials, and pourable from thick liquids prior to disposal, has been a common practice for many years. However, Plasticolors' Waste Minimization Team has also begun segregating material for reuse in the manufacture of new or existing products. Initially, Plasticolors' waste reduction program consisted of collecting and reusing resins. These resins were used to purge out sandmill chambers and related equipment between product runs. This material was identified, collected and stored for use in the next batch of material to be made. Production scheduling was also incorporated into this process so that the colors being processed were in the proper sequence. Two additional mill chambers and pumps were purchased to reduce the frequency of cleaning and, consequently, the amount of purge generated. Plasticolors' largest reduction in generated waste has come from the production area. The lab has also been involved in the WASTEMIN project. The lab revised their procedures, collects smaller quality control samples and retains samples. The pollution prevention techniques concerning minimization and/or reuse of resinous and water waste were conceived, developed and implemented by the Waste Minimization Team. This team was made up of employees from all areas of the company, from line employees to office managers. The team utilized the talents, abilities and input of all the employees. The seven member team was charged with accomplishing a first year 25% waste reduction. These reduction techniques have been used since their implementation. The technology and processes incorporated by Plasticolors were not commercially available. 6.0 Economics Investment costs Two sandmill chambers, pumps and associated equipment $24,556 Operating and Maintenance costs Waste Minimization team 350 hours $5,968 (comprised of seven members meeting weekly) Employee Training 140 hours $2,387 (Procedural and awareness) The payback period was less than one year. The total investment during the plan period of October 1, 1990 to September 30, 1991 was $32,911. Using the previous twelve months as a baseline, the net savings were $83,480 of which $55,656 was divided among all employees as a waste minimization bonus. This amounted to each employee receiving a check for approximately $500. 7.0 Cleaner Production Benefits The reduction in waste and its associated costs had a positive financial impact on Plasticolors. Additional resources are now available for use in other growth oriented areas of their business. The reduction has also had a positive impact on Plasticolors' team concept of doing business and it reinforced efforts to involve operators and technicians in the problem solving process. Plasticolors has strengthened its relationship with the local community in which it is located. 8.0 Obstacles, Problems and/or Known Constraints None of significance. 9.0 Date Case Study was Performed 1990-1992 10.0 Contacts with Citations Plasticolors, Inc. 2600 Michigan Avenue Ashtabula, Ohio 44004 Mr. Jim Ogren, Mr. Ray Brockett and Mr. Don Herndon 216/997-5137 11.0 Keywords 114 Scrubber water 512 Reactive or polymerized organic liquid 1042 Rinse baths, spray, etc. 1047 Surface cleaning 1048 Tank cleaning 2015 Chemical processes, other 01 Equipment or technology modification 02 Process modification or substitution 05 Better housekeeping 06 Waste stream segregation 07 Onsite recycling or recovery for reuse 10 Wastewater reduction 1002 Annual cost savings 1003 Capital costs 1005 Payback period 1008 Treatment/disposal cost avoided [Figures 1-3 follow, one per page] ---------------------------------------------------------- PPG Industries Cleveland 1.0 Headline This facility uses an ultrafiltration/reverse osmosis primer process water reclamation unit (UF/RO unit) to reclaim water for reuse in production cleaning. 2.0 SIC Code 2851 3.0 Name and Location of Company PPG Industries Coatings and Resins Division Cuyahoga County 3800 West 143rd Street Cleveland, Ohio 44111 4.0 Clean Technology Category The PPG Industries' UF/RO unit is used for water reclamation. 5.0 Case Study Summary The PPG Cleveland plant produces three lines of automotive coatings: solvent based topcoats, water borne topcoats and water based primers. To assure quality in the production of water based primers, thousands of gallons of water are used weekly for cleaning during the process. The water that is used becomes contaminated with heavy metals and solvents, thereby requiring disposal as a hazardous waste. Typically, 400,000 gallons of water are disposed of annually. To alleviate this burden, the plant began evaluating in 1991 the potential opportunities available to minimize this waste. In April 1992, after one year of research, the plant designed and installed a combined UF/RO unit to reclaim the water for reuse in production cleaning. A process flow diagram is included as part of this case study report. The batch UF/RO process functions primarily as a progressive filtering system. First, the waste feed water is pre-filtered to remove large solids. The ultrafilter separates suspended solids and high molecular weight particles. Reverse osmosis removes additional smaller sized impurities. The final water is then placed in storage where it can be drawn throughout the primer production areas for reuse in cleaning. Although the water is not processed to 100% purity, the solvents that remain actually aid in the cleaning process. The primary benefit of the UF/RO water reclamation unit is an estimated 95% reduction in the volume of hazardous waste requiring disposal (from 400,000 a year to 20,000 gallons a year). As a result, 380,000 of water a year will be conserved. The UF/RO unit indirectly saves energy by reducing fuel costs related to the transportation and incineration of the waste water. The installation of the unit did not require any changes in the production process nor did it affect the rate of product manufacturing. The new waste stream that is generated from the reclamation process, which is basically a highly concentrated waste water, can be easily handled under the present waste management procedures. The UF/RO unit is designed to batch process 5,000 gallons of waste water a week. Approximately 4,000,000 gallons of water based primer are produced annually. Therefore, roughly one gallon of waste is generated for every ten gallons of product manufactured. The initial batch run of the UF/RO unit was conducted the week of May 4, 1992. Some filter fouling problems occurred due to contaminants encountered during the unit installation. Second batch run began the week of May 18, 1992. All quantitative information presently available is estimated. Both ultrafiltration and reverse osmosis have long been commercially available. The UF/RO unit was not specifically designed for PPG. This project was one of the three 1991 winners of the U.S. EPA/DOE National Industrial Competitiveness through Environment, Energy and Economic (NICE3) Grants. The U.S. DOE announced the 1992 NICE3 Grant at a news conference at the PPG Cleveland plant in April 1992. 6.0 Economics A detailed breakdown of capital costs and equipment specifications is not available. However, the following total estimates are provided: Equipment and installation $406,000 Training $ 5,000 Operational costs of the UF/RO unit are estimated at $130,000 a year, including personnel time. It is estimated that it will take eight hours per week to operate the unit. The UF/RO project is estimated to produce an annual net savings of $250,000. The payback for this investment is estimated to be 7.2 months. 7.0 Cleaner Production Benefits The benefits of this project include: * the minimization of hazardous waste transportation and disposal costs; * the conservation of energy in waste transportation and incineration; * the conservation of water; * business competitiveness promoted by the cost savings; * improved public relations; * reduced liabilities on hazardous materials incidents. 8.0 Obstacles, Problems and/or Known Constraints There have been no constraints in the implementation of the reclamation unit. 9.0 Date Case Study was Performed The UF/RO unit installation was completed in April 1992. 10.0 Contacts with Citations PPG Industries Coatings and Resins Division Cuyahoga County 3800 West 143rd Street Cleveland, Ohio 44111 Ms. Maura C. Tinter, Environmental Coordinator 216/671-7752 11.0 Keywords Aqueous waste with heavy metals and solvents 2018 Aqueous waste with heavy metals and solvents Coating production 07 Onsite recycling or recovery for reuse 1003 Capital costs 1008 Treatment/disposal cost avoided Resource conservation Regulatory incentives [Figure 1, a full page graphic, follows] ---------------------------------------------------------- Premix, Incorporated North Kingsville 1.0 Headline A solvent replacement task force has made solvent substitutions and is investigating further substitutions. 2.0 SIC Code 3089 3.0 Name and Location of Company Premix, Incorporated P.O. Box 281 North Kingsville, Ohio 44068 4.0 Clean Technology Category Premix, Incorporated has always recycled their solvents and will continue to do so in the future. Cleaning solvents are being replaced with solvents that are less hazardous. 5.0 Case Study Summary Premix is a manufacturer of thermoset molding compounds which are compression or injection molded into fiberglass reinforced plastics. Premix both uses and commercially sells its own molding compounds. The molding compounds are basically manufactured in three forms: sheet molding compound (SMC); bulk molding (BMC) and thick molding compound (TMC). In the manufacture of SMC, BMC and TMC, various formulations of resins, pigments, organic peroxides, enhancers, fillers and reinforcement (glass) are mixed together to obtain the molding compound. [NOTE: on the original hard copy, each mention of TMC has the letters TM (for Trade Mark) in superscript following it.] During this manufacturing process, various things (mixers, mixing vessels, SMC and TMC compounding machines, tools, etc.) become saturated with the fiberglass "paste" and must be cleaned prior to making different formulations. These formulation changeovers utilized solvents to assist with the cleaning process. Solvents used in the cleaning process have changed over the years to reflect environmental and health and safety concerns. One consistent characteristic, however, is that Premix will only use solvents that can be recycled by a commercial solvent recycler/supplier. Up until 1988, Premix used a solvent blend that contained methylene chloride. With the health and safety of employees in mind, the company changed from the methylene chloride based solvent to a solvent that contains toluene, 1,1,1- trichloroethane, a chlorofluorocarbon (CFC) and two other volatile organic compounds (VOCs). Its hazardous waste characteristics are D001, F002, F003 and F005. This solvent did not work as well as the methylene chloride solvent but was acceptable in that it still allowed the company to maintain rapid formulation changeovers. Because this solvent contains 1,1,1-trichloroethane and a CFC, it must be phased out within the next