Improving on a Good Thing: Romo Reduces TRI
Releases
Romo Incorporated, a screen and digital printer in
De Pere, Wisconsin has been nationally recognized (see references
below) for its leadership efforts in adopting and sharing
environmentally preferable materials and work practices in screen
printing. A strong focus on environmental stewardship has led Romo’s
management to direct a series of progressive waste reduction
efforts. This case study provides an update on Romo’s most recent
progress in its quest for continuous environmental improvement.
Romo’s efforts show how continued and focused commitment to waste
reduction is needed to sustain and build upon early successes,
thereby providing maximum cost savings and emission reductions.
Like many screen printers, Romo has a diverse
repertoire of products, from small decals for original equipment
manufacture, through point-of-purchase displays, to fleet graphics.
The production equipment fits into a 41,000 square foot plant built
in 1992 and has allowed Romo to transact over $9 million in sales
for 1998.
Since its founding in 1953, the company has seen a
tightening of environmental regulations. In 1986, Romo made a
corporate commitment to stay ahead of the regulatory progression
through pollution prevention. Romo’s focus on source reduction of
emissions enabled the comany to meet regulatory requirements,
avoiding the negative risks associated with non-compliance such as
potential high fines. More importantly, it put Romo in the proactive
driver’s seat of change, charting its own course with adequate
investigation, preparation, and travel time. Romo chose to focus on
pollution prevention because the company believes that it best
enables the company to fulfill its responsibility to provide both
its employees and its community with a safe environment.
The Search
Begins
Romo decided to focus its initial efforts on the
screen washout area, a primary source of air emissions and hazardous
wastes for most screen printers. Screen wash solvent was being
sprayed on dirty screens, collected in an open tank, filtered, and
reapplied. This process was using 20 to 40 gallons of virgin solvent
per day. The filtering method did not sufficiently remove the
suspended solids from the solvents. Selected improvements included
covering the tank and adding a distillation system. For a cost of
$2,900, these improvements cut solvent use more than 90%. Further
reductions were made when the solvent delivery hose was equipped
with an adjustable spray nozzle, similar to those used on garden
hoses. Brushing the screen with solvent before the wash, and
limiting the flow from the nozzle with a block of wood under the
handle to prevent its full travel, further reduced the amount of
screen wash used on each screen.
These two process changes reduced Romo’s toluene
and methyl isobutyl ketone (MIBK) emissions by 39%, from 30,400 to
18,480 lbs, between 1988 and 1991.
Next Steps
Having experienced the success of its initial
efforts, in 1992 Romo joined the EPA’s 33/50 program. In doing so,
the company voluntarily set goals of reducing emissions from their
1991 levels by 33% in one year and by 50% at the end of the fourth
year, 1995. A three-pronged approach was planned to meet these
goals, including:
- reduce the volume of all chemicals used;
- seek alternative application techniques; and
- improve selection of materials used.
Employee input was solicited from all levels and
feasible projects were chosen for each area of the production
process. To qualify for adoption, any change had to reduce chemical
exposure risks to employees, reduce pollution, and to be compatible
with the other tasks in the production process.
After review of suggested improvements, Romo
decided to focus on improving the emulsion removal task and changing
the press wash. Emulsion removal was by the installation of a
high-pressure washer. The washer improved cleaning effectiveness
while reducing usage of water and emulsion remover. In fact, the
emulsion remover concentration was halved while still producing the
same cleaning effect. Work processes were also modified to improve
an initial application of full-strength emulsion remover.
Previously, this had been applied by manual brush and resulted in
excess application that dripped onto the cleaning room floor. The
new process uses a controlled spray, which uniformly applies a
thinner coat of emulsion remover, reducing dripping and waste.
Together, these improvements reduced emulsion remover purchases by
75%.
A new press wash recommended by other screen
printers was chosen. It cleaned with propylene glycol monomethyl
ether, propylene glycol monomethyl ether acetate, and cyclohexanone
rather than toluene or MIBK. At the end of 1992, less than one year
into the 33/50 program, the toluene and MIBK releases had been
reduced by more than 70% to a combined 5,390 lbs. Romo had surpassed
not only the first year’s goal, but made such great strides that the
four-year goal was eclipsed. More details of Romo’s participation in
the 33/50 program are available in the DfE screen printing case
study: Reducing the Use of Reclamation Chemicals in Screen
Printing.
Further
Improvements
Buoyed by their success in the 33/50 program, Romo
swam into the deeper waters of pollution prevention in 1996. Because
of their commitment to continuous environmental improvement, Romo’s
managers decided upon a proactive goal, to eliminate the use of all
chemicals listed in the USEPA’s Toxics Release Inventory (TRI). In
order to implement the goal, they looked for further emission
reductions with new screen cleaning products. A "Solvent Team" was
formed consisting of employees who use the screen cleaning solvents.
Romo’s solvent vendor was able to supply some alternative products
and different samples were provided by other suppliers. Alternative
products were tested under production conditions. Data were gathered
to document the amounts used, any recommended changes in production
procedures, and how easy the products were to use.
