Cleaner Production Demonstration Project at Schweppes Cottee's
EXECUTIVE SUMMARY
1.0 REVIEW OF SCHWEPPES COTTEE'S OPERATIONS
2.0 PLANNING AND ORGANISATION OF THE SCHWEPPES COTTEE'S CLEANER PRODUCTION PROJECT
2.1 CLEANER PRODUCTION APPROACH USED AT SCHWEPPES COTTEE'S
2.2 CLEANER PRODUCTION OPPORTUNITIES AT SCHWEPPES COTTEE'S
2.2.1 Minimisation of Water Usage and Wastewater
2.2.2 Minimisation of Energy Use
2.2.3 BOD5 and Oil and Grease Reduction3.0 CLEANER PRODUCTION INITIATIVES
6.0 SCHWEPPES COTTEE'S PERSPECTIVE
3.1 MINIMISATION OF WATER USAGE
3.1.1 Detailed Evaluation of Opportunity
3.1.2 Project Implementation
3.1.3 Results
3.2 MINIMISATION OF ENERGY USE
3.2.1 Detailed Evaluation of Opportunity
3.2.2 Project Implementation
3.2.3 Results
3.3 BOD5 AND OIL AND GREASE REDUCTION
3.3.1 Detailed Evaluation of Opportunity
3.3.2 Project Implementation
3.3.3 Results
LIST OF TABLES TABLE 1 RESULTS OF INSTALLING WATER SAVING NOZZLES ON CONTAINER WASH SYSTEMS
LIST OF FIGURES FIGURE 1a TYPICAL CONTAINER WASH SYSTEMS ON THE CORDIAL LINES
FIGURE 1b IMPROVED CONTAINER WASH SYSTEM
FIGURE 2 OIL AND GREASE CONCENTRATIONS IN WASTEWATER
The Cleaner Production Demonstration Project is
an initiative of the Environment Australia - Environment Protection
Group (EPG). The aim of the Project was to raise the awareness
of Australian industry and actively promote cleaner production
issues. This was to be achieved by conducting ten successful
cleaner production demonstration projects in industry around Australia,
documenting the benefits and experiences of the project, and publicising
the results to wider industry. Dames & Moore, assisted by
Energetics, were engaged as technical consultants on the project.
The project commenced in June 1994, and ran for 27 months.
Schweppes Cottee's in Liverpool, NSW, were selected
as one of the ten companies to participate in the project. This
case study report presents a record of the progress of the Schweppes
Cottee's project, from initial meeting to project completion,
and detail the results of the project and any problems which may
have been encountered. This case study demonstrates the application
of cleaner production to the food industry.
The Schweppes Cottee's facility in Liverpool is
a medium-sized manufacturing plant which produces cordial, jam,
jelly, ice cream toppings, fruit snacks and coffee. The main
basic raw ingredients used in production are sugar, fruit, food
additives and water, which are processed on a number of production
lines.
The manufacturing process typically involves the following steps:
Completion of the Schweppes Cottee's project comprised
a number of stages, as follows:
Many specific cleaner production opportunities
were identified at the site, which are summarised in Table 1.
Following a relatively long period of investigation and discussion,
five projects were selected for implementation. These projects
focused on water minimisation, energy conservation, and improvement
of wastewater quality, and are summarised below.
Improvements to the line-lube (conveyor lubrication
and sanitisation) system were made by Schweppes Cottee's independently
to the Demonstration Project, with the objectives of decreasing
line-lube and water usage and reducing oil and grease concentrations
in the wastewater discharged from the site. The improvements were
made by line-lube supply company, at no cost to Schweppes Cottee's,
and involved regulating flows and improving controls. The benefits
of the line-lube project are documented in this report.
Schweppes Cottee's allocated the responsibility for implementing the projects to one of their site engineers. There was limited involvement by site management. While the projects were successful, progress was slower than anticipated. The benefits of the project could have been more widespread had management been more involved in the process, and more personnel been made available to work on the project. There appears to be some commitment from plant management to continue investigating and implementing other opportunities for cleaner production which were identified at the outset of the project.