few years. This phase out is taking place because of concerns regarding the stratospheric ozone (the Montreal Protocol). As a result, Premix realized it had a limited amount of time to located a replacement for the solvent. From 1990 through 1992, a loose-knit group of environmental, health and safety, material management and first shift production personnel, along with a representative from the solvent recycler/supplier, attempted to locate an alternative solvent. Considerations for solvent replacements included the evaluation of their ability to be recycled, their hazardous waste characteristics, how well they would work in production (especially during quick changeovers), their content of CFCs and other ozone-depleting chemicals (ODCs) and their VOC content. In 1991 and 1992, several studies were conducted using a solvent mixture of materials such as dipropylene glycol methyl ether and propylene glycol methyl ether acetate. The studies included thickening the mixture to enhance the physical removal of paste wastes and other similar additives. Characteristics of the new solvent mixture are that it contains no VOCs and only has the hazardous waste characteristic of D001. In the spring of 1992 the change of solvents was made. All cleaning in Premix's compound manufacturing area was to be accomplished using the new solvent. Although the solvent worked well as a cleaner, it left an oily residue on several pieces of quality sensitive production equipment. Because of the solvent's low volatility, it remained on the equipment for an unacceptable period of time. Two options are then evaluated to remove the excess solvent. The first option would be to use a solvent with a lower flashpoint to remove the primary solvent. The second option would be to use soap and water to remove it because it is soluble in soap and water. The options were evaluated, and the second option was chosen. After adding the soap and water cleaning step, additional problems occurred. Cleaning time (down time) doubled and the soap and water residue created similar product quality problems. Another informal meeting of the internal group and the solvent recycler/supplier took place. At this meeting, it was concluded that the new solvent would be used for cleaning that is not time critical (mixers, tools, etc.). For time critical processes, such as quick changeovers, it was agreed not to go back to the CFC/ODC solvent but to temporarily go to a solvent mixture of xylene and another VOC. Its hazardous waste characteristics are D001 and F003. This was considered to be a step back, but still a step above the CFC/ODC solvent. It was decided that this solvent would be a temporary solution until an acceptable cleaning procedure could be found for the non-VOC containing solvent. An aggressive group entitled the Solvent Task Force was formed. The Task Force kept all of the same individuals from the previous group (environmental, health and safety, material management and first shift production) but also added a chemist, a plant engineer, a production/quality engineer and second and third shift production personnel. Additionally, it was concluded that the organization should be changed from an informal, loose-knit group to a highly organized group that follows Total Quality Management principles. At this point in time, all of the Task Force's parameters have been established and the first informational/organizational meeting of the Task Force occurred late in July. Anticipated date of completion to obtain an acceptable cleaning method (or methods) with the new solvent is spring 1993. 6.0 Economics The only investment costs that have been and will be incurred in the future will be those related to employees' time spent meeting and testing new cleaning techniques. Operational costs, maintenance costs and payback time have not been determined. 7.0 Cleaner Production Benefits Using the new cleaning solvent for cleaning materials that are not time critical (mixers, tools, etc.) does a better cleaning job than the solvent that has the CFCs, ODCs and VOCs. The new solvent will create a cleaner and safer workplace for employees. The waste codes of solvents sent for recycling have changed from D001/F002/F003/F005 waste to D001/F003 waste. By the spring of 1993, the D001/F003 waste stream will be phased out and replaced with a D001 waste stream. 8.0 Obstacles, Problems and/or Known Constraints The substitute solvent leaves an oily residue on some pieces which has to be removed, and it remains on the equipment for an unacceptable period of time. Because of this it can only be used on certain pieces of equipment. Premix has had difficulty finding a replacement solvent that meets production needs and quality standards. 9.0 Date Case Study was Performed The project was begun in 1991 and is ongoing. Completion is expected in the spring of 1993. 10.0 Contacts with Citations Premix, Incorporated P.O. Box 281 North Kingsville, Ohio 44068 Mr. Raymond A. Kovacs, Environmental Manager 216/224-2181 11.0 Keywords 502 Halogenated solvents Other solvents 2018 Cleaning Manufacture of molding compounds 04 Process raw materials modification or substitution 08 Offsite recycling or recovery for reuse (materials exchange) Worker protection Regulatory incentives Task force Improved quality ---------------------------------------------------------- Republic Engineered Steels, Incorporated Canton 1.0 Headline Waste streams containing 1,1,1-trichloroethane have been eliminated. 2.0 SIC Code 3312 3.0 Name and Location of Company Republic Engineered Steels, Inc. 2633 8th Street, N.E. Canton, Ohio 44704 4.0 Clean Technology Category Process and equipment modifications and a product substitution were implemented to eliminate the use of 1,1,1-trichloroethane. 5.0 Case Study Summary Republic Engineered Steels, Incorporated, an employee owned company, produces high quality bar and specialty steels. Republic joined U.S. EPA's 33/50 Program in May 1991. One goal was to eliminate the use of 1,1,1-trichloroethane. The chemical was utilized in the motor cleaning operation and to a lesser degree as a drying media to detect surface defects in a non- destructive testing application. A steam cleaning/detergent system is now being used for the motor cleaning operation and detergent media in the non-destructive testing application, thus eliminating all 1,1,1-trichloroethane from the facility. The project of eliminating 1,1,1-trichloroethane was carried out by the employee-owners that work in the Electric Repair Shop. After several months of study, an environmentally safe detergent based product was found. The existing operation was modified to use the steam/detergent agent. A new washing tank, steam generator and disposal system was developed, fabricated and put into service. In the original process, 1,1,1-trichloroethane liquid was heated to create the vapor used for degreasing electrical/mechanical parts, including approximately 300 motors up to five tons and associated components. As the parts hung in the tank from an overhead crane, the vapor condensed on parts and removed the grease and oils. A distillation process was used to recover the vapor to use for pressure rinsing of parts. This process required the purchase of 30,000 pounds per year of 1,1,1-trichloroethane. It generated air emissions and 12 drums per year of sludge consisting of grease, oil, 1,1,1- trichloroethane and clay absorbent. This sludge was disposed of as a hazardous waste. The new process utilizes steam, high pressure water and a detergent mixture. For implementation, Republic installed a new stainless steel collection tank and plant steam was converted to a package steam generator. The new cleaning process eliminated the use of city water for cooling the condensate. Parts are now sprayed with all or part of the new system based on the grease and oil levels, and electrical parts are put into a bake oven overnight to drive out moisture inherent to the new process. This moisture must be removed from electrical insulation before further work can be performed. In the new process, process rinse water is pumped to the Water Quality Control Center. Cleanout of the holding tank has been reduced from six times per year to one time per year. The new waste stream consists of soap, water, oil and grease. Because of this change, Republic has eliminated bulk 1,1,1-trichloroethane storage (a 500 gallon tank) and the potential spill hazard associated with storage and handling of the material. In addition, sludge transportation and disposal costs have been significantly reduced, and hazardous waste manifesting requirements have been eliminated. The following chart compares the old and new processes: [ a 2 column table appears here. SEE ORIGINAL HARD COPY] The new process takes longer; previously parts did not require constant attention, but were left to hang in the solvent vapor. Now the parts require additional attention. However, carbon dust is removed by the new process which the 1,1,1-trichloroethane was not able to remove. The elimination of 1,1,1-trichloroethane was complete on December 31, 1991. This process change and design was developed internally as an employee project. The commercial parts washing systems that were available were rejected because of high capital costs. The detergent was specifically designed to meet Republic's needs for a detergent with a moderate pH that was anti-foaming and non-toxic. 6.0 Economics The following costs include labor and material costs: Steam Jenny, model S-1000C, 350,000 BTU per hour $8,000 4' x 10' x 8' wash tank, volume 320 Cubic feet $5,000 Stainless steel plate and angle iron Piping 0 200', 2" PVC (schedule 80) $5,000 Process/rinse water pump $ 900 ______ $8,900 The following costs include operational and maintenance costs: Old New Maintenance cost $ 3,800 $ 1,280 Disposal $ 6,400 $ 1,080 1,1,1-trichloroethane $18,000 $ 0 Detergent $ 0 $ 3,500 ------- ------- $28,200 $ 5,860 Republic estimates a net savings of $22,000, with less than a one year payback time. The actual savings for the first six months after implementation was $10,700. 7.0 Cleaner Production Benefits Cleaner production benefits include: * elimination of air emissions of 1,1,1-trichloroethane; * elimination of employee exposure to 1,1,1-trichloroethane; * lowered operating costs; * elimination of hazardous waste manifesting requirements; * elimination of off-site Comprehensive Environmental Response, Compensation, and Liability Act liability; * elimination of liabilities associated with transportation and handling of 1,1,1-trichloroethane. 8.0 Obstacles, Problems and/or Known Constraints Problems in this change involved finding an appropriate detergent. The pH level and toxicity were important, because Republic did not want to impact the Water Quality Control Center and NPDES permitting. 9.0 Date Case Study was Performed This project began in the summer of 1991, and was on-line December 31, 1991. 10.0 Contacts with Citations Republic Engineered Steels, Inc. 2633 8th Street, N.E. Canton, Ohio 44704 Mr. Eric D. Howland, Manager, Power and Utilities 216/438-5306 Information for this activity was gained through washing equipment manufacturers, similar local operations and consultations with detergent/chemical suppliers. 