After several months of testing, Romo’s Solvent
Team chose to adopt new products for its press wash, screen wash,
and emulsion remover. The active ingredient in the press wash is
isobutyl isobuterate, and the screen wash relies on propylene glycol
ethers and other nonhazardous proprietary chemicals. The chosen
replacements do not contain toluene, MIBK, or any other TRI-listed
chemicals.
Impacts
Savings
Table 1 shows the change in chemical use before and
after the 1996 switch. Unit costs of the replacement press and
screen washes, designated in Table 1 as ‘post-96', are higher than
their ‘pre-96' counterparts. However, the volumes used are
substantially reduced, resulting in a net savings of $3,170 per
year, a reduction of 12.6%.
Approximately one quarter of the 1995 press wash
use has continued in 1998. The post-96 press wash has not been able
to clean some of the difficult jobs as well as the pre-96 press
wash, especially when printing halftone images. Hazardous waste
disposal and labor costs did not change significantly.
Table 1. Effects of 1996 Changes on Solvent Use and
Costs
|
Amount Used
(gal/yr) |
Unit Cost
($/gal) |
Total Yearly
Material Cost |
Materials and Costs before 1996 Improvements |
Pre-96 Press Wash |
2530 |
$3.26 |
$8,248 |
|
Pre-96 Screen Wash |
1265 |
$13.30 |
$16,825 |
1995 total |
|
$25,072 |
Materials and Costs after 1996 Improvements |
Post-96 Press Wash |
1045 |
$13.30 |
$13,899 |
|
Post-96 Screen Wash |
385 |
$15.20 |
$5,852 |
Pre-96 Press Wash |
660 |
$3.26 |
$2,152 |
1998 total |
|
$21,902 |
Annual Savings |
$3,170 |
A new emulsion remover is an integral part of the
screen cleaning process. The combination of new press and screen
washes and emulsion remover cleans so much better than the previous
chemicals that the need for an optional final step in screen
cleaning, secondary haze removal, has been reduced. Only 5% of the
screens used in 1997 required haze removal, down from 33% of all
screens in 1988. Two areas of savings result from this change.
First, fewer gallons of haze removing chemicals are purchased.
Second, since the screens’ exposure to the caustic haze remover is
reduced, the screens are replaced less frequently. Spent haze
remover is captured in a drain trap which requires infrequent
cleaning and disposal, the costs of which are minimal and have not
changed appreciably.
Emission Reduction
Impressive waste reduction has been attained by
Romo in this round of changes. Table 2 depicts a total reduction in
TRI chemical emissions of 64% between 1995 and 1998. Some rebound in
emissions has occurred between 1996 and 1998. A portion of this can
be explained by Romo’s fast growth, especially in areas which
require use of the pre-96 cleaning system.
Table 2. TRI Releases at Romo
|
Toluene (lb) |
MIBK (lb) |
Total TRI Releases
(lb) |
Change in Total TRI Releases (%) |
Change in Company Sales Revenue
(%, unadjusted for inflation) |
1995 |
9,106 |
3,984 |
13,090 |
|
1996 |
2,101 |
919 |
3,020 |
1998 |
3,749 |
937 |
4,686 |
Change
1998-1995 |
-5,357 |
-3,047 |
-8,404 |
-64% |
70% |
Future Plans
Romo plans to continue its progress toward
increased environmental stewardship with more basic changes in its
printing materials. Currently the only product used that releases a
TRI-listed chemical is the pre-96 press wash. This solvent is only
used to clean solvent-based inks. As part of its ‘zero TRI
reportable’ goal, Romo has been working to reduce its use of
solvent-based inks, replacing them with UV-cured inks. In the midst
of the changes described here, UV ink use continued to increase from
40% of Romo’s total ink volume in 1995 to 60% in 1998. Individual
product lines are converted to UV ink through the expertise of
Romo’s research and development team. More progress is planned for
the future. Based upon their success with UV inks, Romo is committed
to completely phase out solvent-based inks, expecting to reach its
goal of eliminating all TRI releases by 2003.
References
Details of Romo’s participation in the 33/50 program are
available in the DfE screen printing case study: Reducing the
Use of Reclamation Chemicals in Screen Printing, EPA
744-F-93-015, available from the Pollution Prevention Information
Clearinghouse, 202-260-1023, or www.epa.gov/opptintr/dfe/screenprinting/case_studies/case1/!project.pdf
Romo was awarded an 1997 Environmental Champion award by USEPA
and Chemical Engineering Magazine. A description can be found at
http://www.che.com/
A video case study describing Romo’s recent pollution
prevention activities is contained in Using Screen Printing
Technologies for Business and Environmental Success. A
videotape with written description is available from PNEAC.
Romo’s Quality Manager, Jon Weber, can be reached at
920-336-5100, jweber@romoinc.com.
The Screenprinting and Graphic Imaging Association offers
technical assistance to screenprinters. Visit SGIA’s web site at
http://www.sgia.org/ or contact
Marci Kinter at 703-385-1335 or marcik@sgia.org.
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