Installing trigger nozzles on hoses | Reducing water usage and wastewater volumes. Inexpensive to install. | Theft of nozzles was considered to be likely. | Nozzles not installed
| ||
Line lube system improvements | Collecting and recycling line lube | Reducing line lube usage. Improving wastewater quality. Reducing water usage. | Recycled line lube would require filtering and re-dosing, and involve a complicated collection system. Potentially expensive. | Line lube not recycled.
| |
Improved control of line lube application system | Reducing line lube usage. Improving wastewater quality. Reducing water usage. Could be installed at the expense of line lube suppliers | Improved system remains the property of the line lube supplier. | Improvements were implemented
| ||
Utilising sand filter backwash | "Backwash" water produced during cleaning of the water filters could be recycled and used in other areas of the plant | Reducing water usage and wastewater volumes. Some infrastructure already available onsite. | Estimated cost of $2,500 | Project was implemented
| |
Jam Capping Machine improvements | Install collection and recycling systems on the jam capping machines, gripper rinser, and bottle washer. | Reducing water consumption and wastewater volumes. | Complicated and potentially expensive. Throttle valves could be installed on the jam capping machines as an alternative. | System not installed. Throttle valves to be installed in the future.
| |
Jam cooler improvements | Modify Jam Cooler to resemble the more efficient Fruitsnacks Cooler. | Reduce water consumption and wastewater volumes. | Expensive and difficult to engineer. | Improvements not made.
| |
Improving Container Wash systems | Recycling wash water, installing water-saving nozzles, and improving control system. | Reduce water consumption and wastewater volumes. | Cost approximately $2,000 for each production line. | Water saving nozzles installed on each line. Wash water recycled on one line, with the system to be extended to other lines in the future. Improved control system to be installed in the future.
| |
Hot Water Maker | Improving control of steam to the hot water maker | Reduce energy consumption. | None | Project was implemented.
| |
Steam Traps and Steam Isolation Valves | Maintenance program | Reduce energy consumption | No integrated steam system at the site, with limited information on steam piping routes. Project potentially complicated and time consuming. | Not implemented in the time-frame of the Project. Will be implemented in the near future.
| |
Compressed air on Cap Dryers | Using an alternative method to compressed air to dry bottle caps. | Reduce energy consumption | Capital costs associated with installing blowers and jets. | Not implemented in the time-frame of the Project. Will be implemented in the near future.
| |
Revised Energy Management structure | Install metering equipment to track energy usage, make plant managers accountable for energy used on each line. | Possible 15% saving in energy. | Complicated steam, electricity and compressed air supply systems at the plant, requiring significant time and cost to redirect lines and install metering equipment | Not implemented in the time-frame of the Project. Will be implemented in the near future.
| |
Collect and recycle spilt cordial | Collect cordial spilt at the filler, and recycle for reuse. | Reduce product wastage and BOD concentrations in wastewater. | Line-lube contacts bottles before they are filled, and therefore may contaminate spilt cordial, making it unsuitable for reuse. It was not possible to eliminate line-lube from areas upstream of the filler. | This project did not proceed.
|
Schweppes
Cottee's, a division of Cadbury Schweppes Pty. Ltd., manufactures
a number of products including cordial, jam, jelly, ice cream
toppings, fruit snacks and coffee at its plant in Liverpool, NSW.
The main basic raw ingredients used in production are sugar,
fruit, food additives and water, which are processed on a number
of production lines.
The manufacturing process typically involves the following steps:
The production lines are as follows:
Jam Production: | J1 | Jam |
J2 | Hot fill juices and beverages | |
Cordial Production: | C1 | Cordials |
C2 | Bulk jam | |
C3 | Cordial jug line | |
C4 | Topping | |
C5 | Jam and topping | |
Dry Mix: | Fruit Snacks | |
5 Coffee production / packaging lines | ||
4 Jelly packaging machines | ||
1 Saline line |
An ancillary feature of the site is the blow-moulding plant, where
six different types of plastic bottles are manufactured on 8 moulding
machines.
At the outset of this project, approximately 161 million litres
of water was used at the site per year, the majority of which
is used for washing bottles and jars. Water is also used for
washing down equipment and floors, sterilising equipment, and
in-line washing of cooking and mixing vessels (CIP or Clean-In-Place).