11.0 Keywords 609 Other organic sludge 800 Organic gases 2136 Vapor degreasing Drying media to detect surface defects 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 1002 Annual cost savings 1003 Capital costs 1005 Payback period 1008 Treatment/disposal cost avoided Worker protection Regulatory incentives ---------------------------------------------------------- Textileather Corporation Toledo 1.0 Headline Excess cleaning oil is recycled. 2.0 SIC Code 2295 3.0 Name and Location of Company Textileather Corporation 3729 Twining Street Toledo, Ohio 43608 4.0 Clean Technology Category Waste stream segregation at Textileather Corporation allows for recycling and reuse of excess oil and excess compounds. 5.0 Case Study Summary Textileather Corporation manufactures vinyl coated fabrics and film, primarily for the automotive industry. Excess cleaning oil is kept separate from excess compounds generated in Textileather's coating process. Excess compounds are and have been recycled on a regular basis. The excess cleaning oil is analyzed and, based on analysis, is processed through existing equipment to a specified solids level. The processed oil is filtered and stored in bulk storage tanks prior to sale and shipment to a certain customer. Formerly, the excess cleaning oil was managed as a hazardous waste. As a waste, the excess cleaning oil was shipped to an offsite facility for stabilization, then taken to a hazardous waste landfill. No changes were made in the coating process or cleanup procedures. The described methods are employed to eliminate disposal of the excess cleaning oil as a hazardous waste. The coating process produces about 4,000,000 linear yards of goods. Goods are produced in various colors and widths, in increments of up to 10,000 yards. Each color change requires a thorough cleanup of equipment. On average, 100 gallons of cleaning oil are used per day. Most of the equipment used to process excess cleaning oil into a saleable product was available at the facility. 6.0 Economics Capital costs were less than $10,000. A pump plus a few hundred feet of ordinary steel piping were installed to supplement existing equipment. Maintenance costs are minor. Labor used to correct excess cleaning oil to saleable product offsets labor formerly required to handle the excess oil as a hazardous waste. Payback on investment was less than six months. 7.0 Cleaner Production Benefits Reprocessing of excess cleaning oil into saleable products saves about $50,000 per year. If not reprocessed and sold, excess cleaning oil would account for about 120 cubic yards of waste, on an annual basis. 8.0 Obstacles, Problems and/or Known Constraints The critical constraint is securing and maintaining customers for the reprocessed oil. 9.0 Date Case Study was Performed The recycling effort began during 1990. 10.0 Contacts with Citations Textileather Corporation 3729 Twining Street Toledo, Ohio 43608 Mr. Mike Sapovich 419/729-7566 This recycling effort was initiated and developed internally. 11.0 Keywords Excess cleaning oil Excess compound 2018 Cleaning 2020 Coating 06 Waste stream segregation 07 Onsite recycling or recovery for reuse 08 Offsite recycling or recovery for reuse (materials exchange) 1002 Annual cost savings 1008 Treatment/disposal cost avoided Saleable product ---------------------------------------------------------- Ultra Forge, Incorporated Cuyahoga Falls 1.0 Headline The solvents 1,1,1-trichloroethane and tetrachloroethylene have been completely removed from the plant as an emission source and a hazardous waste. 2.0 SIC Code 3714 3.0 Name and Location of Company Ultra Forge, Inc. 129 Marc Drive Cuyahoga Falls, Ohio 44223 4.0 Clean Technology Category Ultra Forge, Incorporated has completely eliminated the use of 1,1,1-trichloroethane and tetrachloroethylene through the source reduction technique of material substitution, made possible by the purchase of higher cost equipment to replace traditional solvent vapor degreasing equipment. Three vapor degreasing lines have been replaced over the last four years by spray washing equipment using low concentration alkaline solutions followed by spray rinses. 5.0 Case Study Summary Ultra Forge manufactures aluminum wheels and hubs for the trucking industry. The facility has three chlorinated solvent vapor degreasing lines to clean products of oil residue from machining operations and polish from a polishing operation. There were both gaseous fugitive and stack emissions of 1,1,1- trichloroethane and tetrachloroethylene from the degreasing lines as well as liquid hazardous waste that was created by periodic degreaser tank cleaning. This liquid waste was transported to a solvent recycler for treatment and resale. The amount of gaseous 1,1,1-trichloroethane and tetrachloroethylene emitted to the atmosphere in 1989 was 59,700 and 80,000 pounds, respectively. The amount of liquid solvent hazardous waste removed from the plant in 1989 for recycling was 6,000 pounds for 1,1,1- trichloroethane and 7,000 pounds for tetrachloroethylene. After extensive equipment and alkaline washing solution tests, a replacement chemical for 1,1,1-trichloroethane was found in 1989. Production rates and quality would not be decreased. Both the wash solution and rinse waters were tested to be within the parameters necessary to release this effluent to the local publicly owned treatment works as necessary to operate the spray washing equipment. No hazardous waste was created by this new process. It took a longer test and evaluation period to replace the higher boiling tetrachloroethylene used in the polishing degreasing operation. However, a non-toxic chemical solution and spray wash equipment were found in 1991 that would allow that combination to be substituted for the tetrachloroethylene degreaser with the same results as the 1,1,1-trichloroethane replacement project. Operating procedures are no more of a task than with the vapor degreasers. Energy use difference between vapor degreasers and the new spray wash equipment has not been calculated in great detail. Information on the scale of operation is not available at this time. The two 1,1,1-trichloroethane lines were replaced in 1989 and 1990. The tetrachloroethylene vapor degreaser line will be shut down at the end of June 1992. The replacement cleaner and spray equipment for that process have been proven effective and the new line will start operation at the end of June 1992. None of the chemicals or spray wash equipment was invented by Ultra Forge personnel. All of this equipment and alkaline-based solution chemicals are available from manufacturers. 6.0 Economics The three vapor degreasing lines were replaced using equipment with a capital cost of approximately $350,000. Detailed descriptions and specifications of purchased equipment is not available at this time. The cost of the new alkaline-based chemicals is less than the sum of the chlorinated solvent purchase price and disposal cost per single product manufactured. No payback time was computed in detail. The project was done to increase worker protection, to decrease spill and hazardous waste liability and to eliminate any exposure and pollution control costs under the Clean Air Act Amendments of 1990. 7.0 Cleaner Production Benefits These projects were done in order to protect the workers at Ultra Forge as well as the surrounding community and to reduce potential liability under Workmen's Compensation laws, Resource Conservation and Recovery Act and the Clean Air Act much more than any derived economic benefit. 8.0 Obstacles, Problems and/or Known Constraints The details of problems encountered can be made available upon request of an interested party. 9.0 Date Case Study was Performed The initial planning to replace the solvent vapor degreasers began in early 1989 and the entire process was completed by June 1992. 10.0 Contacts with Citations Ultra Forge, Inc. 129 Marc Drive Cuyahoga Falls, Ohio 44223 Mr. Donald J. Hagarty, President 216/929-2945 The information gained through attending various trade shows and meeting with chemical company representatives and spray wash equipment manufacturers led to the implementation of these projects. 11.0 Keywords 512 Halogenated solvents 800 Organic gases 2136 Vapor degreasing 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 1002 Annual cost savings 1003 Capital costs 1008 Treatment/disposal cost avoided Worker protection Decreased liability Regulatory incentives ---------------------------------------------------------- Van Dorn Plastic Machinery Company Strongsville 1.0 Headline Through the use of substitution this facility has totally eliminated the use of chlorinated solvent blends for a cleaning operation and has been using an alkaline soap solution, applied by a steam cleaner, for machine cleaning. 2.0 SIC Code 3559 3.0 Name and Location of Company Van Dorn Plastic Machinery Company 11792 Alameda Drive Strongsville, Ohio 44136 4.0 Clean Technology Category Van Dorn Plastic Machinery Company has implemented a material/product substitution for chlorinated solvents. An alkaline soap solution that contains an adequate rust inhibitor package is applied by means of a steam cleaner application. 5.0 Case Study Summary Van Dorn manufactures plastic injection molding machines. In 1987, the machines that Van Dorn manufactures were cleaned prior to painting with chlorinated solvent blends and virgin 1,1,1- trichloroethane by means of a pressure washer. This process generated approximately 120 gallons of waste solvent for every machine washed. This resulted in the generation of approximately 19,000 gallons of waste chlorinated solvent which was sent to a permitted facility for recycling or reclamation annually. In 1988, the decision was made to eliminate the generation of hazardous waste and reduce the enormous expense associated with the reclamation of the chlorinated solvent blends. The reasons for taking this action were not only regulatory, but also provided the company with the opportunity to exercise good management practices and realize a very substantial savings cost in return. Van Dorn decided to implement the waste minimization technique of material substitution. Upon locating an alkaline soap solution that had acceptable cleaning characteristics and a sufficient rust inhibitor package, the company began experimenting with mixture ratios and temperature ranges of the steam cleaner. It found the proper ranges to accomplish the cleaning of the machinery without sacrificing the quality of the product. This technology and process were commercially available. The need to maintain the water-tight integrity of the electrical components on the machines was of the utmost importance, due to the fact that the alkaline soap solution was water based and did not evaporate as did the solvent blends. The results of the above actions allowed Van Dorn to reduce the chlorinated solvent waste stream from 19,000 gallons per year down to zero gallons per year. 6.0 Economics * steam cleaner $1,200 * wastewater disposal facility approximately 1,000 gallons per month at $0.19 per gallon for pre-treatment and disposal This waste stream is now classified as non-hazardous wastewater containing oil and grease. It is transported off site to a permitted facility for ultrafiltration and pre-treatment prior to release. * 1988 cost of solvent disposal $43,181 * 1989 cost of wash water disposal $ 2,280 * 1989 savings on disposal $40,901 The operational and maintenance costs are minimal. There was no cost for maintaining the steam cleaner for the first year. The second year of the project, the burner on the steam cleaner had to be replaced at a cost of approximately $250. There were no changes in the operation nor in the personnel needed to do the job. The minimization project was developed to substitute the product and not change the job requirements in any way. The payback time for this project was almost immediate. Within two months the money that would have been spent on disposal of the chlorinated solvent paid for two steam cleaners and the first two drums of alkaline soap solution. 7.0 Cleaner Production Benefits Since the implementation of an alkaline soap and water wash, the facility has realized the following benefits that can be attributed to practicing sound waste minimization techniques: * a safer, more healthy working environment for employees; * movement towards the facility goal of obtaining small quantity generator status for hazardous waste management; * reduced liabilities in the management of the chlorinated hazardous waste stream and the Clean Air Act. As Van Dorn has realized a payback within two months, it supports the concept that waste minimization not only is in the best interest of the environment, but also represents sound management practices. 8.0 Obstacles, Problems and/or Known Constraints The following issues should be considered when substituting alkaline soap solutions in place of chlorinated solvents: * Rust The water based soap solution must have an excellent rust inhibitor package or bare metal surfaces will experience flash rusting. * Residue The soap must be strong enough to remove all contamination from the part or product, but if the part or product is to be painted there cannot be any alkaline residue remaining on the surface. Otherwise, the finish coat will not adhere properly and the paint finish itself will appear to have been applied over a dirty, unprepared surface. * Product dry time Forced air can be used to clear the product of any free standing soap solution. The alkaline soap solution has an evaporation rate equal to water, so it may be necessary to use forced air to accelerate dry time if time is a critical factor between the wash operation and the actual painting of the product. 9.0 Date Case Study was Performed This project was started in December of 1988 and was fully implemented by April of 1989. 10.0 Contacts with Citations Van Dorn Plastic Machinery Company 11792 Alameda Drive Strongsville, Ohio 44136 Mr. James Erclauz, Facilities Engineer 216/238-8960 Information was supplied through vendors/suppliers. 11.0 Keywords 502 Halogenated solvents 2018 Cleaning 02 Process modification or substitution 03 Product reformulation or redesign 04 Process raw materials modification or substitution 09 Management strategies 1002 Annual cost savings 1008 Treatment/disposal cost avoided Worker protection Regulatory incentives ---------------------------------------------------------- Wallbridge Coating Company Walbridge 1.0 Headline Implementation of a metal recovery and sludge recycling plan has reduced the amount of hazardous waste. 2.0 SIC Code 3479 and 3471 3.0 Name and Location of Company Walbridge Coating Company 30610 East Broadway Walbridge, Ohio 43465 4.0 Clean Technology Category Process and equipment modifications were implemented to recover zinc and nickel sulfate from a waste water stream and generate a commercially usable by-product. 5.0 Case Study Summary Walbridge Coatings is an electrogalvanizing facility staffed by 140 employees located in Walbridge, Ohio. Zinc and zinc/nickel alloy coatings are applied to cold rolled steel for the purpose of corrosion resistance. As part of the electrogalvanizing process various rinsates are generated. The wastewaters are processed through an ion exchange unit that is able to reclaim 95% of the zinc and nickel which is then returned to the process as raw materials. The remaining wastewater is pretreated and discharged to the sanitary sewer. The resulting sludge that is generated in the pretreatment process is a listed hazardous (F006) waste. Recently, in an effort to reduce their hazardous waste stream, Walbridge developed a program to sell its zinc/nickel hydroxide sludge to Hall Chemical Company. For every 1,000 tons of steel that the company coats, 21,000 pounds of hydroxide sludge is produced. Therefore, based on current production levels of this product, 740,000 pounds of hydroxide sludge will be generated per year. Future volumes could increase to 16,000,000 pounds a year. Process changes and modifications to the recovery unit were made, allowing Walbridge to recover the zinc as well as the zinc/nickel alloy material. A source was located that could use this zinc- only hydroxide sludge as feeder stock for their process. This has the potential to eliminate an additional 6,000,000 pounds of sludge from the landfill. 6.0 Economics The ion exchange unit that was installed to reclaim metals from the electroplating process was built by a company that worked with Walbridge engineers on the specific design of the unit. The total project costs including recovery and pretreatment was $5.7 million. 7.0 Cleaner Production Benefits At one time, 740,000 pounds of zinc/nickel sludge was sent offsite for land disposal. Currently, this sludge is being sent to another company for feeder stock. In return, the mixed metals carbonate generated from this material is being shipped back to Walbridge for use as raw material in their process. The recent location of a commercial use for the zinc sludge will improve these numbers even more. 8.0 Obstacles, Problems and/or Known Constraints There are currently concerns over the amount of zinc hydroxide sludge which the receiving company will be able to use, given the current market conditions. 9.0 Date Case Study was Performed This case study began in 1989 and continued through 1991. 10.0 Contacts with Citations Walbridge Coating Company 30610 East Broadway Walbridge, Ohio 43465 Mr. Thomas Moore, Vice President/General Manager Mr. Robert Killian, Environmental Coordinator 419/661-5919 11.0 Keywords 218 Other inorganic sludge 2067 Ion Exchange Electrogalvanizing 01 Equipment or technology modification 02 Process modification or substitution 07 Onsite recycling or recovery for reuse Offsite reuse (materials exchange) 1003 Capital costs 1008 Treatment/disposal costs avoided ---------------------------------------------------------- Whirlpool Corporation: Marion Division Marion 1.0 Headline A variety of source reduction activities have resulted in cost savings, reduced emissions, avoidance of disposal costs and a safer work environment for employees. 2.0 SIC Code 3633 3.0 Name and Location of Company Whirlpool Corporation Marion Division 1300 Marion-Agosta Road Marion, Ohio 43302 4.0 Clean Technology Category The employees of the Marion Division of Whirlpool Corporation have embarked on an aggressive pollution prevention program to decrease the amount of solid waste being generated by the Division, as well as improve the quality of air and water releases. The first step in their pollution prevention plan for solid waste was installation of a cardboard baler, followed by installation of compactors for trash and cardboard. Soon after that, the Division expanded its prevention program with the recycling of plastic pellets, hydraulic and gear oil and xylene. The paint department was the site of process and equipment modifications which reduced solid waste and improved air emissions. New paint application guns were purchased to improve paint transfer, and the size of the loop traveled by parts to be painted was reduced to lessen the amount of paint used. A cleaner regeneration system enabled the Division to decrease the amount of cleaner being purchased and also reduced the volume of wastewater being sent to the Wastewater Treatment Plant (WWTP) by 40,000 gallons per week. The Division realized a substantial improvement in the amount of toxic emissions produced by the paint department by switching from anodic electrostatic-coat paint to a cathodic paint to eliminate methyl ethyl ketone. An improved paste for the paint department's base material replaced the previous paste which had a Volatile Organic Compound (VOC) content of 1.6 pounds per gallon. The new paste has 0.9 pounds of VOC per gallon. Conventional paint was replaced with a high solids paint. Stoddard solvent, which is considered hazardous waste when spent, was replaced with a non-hazardous solvent for parts washing. Employee involvement, interdepartmental cooperation, and training have all been key factors the success of the Division's prevention program. An intensified housekeeping effort involving everyone at the Division has been crucial to the success of all pollution prevention efforts. Training and supervision have been important in keeping costs reasonable when changes have been implemented. When the switch to non-hazardous solvents for parts washers occurred, labor to service the parts washers was supplied by the environmental department. This was a lower cost than using an outside service but required training and supervision to ensure proper maintenance. The solvent still required the same commitment in-house for man-hours to operate and training to ensure safe and efficient operation. The compactors initially required additional manpower for segregation and operation but have now been established as part of normal operations by anyone generating the waste stream. This has cost-justified the existence of the compactors but required training to ensure proper operation and proper waste stream input. Production planning and sequencing is an integral function of the changes initiated at the Marion Division in 1991 and projected through 1995. The close interaction with the futures engineering group has resulted in establishing a proactive approach to production strategy for air emissions, which will meet both production needs and environmental regulations. The environmental and safety engineers are included in assessment of capital projects, purchases and policy addressing pollution prevention issues up front. Periodic assessment of pollution prevention activities are completed during Environmental Risk Management Committee meetings conducted quarterly. The data is then compiled by the environmental department. Review of pollution prevention activities has been in place for over five years and quantification of actual waste volumes, by installation and use of a truck scale, has been ongoing since 1987. This is essential for auditing the success of programs at Whirlpool. This