High quality water is required as any grit present could damage
equipment. Water is therefore passed through sand filters to
remove fine particles prior to use. Approximately 10 % of the
water used at the plant is used in products. Approximately 80%
of the water consumed at the site is discharged as wastewater,
with the remainder used in the cooling towers and evaporated to
atmosphere.
Services supplied to the site include steam, from two gas fired
boilers, refrigeration, cooling water and compressed air.
The production workforce at Schweppes Cottee's is seasonal. In
July, 1996 (low season) 125 people were employed at the site on
the production lines. 21 people are plant supervisors / managers,
14 are engineers, technical support and QA personnel, 27 are tradespeople,
25 work in distribution (forklift drivers and supervisors), along
with a small office / support workforce.
Plant supervisors and managers are primarily responsible for production.
Environmental aspects associated with the line, such as energy
and water usage and waste production, are not main features of
their responsibilities.
Total Quality Management (TQM) teams comprising management and
production personnel meet regularly to discuss and address issues
such as water minimisation.
2.0 PLANNING AND ORGANISATION OF THE
SCHWEPPES COTTEE'S CLEANER PRODUCTION PROJECT
2.1 CLEANER PRODUCTION APPROACH USED
AT SCHWEPPES COTTEE'S
At the outset of the project, during the application and assessment
stages, Schweppes Cottee's demonstrated commitment for this project,
having already identified water and wastewater as the areas in
which cleaner production efforts could be concentrated.
A structured approach was used in the identification and implementation of Cleaner Production to Schweppes Cottee's. The approach was as follows:
Schweppes Cottee's personnel involved in the Cleaner Production Project were:
Kevin Jeffress, Operations Manager: | Involved in initial discussions to identify opportunities for cleaner production at the site, and approved and allocated finances necessary for the implementation of the selected projects. |
David Fox, Engineering Manager: | Responsible for the day-to-day running of the project. David was actively involved in identifying cleaner production opportunities, conducting any monitoring necessary, and implementing the selected projects. |
Warren Pulling, Process Control Manager: | Provided technical support for selected aspects of the project, mostly in the area of monitoring. |
From the outset, and throughout the course of the project, it
was envisaged that Schweppes Cottee's were to be responsible for
the day-to-day running of the project. Dames & Moore and
Energetics acted as catalysts for ideas, responsible for
providing technical back-up as required, and documenting the results
of the project.
2.2 CLEANER PRODUCTION OPPORTUNITIES
AT SCHWEPPES COTTEE'S
The specific cleaner production opportunities were identified
by the consultant, Dames & Moore, during the initial site
audit and in following visits. The opportunities were in three
key areas:
These are discussed in more detail below.
2.2.1 Minimisation of Water Usage
and Wastewater
The water consumption at this site at the outset of the project
was 161 ML per year, and effluent discharges averaged about 600
kL per day. This is a significant contributor to the overall
cost of the operations and the site Total Quality Management (TQM)
team had identified water usage and waste water minimisation as
an important area that deserved review. The cost of supply of
water and disposal of wastewater was calculated at $2/kL of water.
One of the major areas where water is used is in product container
washing. This is typically required because of slight spillage
of product over the outside of the container which will result
in the container itself becoming sticky. Research has shown that
sticky containers have a detrimental effect on the sales of product
as when shoppers pick up a sticky container, they almost invariably
replace it and try another, often from one of the opposition manufacturers.
While this water requirement is vital, an area for cleaner production
opportunities was in the overall water consumption.
Ideas for the minimisation of water usage at the plant were as
follows:
General
Jam Lines
-Cleaning the screens in the cooler;
-Installing spray nozzles in the cooler to replace the current perforated plate system, to give more efficient cooling and reduce the water demand; and
-Water used at the end of the cooler appeared to be by-passing
the jars, and was therefore not used for cooling. To prevent
water flowing through this section of the cooler, the final pump
could be switched off, or perforations in the last section of
the cooler could be blocked off.
Fruit Snacks, and Cordial and Topping Plants
In each of these areas, containers are washed after they are filled,
to eliminate any sticky residue on the outside of the container.