method has been used for solid waste and liquid waste assessments. Air emissions have been quantified primarily through actual paint use data coupled with MUDS (Whirlpool's computer program listing actual usage data) and vendor supplied data. 5.0 Case Study Summary The Whirlpool Corporation, Marion plant, is a metal finishing appliance manufacturing facility employing 2,200 people in a three-shift operation. This plant is the world's largest manufacturer of clothes dryers. Major plant areas can be broken down into press and fabrication, plastics presses, wet phosphate, paint mix and application, and assembly. Peripheral areas include wastewater treatment, boiler operation and pyrolytic ovens used to burn the paint from hooks used on the conveyor lines. Pollution prevention was initiated with waste minimization efforts in the mid-80's and extended from that effort to the current plan. The recycling of cardboard began with the purchase of a baler, which created a dust and particulate problem and was replaced by a compactor. The compactor was very successful at reducing volumes and allowing efficient recycling. Separation of solid waste was accomplished by installing a two-compactor system in 1990. These initial efforts were successful because of employee involvement and good management practices. Cost savings were realized from the recycling of cardboard. This recycling project led employees to work with vendors to design plastic returnable containers to lessen cardboard waste. The Marion Division is undergoing extensive changes in production planning. Just-in-Time inventory, Kanban and Point of Use Supply strategies are being implemented. These manufacturing principles will assist in efforts to minimize waste and prevent waste production. Use of employee involvement teams has been crucial to identify waste production areas. Through their efforts the use of returnable containers has been implemented in the following areas: lint screens, harnesses, timers, thermo discs and heat elements. This practice is too new to quantify but the effect will be decreased cardboard waste generation, decreased drum/material disposal, and increased attention to generation quantities. An Environmental Risk Management group has been in place since 1988 to review progress on environmental projects. The eight- member group, consisting of the environmental engineer and staff personnel, meets on a quarterly basis. In addition, they receive information from the environmental department on current regulations and compliance status of ongoing programs and projects. All of the directors from the Marion Division are a part of this group, which ensures that input from each department is incorporated into decisions regarding environmental efforts. This approach allows the exchange of information from one department to another and aids in prioritizing projects. Each year summary environmental reports are prepared. Many of the projects initiated early in the process were concerned with recycling and waste minimization. Two crucial projects were initiated in 1990 to comply with new regulations in the area of hazardous waste minimization. First, a 105 degree Fahrenheit flashpoint parts washer solvent, which as a hazardous waste, was replaced with a 140 degree Fahrenheit flashpoint which is a non-hazardous waste. The second was the installation of a solvent recovery still to recover xylene from xylene paint feed. Xylene is used at the Marion plant to clean paint guns. The parts washers had traditionally been serviced by an outside contractor. However, in 1988, the process was switched to maintenance by Whirlpool personnel with the use of the non- hazardous solvent. The parts washers were justified on the basis of a cost avoidance for hazardous waste handling and disposal. The xylene recovery still was justified on the basis of the regulatory requirement for waste minimization. The still was not cost justifiable initially, due to the increased cost for disposing of still bottoms and the labor required to operate the still. Review of processes beyond minimization began in 1990. The most extensive review has been in the area of air emissions. This was driven by the 1990 Clean Air Act and the economy of efficient production. In 1988, the Marion Division reported 1,684,714 pounds of Hazardous Air Pollutants (HAPs). To determine the feasibility for Whirlpool to participate in the voluntary 33/50 Program, an extensive review of past Superfund Amendments and Reauthorization Act (SARA) reporting was coupled with actions taken to reduce levels of emissions and total chemical use. This review was extended to present and future projects. When the Clean Air Act Amendments of 1990 were passed, it included the provision that a 90% reduction from the base year emission levels would allow for an additional six year compliance period for the remaining 10% reduction. This provided further impetus to closely examine Marion Division's options to reduce emissions at the source. The first major action taken by Whirlpool included extensive interaction with its paint suppliers. The "futures" engineering group and the paint department engineers relied upon data crunching to confirm status and probability of success of proposed strategies. A switch to high-solids paint was completed in 1991. This resulted in a significant reduction of 245,000 pounds of VOC emissions per year from the previous conventional paint use and a 40% reduction in emissions from 1987 levels. The high-solids paint transition increased production overtime for a three-month period for a "learning curve". This paint is much more sensitive to showing hand prints and requires more expertise handling products which have been painted. The high solids paint was a commercially available option. Material and training were available but expensive to implement. Emphasis on reduction of air pollution was critical to drive transition. Flow-coat paint application was replaced by E-coat in July 1992. This will result in a reduction of 80 tons per year. These changes are anticipated to reduce levels of the seventeen targeted chemicals by 62% by 1995. Another potential change in the paint department could eliminate the need for one entire paint system. Workers will be assigned new duties but jobs will not be lost. There are no new waste streams created by this switch. Volume of solid waste and air emissions will be tremendously decreased. This potential change theoretically represents an additional 30% reduction in VOC emissions from 1987 levels. Lesser actions to achieve reductions have included: the purchase of new paint application guns to increase transfer efficiency; reduction of lead content in raw paint material by the vendor; elimination of lead chromate in raw material; decreased travel time for parts to be painted to increase transfer efficiency, which resulted in a reduction of 390,000 pounds reduction per year; change of vendors to eliminate methyl ethyl ketone (product substitution), which resulted in a reduction of 79,000 pounds per year; and change from one resin to another (product substitution) resulted in a reduction of 295,000 pounds per year. The paint application area experienced positive results from the process and equipment modifications. The changes reduced over- spray, thus reducing waste generation and scrap generation. The modifications did not have an adverse impact on production. The change in July 1992 eliminating flow-coat paint had a significant reduction in VOC emissions and eliminated the flow-coat drip sheet waste stream. Flow-coat plastic drip sheets are placed beneath the conveyor lines to catch drippings from the water- based paint. Production rates have not and will not be impacted by the switch of this system to an electrostatic deposition paint system. Two major projects have been initiated at the WWTP in the recent year. One was part of a supplier request to increase efficiency of cleaner use (cleaner regeneration). The second was the installation by the supplier of an automated system to control chemical feed and water use of the wet phosphate system. Previous cleaner usage was inefficient since the cleaner was maintained in the tank until spent and then discharged full volume to batch treatment at the WWTP. Batches of 8,000 gallons were collected to a total volume of 40,000 gallons or more per week. This waste stream required the addition of acid to separate oil and alum to break emulsions. The oil was then disposed of as a waste oil for a disposal cost of $0.20 per gallon. The water layer required the addition of lime and clarification processes to discharge. The supplier installed a regeneration system which allowed cleaner regeneration and reuse. This decreased the flow of wastewater to the WWTP to 1,000 gallons per week. Concentration and required modifications to the treatment process made the waste stream difficult to treat. An investment of $10,000 in capital equipment and $30,000 in annual operating chemical costs was required up front. The supplier is continuing to research the feasibility of reusing the treatment chemical. This would decrease annual operating costs to $10,000 per year. Segregation of waste might allow reuse. This possibility is under investigation. Whirlpool Corporation purchased the Marion plant in 1955. The wet phosphate system is one of the oldest operating systems within the complex. This system previously was dosed manually in response to operator testing of chemical concentration levels in different stages. The automated system modernizes the process to allow electronic control of chemical feed rates and water use rates in direct response to automated testing equipment. This system has been in place since mid-1991 and has not shown quantifiable improvement in water use, although chemical use has decreased. The cost of installation in this instance would not offset the savings. Detailed cost studies for cleaner treatment are available from the Marion Division. The cleaner regeneration is two-thirds of the way through implementation and debugging. The regeneration process has proven effective and the WWTP batch treatment is undergoing further experimentation to improve efficiency. If the potassium hydroxide can be reused to break out the oil in the regeneration waste stream, a cost savings will be realized of $30,000 per year in operating expenses. Filtration as used in the cleaner regeneration was available but was adapted specifically to the system and was the first installation by the supplier. The specific system is not commercially available. Equipment in place at the WWTP was modified to handle the concentrated waste stream and represented further capital and operating expenses. For the automated system, the supplier had a system designed and commercially available. Effluent toxicity limits are a very new concept to wastewater treatment and an outside contractor was utilized as the source laboratory and consultant in this endeavor. 6.0 Economics The switch to E-coat will result in a savings of $165,000 per year from flow-coat operation. For cleaner regeneration, if the potassium hydroxide cannot be reused, the payback period is expected to be three years. If the potassium hydroxide can be reused three times then the payback period is one year. The automated system does not show a payback. At present estimates the cost of operation would be $30,000 per year. High-solids paint showed a payback of roughly one year for training time and equipment modification. 7.0 Cleaner Production Benefits Pollution prevention will provide a more healthy atmosphere because of the tremendous reduction in air emissions from the base year of 1987. This change is driven by regulatory compliance. The changes to achieve compliance with anticipated standards of the Clean Air Act Amendments of 1990 should not be financially prohibitive. Sufficient time should be available to respond appropriately to the regulations assuming the proposed change is technologically feasible. Changes to achieve compliance with the Clean Water Act are extremely prohibitive financially because of unfamiliarity of the tested parameter and the protocol for Toxicity Identification/Reduction Evaluation (TI/RE). Increased public awareness and the "Right-to-Know" are leading to more interest and knowledge of industrial efforts to prevent pollution. The involvement of plant personnel in areas such as returnable containers is testimony to the outstanding success possible with management and production work force teamwork. Public relations will be improved as the community is made aware of the efforts taken to stop pollution at the source. 8.0 Obstacles, Problems and/or Known Constraints During the cleaner regeneration process, the Marion Division encountered such a highly-homogenized oil that break-out by routine treatment methods proved unsuccessful. This resulted in an expenditure of an additional $40,000 for hauling waste oil, until proper treatment methods were established. Continued experimentation on the treatment system increases the payback period. Extensive changes have resulted in a re-evaluation of the air systems. The following are obstacles that have been encountered: plant lay-outs; redesign of flow-coat area to accommodate E-coat; and difficult transitions in an operating plant to allow installation of "new" systems without disrupting a working system. 9.0 Date Case Study was Performed Cleaner regeneration completed in February 1991. The automated system was completed in October 1991. High-solids paint transition July 1991, for Ransburg 1, and October 1991 for Ransburg 2. 10.0 Contacts with Citations Whirlpool Corporation Marion Division 1300 Marion-Agosta Road Marion, Ohio 43302 Ms. Mary Jakeway 614/383-7607 11.0 Keywords 105 Alkaline solution with metals but no cyanides 108 Spent caustic 117 Other organic liquid 202 Lime sludge with metals/metal hydroxide sludge 309 Empty or crushed metal drums or containers 503 Nonhalogenated solvent 506 Waste oil 509 Organic paint, ink, lacquer or varnish 602 Still bottoms of nonhalogenated solvents or other organics 703 Solid resins or polymerized organics 1014 Degreasing 1018 Drums, storage, disposal 1019 Filtration 1029 Maintenance 1032 Metal cleaning 1041 Recycling 2047 Electrostatic finishing 2050 Emulsion breaking 2079 Metal cleaning 2080 Metal finishing 2094 Paint spray cleanup 2117 Process water treatment 2130 Surface cleaning 2137 Wastewater treatment 4001 Drying 4007 Pyrolysis 01 Equipment or technology modification 02 Process modification or substitution 04 Process raw materials modification or substitution 05 Better housekeeping 06 Waste stream segregation 07 Onsite recycling or recovery for reuse 09 Management strategies 10 Waste reduction audits 11 Wastewater reduction 1002 Annual cost savings 1003 Capital costs 1004 Material value 1005 Payback period 1006 Return on investment 1008 Treatment/disposal cost avoided 2001 Implementation ---------------------------------------------------------- York International Corporation Elyria 1.0 Headline Toxics Release Inventory emissions have been reduced by 90% over four years through process modifications and material substitutions. 2.0 SIC Code 3585 3.0 Name and Location of Company York International Corporation 745 Industrial Park West P.O. Box 4022 Elyria, Ohio 44036 4.0 Clean Technology Category Substantial pollution prevention has occurred through process modifications and material substitutions in metal cleaning operations. Changes were investigated in painting operations. 5.0 Case Study Summary York International Corporation is a heating and air conditioning manufacturer. The two major areas of pollution prevention centered on York's vapor degreasing operations in the coil manufacturing department and paint line facility. Incentives were environmental concern and cost abatement. Process modifications allowed York to change from a vapor degreasing operation to cleaning of return bends with a hot water and detergent solution. Material substitution allowed the company to replace post painted sheet metal parts with pre-painted coil stock. In 1989, the company was using an open top vapor degreaser to clean the return bends on the coil assemblies. They sent a total of 5,610 gallons of used tetrachloroethylene off site for disposal. In the fall of 1989, York removed the vapor degreaser and installed a wash tank. The parts are now immersed in a bath of hot water and detergent. They are then rinsed in clean water and allowed to drain and air dry. In 1991, the company disposed of 3,300 gallons of non-hazardous waste water from this operation. Not only was the volume of waste generated reduced, but the waste changed from a hazardous to a non-hazardous waste. The equipment within the paint line facility was old and somewhat inefficient. There were two automated water wash booths for primary application of paint and two dry filter booths for manual reinforcement and touchup. There was a five stage washer, a dry- off oven and a bake oven. Hazardous waste generated by the paint line for 1990 included 8,910 gallons of solid sludge, 21,065 gallons of liquid and 2,640 gallons of xylene based solvent. There were also 3,630 gallons of non-hazardous waste water generated from the booths and approximately 6,000 gallons of non-hazardous water and sludge generated from the washer. York had investigated updating its spray equipment at a cost of approximately $100,000 and had spent considerable time working on this project. The proposed change would have reduced pollution levels by around 30%. However, York opted to eliminate the process altogether and switched to pre-painted steel. The economics provided a perfect opportunity to not only reduce the associated pollutant levels, but to eliminate them entirely at the York facility. 6.0 Economics The total cost for the washer, including installation and miscellaneous items, came to approximately $35,000. With annual savings of $51,000, the payback time was just over eight months. The cost to modify the dies was approximately $360,000 over a two year phase-in period. $71,450 was spent on removal of the paint line. With annual savings of $644,800, the payback time was just over eight months. 7.0 Cleaner Production Benefits York has been able to realize substantial annual savings while providing a safer environment for employees and the community. The burden of record keeping and filing environmental reports has been lessened since they no longer have to report on paint and tetrachloroethylene usage. They no longer have to maintain air permits for the vapor degreaser, paint booths, washer, dry-off oven and bake oven. The water usage has gone from around 44,000 gallons per day to around 20,000 gallons per day, allowing York to voluntarily surrender its industrial wastewater discharge permit to the City of Elyria. This was done while production and the number of employees doubled. 8.0 Obstacles, Problems and/or Known Constraints York found that many people have a resistance to change. The detergent York is now using does not clean as well as the tetrachloroethylene did. York had to decide what degree of cleanliness was really required versus what was done in past history. The paint line removal meant a total re-education of plant personnel on handling of finished material. The pre-paint finish is of better quality as proven by a salt spray test, and in general has a better appearance. However, adjustments had to be made for proper handling of the coated material for press and forming operations. The company did not provide for a touchup or paint repair area to force the issue of proper material handling. The types of changes made were in line with readily available technology and did not require extensive capital expense. 9.0 Date Case Study was Performed The vapor degreaser was taken out of service in September 1989 and removed from the building during November of that year. The paint line removal was phased-in over a two year period. It was a slow process to reduce the amount of material going though the paint line and coordinate this with die changes and availability of pre-painted steel. York ceased painting at the end of July 1991. Equipment removal was completed in October of 1991. 10.0 Contacts with Citations York International Corporation P.O. Box 4022 Elyria, Ohio 44036 Mr. Earnest C. Killion, Senior Manufacturing Engineer 216/323-5561 ext. 336 Other companies provided valuable information to York. For further assistance, please contact Mr. Killion. 11.0 Keywords 512 Halogenated solvents 513 Nonhalogenated solvents 2136 Vapor degreasing 2079 Metal cleaning 02 Process modification or substitution 04 Process raw materials modification or substitution 09 Management strategies 1002 Annual cost savings 1003 Capital costs 1005 Payback period 1008 Treatment/disposal cost avoided ---------------------------------------------------------- Appendices Appendix A Initial Guidelines to Completing the Ohio Pollution Prevention Case Study GUIDELINES TO COMPLETING THE OHIO POLLUTION PREVENTION CASE STUDY March 1992 INTRODUCTION In an effort to promote pollution prevention success stories in Ohio, the Ohio EPA Pollution Prevention Section has prepared the following "Guidelines to Completing the Ohio Pollution Prevention Case Study". These guidelines are adapted from the U.S. EPA Pollution Prevention Information Clearinghouse (PPIC) Case Study Format. The Ohio EPA encourages companies that are practicing pollution prevention to utilize these guidelines to publicize their efforts. If you have any questions or comments about these guidelines, please contact the Ohio EPA Pollution Prevention Section at (614) 644-3469. Ohio EPA is compiling this information for a report on pollution prevention in the Lake Erie Basin portion of the state. Your response would be appreciated by May 1, 1992. 1.0 HEADLINE The headline is a short phrase or description of the case study, including quantitative descriptions of the industry or process, waste type, and pollution prevention techniques used to limit waste production. The headline should also describe what factors caused you to pursue pollution prevention (e.g., compliance costs, regulatory burdens, good management practices, cost savings, etc.). 2.0 SIC OR ISIC CODE Use the four-digit Standard Industrial Classification (SIC) code(s) that best describe(s) the industry segment(s) referenced by the case study. Use as many SIC codes as necessary. However, place the primary SIC code first. A listing of the SIC codes is attached. Be sure to use the most specific SIC code available (i.e., first use four-digit code, then three-digit code, and so on). Specify International SIC codes with an "I" before the digit classification (e.g., I2216). 3.0 NAME AND LOCATION OF COMPANY Please identify the name and location of the facility that implemented the pollution prevention case study. The address (i.e. street, city, state, county, zip code) should also be included. 4.0 CLEAN TECHNOLOGY CATEGORY This section should include a brief description of the processes behind the pollution prevention activity referenced in the case study, such as: * Periodic assessments * Process/equipment modifications * Recycling, reuse and reclamation * Material/product substitutions * Training and supervision * Housekeeping * Production planning and sequencing * Waste segregation and separation 5.0 CASE STUDY SUMMARY This section should include a comprehensive description for the following areas: 5.1 Process and Waste Information: Describe the relevant original manufacturing process or area of the plant to which pollution prevention techniques apply, the physical state of the waste stream (solid, liquid, gas or sludge), the changes in the process resulting from the pollution prevention technique, and a description of any positive or negative effects on the wastes, products, or production rates after new technology implementation. This description should include any changes in: * Products or production rates resulting from the application * New or existing waste stream generation and composition * New or existing raw materials and consumption rates * Energy usage * Operating procedures 5.2 Scale of Operation: Describe the size of the process or operation. If possible, include quantitative information on the amount of product being produced or manufactured and the amount of waste being generated. 5.3 Stage of Development: Describe the stage of development the pollution prevention technique is (was) in at the time the case study was performed. Also, include whether the quantitative information provided is actual or estimated. 5.4 Level of Commercialization: Indicate whether the technology or process was commercially available at the time of the case study. Indicate whether or not the equipment and/or materials were readily available or if they were specially designed for the application. 5.5 Material/Energy Balances and Substitutions: Tabulate actual quantitative changes in material generation and use prior to, and resulting from, the implementation of the pollution prevention technique. Use the following table as a guide to include quantitative information (with corresponding units) concerning all affected waste streams or products. Designate "NA" where information is not available. Material Category Qty. Before Qty. After Waste Generation Feedstock Use Water Use Energy Use 6.0 ECONOMICS This section should include a summary of the costs and savings reported in the case study. 6.1 Investment Costs: Summarize all capital costs and provide a detailed description of the purchased items or services. Include specifications for each item (i.e., size, quantity used, capacity, etc.). 6.2 Operational and Maintenance Costs: Describe changes in the operational and maintenance costs (per month or year). Also describe changes in personnel or work hours required to implement the pollution prevention technology. 6.3 Payback Time: Describe the approximate payback period for the particular pollution prevention technology used in the case study (total investment/net savings per year). 7.0 CLEANER PRODUCTION BENEFITS This section should include a detailed discussion of the benefits resulting from the pollution prevention technique, including but not limited to: * Economic benefit * Improved public relations * Reduced liabilities * Changes in regulatory compliance 8.0 OBSTACLES, PROBLEMS AND/OR KNOWN CONSTRAINTS This section should include a description of the technical constraints that have or could prevent technology implementation (i.e., physical, chemical or biological limits of a manufacturing or treatment process); a description of any regulatory barriers in implementing the pollution prevention technology; and, a description of all other problems encountered during implementation not previously listed. 9.0 DATE CASE STUDY WAS PERFORMED This section should include the actual date the pollution prevention measures were initiated and the completion dates of any intermediate or final pollution prevention projects. 10.0 CONTACTS AND CITATIONS This section should include a description of the reference material used to implement the pollution prevention project(s). 10.1 Type of Source Material Identify the type of source material used. Examples include: * book or chapter * journal * organizational report * conference proceedings * unpublished material * other (specify) 10.2 Citation: Identify the citation for the document for the material abstracted. Include author(s); title; volume; number; and month and year of publication. Include the National Technical Information Service (NTIS) number if it is available through that system. 10.3 Level of Detail of the Source Material: Indicate whether or not additional detail is available in the source document for this case study. If so, briefly describe the additional material. 10.4 Industry/Program Contact and Address: Identify the name, address, and phone number of the person who can be reached for further information concerning the case study. 10.5 Abstractor Name and Address: Identify the name, organization and address of the person preparing the case study abstract. 11.0 KEYWORDS This section should include keywords from Appendices A through D which are used to identify and cross-reference case studies. 11.1 Waste Type: Select the keyword(s) from Appendix A which identifies the conventional waste(s) that is/are acted on by the pollution prevention option. Do not identify the waste(s) generated after implementing the pollution prevention technique. 11.2 Process Type/Waste Source: Select the keyword(s) from Appendix B which identifies the original industrial process(es) or source of waste that is/are modified by the pollution prevention technique. 11.3 Waste Reduction Technique: Select the keyword(s) from Appendix C which identifies the techniques implemented at the facility which are principally responsible for reducing waste generation. 11.4 Other Keywords: Select the keyword(s) from Appendix D which accurately describe the case study and may assist the user in locating this abstract, including: * Environmental media (i.e., air, land or water) * Product names * Feedstock * Special incentives * Geographic or institutional keywords (i.e., Ohio, U.S. EPA, etc.) Use as many keywords as deemed appropriate. If you do not find ideal keywords, you may add new ones to the list. 12.0 ASSUMPTIONS List any assumptions used when abstracting. Reference the sections where the assumption was made. Any discrepancies found in the source document should also be noted. 13.0 PEER REVIEW Indicate whether or not the source material has gone through a formal review process. Indicate Yes, No, or Unknown for each reference. ---------------------------------------------------------- Appendix B Abbreviated Guidelines to Completing the Ohio Pollution Prevention Case Study GUIDELINES TO COMPLETING THE OHIO POLLUTION PREVENTION CASE STUDY June 24, 1992 Your response would be appreciated by July 10, 1992. Thank you in advance for your cooperation. If you are unable to provide detailed information or follow the suggested outline, please provide a partial completion of this outline. We also would be glad to accept information by telephone or fax. Please call the Pollution Prevention Section at (614) 644-2971 or fax at (614) 644-2339. 1.0 HEADLINE The headline is a short phrase or description of the case study. 2.0 SIC OR ISIC CODE Use the four-digit Standard Industrial Classification (SIC) code(s) that best describe(s) the industry segment(s) referenced by the case study. 3.0 NAME AND LOCATION OF COMPANY Please identify the name and location of the facility that implemented the pollution prevention case study. 4.0 CLEAN TECHNOLOGY CATEGORY This section should include a brief description of the processes behind the pollution prevention activity referenced in the case study, such as: * Periodic assessments * Process/equipment modifications * Recycling, reuse and reclamation * Material/product substitutions * Training and supervision * Housekeeping * Production planning and sequencing * Waste segregation and separation 5.0 CASE STUDY SUMMARY This section should include a comprehensive description for the following areas: 5.1 Process and Waste Information: Describe the relevant original manufacturing process or area of the plant to which pollution prevention techniques apply, the physical state of the waste stream (solid, liquid, gas or sludge), the changes in the process resulting from the pollution prevention technique, and a description of any positive or negative effects on the wastes, products, or production rates after new technology implementation. This description should include any changes in: * Products or production rates resulting from the application * New or existing waste stream generation and composition * New or existing raw materials and consumption rates * Energy usage * Operating procedures 5.2 Scale of Operation: Describe the size of the process or operation. If possible, include quantitative information on the amount of product being produced or manufactured and the amount of waste being generated. 5.3 Stage of Development: Describe the stage of development the pollution prevention technique is (was) in at the time the case study was performed. Also, include whether the quantitative information provided is actual or estimated. 5.4 Level of Commercialization: Indicate whether the technology or process was commercially available at the time of the case study. Indicate whether or not the equipment and/or materials were readily available or if they were specially designed for the application. 6.0 ECONOMICS This section should include a summary of the costs and savings reported in the case study. 6.1 Investment Costs: Summarize all capital costs and provide a detailed description of the purchased items or services. Include specifications for each item (i.e., size, quantity used, capacity, etc.). 6.2 Operational and Maintenance Costs: Describe changes in the operational and maintenance costs (per month or year). Also describe changes in personnel or work hours required to implement the pollution prevention technology. 6.3 Payback Time: Describe the approximate payback period for the particular pollution prevention technology used in the case study (total investment/net savings per year). 7.0 CLEANER PRODUCTION BENEFITS This section should include a detailed discussion of the benefits resulting from the pollution prevention technique, including but not limited to: * Economic benefit * Improved public relations * Reduced liabilities * Changes in regulatory compliance 8.0 OBSTACLES, PROBLEMS AND/OR KNOWN CONSTRAINTS This section should include a description of the technical constraints that have or could prevent technology implementation (i.e., physical, chemical or biological limits of a manufacturing or treatment process); a description of any regulatory barriers in implementing the pollution prevention technology; and, a description of all other problems encountered during implementation not previously listed. 9.0 DATE CASE STUDY WAS PERFORMED This section should include the actual date the pollution prevention measures were initiated and the completion dates of any intermediate or final pollution prevention projects. 10.0 CONTACTS AND CITATIONS This section should include a description of the reference material used to implement the pollution prevention project(s). 10.1 Type of Source Material Identify the type of source material used. Examples include: * book or chapter * journal * organizational report * conference proceedings * unpublished material * other (specify) 11.0 KEYWORDS Ohio EPA can provide a list of keywords which may be used to identify and cross-reference case studies. Further detail on the above can be provided by Ohio EPA. If you have any questions or comments about these guidelines, please contact the Ohio EPA Pollution Prevention Section at (614) 644-3469. --------------------------------------------------- Appendix C Keywords Waste Type Codes 100 INORGANIC LIQUIDS 101 Aqueous waste with low toxic organics content 102 Spent mineral acid with dissolved heavy metals 103 Spent mineral acid without dissolved heavy metals 104 Acidic aqueous waste 105 Alkaline solution with metals but no cyanides 106 Alkaline solution with metals and cyanides 107 Alkaline solution cyanides but no metals 108 Spent caustic 109 Alkaline aqueous waste 110 Aqueous waste with dissolved sulfides 111 Aqueous waste with other reactives (e.g., explosives) 112 Other aqueous waste with high dissolved solids 113 Other aqueous waste with low dissolved solids 114 Scrubber water 115 Leachate 116 Waste liquid mercury 117 Other inorganic liquid 200 INORGANIC SLUDGES 201 Lime sludge without metals 202 Lime sludge with metals/metal hydroxide sludge 203 Wastewater treatment sludge with toxic organics 204 Other wastewater treatment sludge 205 Untreated plating sludge without cyanides 206 Untreated plating sludge with cyanides 207 Other sludge with cyanides 208 Sludge with reactive sulfides 209 Sludge with other reactives 210 Degreasing sludge with metal scale or filings 211 Air pollution control device sludge (B29)** 212 Sediment/lagoon dragout contaminated with organics (B30) 213 Sediment/lagoon dragout contaminated with inorganics only 214 Sediment/lagoon dragout contaminated with mixed inorg/org 215 Drilling mud (B32) 216 Asbestos slurry of sludge (B33) 217 Chloride or other brine sludge (B34) 218 Other inorganic sludge (B35) 300 INORGANIC SOLIDS 301 Soil contaminated with organics (B36) 302 Soil contaminated with inorganics only (B37) 303 Soil contaminated with organics and inorganics 304 Ash, slag or other residue from incineration of wastes (B38) 305 Other "dry" ash, slag or thermal residue (B39) 306 "Dry" lime or metal hydroxide solids chemically "fixed" (B40) 307 "Dry" lime or metal hydroxide solids not "fixed" (B41) 308 Metal scale, filings, or scrap (B42) 309 Empty or crushed metal drums or containers (B43) 310 Batteries or battery parts, casings, cores (B44) 311 Spent solid filters or adsorbents (B45) 312 Asbestos solids and debris (B46) 313 Metal-cyanide salts/chemicals (B47) 314 Cyanide salts/chemicals (B48) 315 Reactive sulfide salts/chemicals (B49) 316 Other reactive salts/chemicals (B50) 317 Other metal salts/chemicals (B51) 318 Other waste inorganic chemicals 319 Lab packs of old chemicals (B52) 320 Lab packs of debris only (B54) 321 Mixed lab packs (B55) 322 Spent carbon with adsorbed inorganics 323 Other inorganic soils (B56) 400 INORGANIC GASES 500 ORGANIC LIQUIDS 501 Concentrated solvent-water solution (B58) 502 Halogenated (e.g., chlorinated) solvents (B59) 503 Nonhalogenated solvent (B60) 504 Halogenated/nonhalogenated solvent mixture (B61) 505 Oil-water emulsion of mixture (B62) 506 Waste oil (B63) 507 Concentrated aqueous solution of other organics (B64) 508 Concentrated phenolics (B65) 509 Organic paint, ink, lacquer, or varnish (B66) 510 Adhesives of epoxies (B67) 511 Paint thinner or petroleum distillates (B68) 512 Reactive or polymerized organic liquid (B69) 513 Other organic liquid (B70) 600 ORGANIC SLUDGES 601 Still bottoms of halogenated (e.g., chlorinated) solvents 602 Still bottoms of nonhalogenated solvents or other organics 603 Oily sludge 604 Organic paint or ink sludge 605 Reactive or polymerized organics 606 Resins, tars, or tarry sludge 607 Biological treatment sludge 608 Sewage or other untreated biological sludge 609 Other organic sludge 700 ORGANIC SOLIDS 701 Halogenated pesticide solid 702 Nonhalogenated pesticide solid 703 Solid resins or polymerized organics 704 Spent carbon with adsorbed organics 705 Reactive organic solid 706 Empty fiber or plastic containers 707 Lab packs of old chemicals only 708 Lab packs of debris only 709 Mixed lab packs 710 Other halogenated organic solid 711 Other nonhalogenated organic solid 800 ORGANIC GASES Process or waste source codes 1000 MECHANICAL 1001 Aluminum polishing 1002 Automotive lubrication 1003 Automotive repairs 1004 Batteries, scrap treatment 1005 Bleaching 1006 Bending 1007 Boiler Maintenance 1008 Carpentry/woodworking 1009 Casting 1010 Cold rolling 1011 Cutting 1012 Deburring 1013 Decanting 1014 Degreasing 1015 Drilling 1016 Drip racks 1017 Dewatering 1018 Drums, storage, disposal 1019 Filtration 1020 Flow restriction 1021 Foundry casting 1022 Forming operations 1023 Grinding operations 1024 Injecting 1025 Lathing 1026 Leaks 1027 Lubrication, general 1028 Machining 1029 Maintenance 1030 Material feed operations 1031 Material handling 1032 Metal cleaning 1033 Metal forging 1034 Milling 1035 Molding 1036 Packaging 1037 Printing, vapor recovery 1038 Pulping 1039 Pumping 1040 Punching operations 1041 Recycling 1042 Rinse baths, spray, etc. 1043 Rinsing 1044 Shaping operations 1045 Spills 1046 Stockyard maintenance 1047 Surface cleaning 1048 Tank cleaning 1049 Water recycling 2000 PHYSICAL/CHEMICAL 2001 Absorption 2002 Acidification 2003 Acrylics 2004 Adsorption 2005 Anodizing 2006 Bleaching 2007 Brightdipping 2008 Cadmium plating 2009 Calcination 2010 Carbon adsorption 2011 Cartridges, drycleaning 2012 Cementation 2013 Centrifugation 2014 Chemical manufacturing 2015 Chemical processes, other 2016 Chemical synthesis 2017 Chrome 2018 Cleaning 2019 Cleanup control 2020 Coating 2021 Concentration 2022 Condensation 2023 Coolant, cutting oil recovery 2024 Cooling 2025 Copper, nickel plating 2026 Counter-current recovery 2027 Crystalization 2028 Cutting 2029 Cyanide treatment 2030 Degreasing 2031 Deinking 2032 Detergents 2033 Developing, photographic 2034 Dewatering 2035 Die casting 2036 Distillation 2037 Drag-out, bath 2038 Drag-out, recovery 2039 Dry cleaning 2040 Dyebaths 2041 Electrolysis 2042 Electrolysis, NOT plating 2043 Electrolytic recovery 2044 Electronic components, cleaning 2045 Electronic manufacturing 2046 Electroplating 2047 Electrostatic finishing 2048 Electrowinning 2049 Emulsification 2050 Emulsion breaking 2051 Etching 2052 Extraction 2053 Farm chemicals 2054 Farming 2055 Finishing 2056 Finishing textiles 2057 Flexographic printing 2058 Flotation 2059 Forging operations 2060 Forming operations 2061 Furniture finishing 2062 Gluing 2063 Gravure printing 2064 Hydraulic fluid recovery 2065 Hyperfiltration 2066 Inking 2067 Ion exchange 2068 Jewelry plating 2069 Laboratory 2070 Laminating 2071 Landfill leaching 2072 Laundry 2073 Liquid-liquid extraction 2074 Low liquid dye baths 2075 Lubrication, general 2076 Magnetic tapes 2077 Masonry 2078 Metal casting 2079 Metal cleaning 2080 Metal finishing 2081 Metal forging 2082 Metal forming 2083 Metal recovery from sludge 2084 Metal cleaning [ redundant entry with 2079! ] 2085 Metal plating 2086 Metal finishing [ redundant entry with 2080! ] 2087 Neutralization 2088 Non-toxic material substitution 2089 Oil recovery 2090 Organic chemicals formulation 2091 Oxidation 2092 Oxide coating 2093 Pad batch dyeing 2094 Paint spray cleanup 2095 Paint formulating 2096 Paint stripping 2097 Painting 2098 Paper manufacturing 2099 Pesticides formulation 2100 Petroleum refining 2101 Photo processing 2102 Photography 2103 Photographic film developing 2104 Photographic metals recovery 2105 Pickling steel 2106 Plastic containers 2107 Plastics manufacturing 2108 Polyethylene production 2109 Polymer film/coating 2110 Polymerization 2111 Precipitation 2112 Pressurization 2113 Printed circuit boards 2114 Printing 2115 Printing on polyethylene film 2116 Printing cleanup 2117 Process water treatment 2118 Reduction 2119 Resin absorption 2120 Reverse osmosis 2121 Rubber products 2122 Sedimentation/Settling 2123 Sizing recovery 2124 Smelting 2125 Staining 2126 Stripping 2127 Solvent adsorption 2128 Solvent stripping 2129 Specific ion adsorption 2130 Surface cleaning 2131 Supercritical fluid extraction 2132 Supercritical oxidation 2133 Tanning treatments 2134 Textiles manufacturing 2135 Ultrafiltration 2136 Vapor degreasing 2137 Wastewater treatment 2138 Water softening 2139 Welding operations 2140 Wet air oxidation 2141 Zinc plating 3000 BIOLOGICAL 3001 Aquaculture 3002 Bio-oxidation 3003 Dairy production 3004 Farming 3005 Fermentation 3006 Fish production 3007 Fruit production 3008 Meat production 3009 Poultry production 3010 Wastewater treatment 4000 THERMAL 4001 Drying 4002 Evaporation 4003 Freeze vaporization 4004 Heating 4005 Incineration 4006 Ovens, baking 4007 Pyrolysis 4008 Refrigeration 4009 Smelting 4010 Steel making 4011 Welding operations Waste Reduction Technique Codes 01 Equipment or technology modification 02 Process modification or substitution 03 Product reformulation or redesign 04 Process raw materials modification or substitution 05 Better housekeeping 06 Waste stream segregation 07 Onsite recycling or recovery for reuse 08 Offsite recycling or recovery for reuse (materials exchange) 09 Management strategies 10 Waste reduction audits 11 Wastewater reduction 12 General information on waste reduction Economic and Other Keyword Codes 1000 ECONOMIC EVALUATION 1001 Amortization 1002 Annual cost savings 1003 Capital costs 1004 Material value 1005 Payback period 1006 Return on investment 1007 Total cost accounting 1008 Treatment/disposal cost avoided 2000 TECHNOLOGY 2001 Implementation 3000 ENERGY VALUE * Source, United States Environmental Protection Agency, National Survey of Hazardous Waste Generators, November 1989. ** Waste codes with a (B##) designation are taken directly from US EPA's 1989 November National Survey of Hazardous Waste Generators Questionnaire Form GA
Last Updated: April 21, 1997