In many of these areas, the washing system comprised one or two
washes, with wash water discharged to the drain. Often, the container
wash system continued to operate when containers were not on the
conveyor, or when the conveyor was not running, resulting in wasted
water. Possible improvements in these systems included:
The potential for savings in this area were expected to be excellent
and some of the issues dealt with in this area are closely aligned
with some of the housekeeping and operating practices.
Potential projects to minimise water usage were selected for further
investigations as follows:
2.2.2 Minimisation of Energy Use
Schweppes Cottees uses approxiamately 9.5 million kilowatt hours
and 73, 200 m3 of gas each year. Ideas for the minimisation
of energy usage at the plant were as follows:
Any reduction in steam usage not only results in a cost saving
benefit for the company, but could also reduce the CO2
emissions resulting from the burning of fossil fuels used to generate
steam.
The following potential projects were identified for further investigation:
2.2.3 BOD5 and Oil and
Grease Reduction
Ideas for the reduction of BOD5 concentrations in trade
waste are as follows:
The principal idea for the reduction of oil and grease concentrations
in trade waste was as follows:
Specific projects identified for further investigation were:
3.0 CLEANER PRODUCTION INITIATIVES
3.1 MINIMISATION OF WATER USAGE
3.1.1 Detailed Evaluation of Opportunity
Installation of Trigger Nozzles
Benefits : | Saving water, reducing wastewater volume, minimal installation cost. |
Drawbacks: | Management has tried this approach before, with the experience that most of the nozzles were stolen, and felt that this problem would recur |
Outcome: | Trigger nozzles were not installed. |
Collecting and Recycling Line Lube/Controlling Line Lube Sprays
Benefits : | Approximately $45,000 is spent annually on 13 kL litres of line lube. Collecting and recycling line lube would reduce costs, wastewater volumes and water usage. Line lube has high concentrations of oil and grease. By reducing the amount of line lube used, concentrations of oil and grease in the wastewater would be reduced |
Drawbacks: | During the timeframe of the Project, independent changes were being made to one of the jam lines, the changes included re-organisation and improvements in the line lube system on this line. Controlling line lube to co-ordinate with conveyor movement was seen to be a relatively complicated project. Management preferred to wait until the new system was installed, determine whether any lessons could be learnt from this system, and apply any improvements to the rest of the lines at a later stage. Discussions with line-lube suppliers and other manufacturers revealed that the collection and recycling of line lube may not be feasible, as the recycled line lube would have to be filtered and re-dosed prior to reuse. |
Utilising Sand Filter Backwash Water
Benefits : | The volume of water used to backwash sand filters (which is currently disposed to sewer) is approximately 5,700 kL/year or approximately 3.5% of total water usage. This water is clean, containing very low concentrations of suspended solids and could be used for a variety of non-product uses. Opportunities for re-use included: cooling tower make-up water; boiler feed water; and line lube water. Water demands in these areas were monitored or estimated (where monitoring was not possible) as: | ||
Cooling Tower 1 Cooling Tower 2 Cooling Tower 5 Cooling Tower 6 Cooling Tower 7 Fruit Snacks Cooling Tower Boiler Feed Water Jam Plant Line Lube | 2,048 kL/year 2,093 kL/year 786 kL/year 2,385 kL/year 539 kL/year 700 kL/year 11,947 kL/year 2,500 kL/year | ||
The benefits of collecting and reusing the filter backwash water were seen as: | |||
- reduction in water usage; and | |||
- reduction in wastewater volumes. | |||
Drawbacks: | The collection and re-use of water involved initial flow measurements, and subsequent installation of piping and pumps. Collection tanks were available onsite. The costs to conduct flow measurements and install the recycling system were estimated at $2,500 | ||
Outcome: | It was decided to proceed with this project. The results of the project are discussed in later sections of this report. |
Prevent overflow of water from the jam capping machine.
Clean water was overflowing from the jam capping machine directly to site drains. While investigating potential uses for this water, other areas where clean water is wasted, were identified, namely:
The volumes of water wasted in each of these areas were measured
or estimated as:
Jam Line Cappers | 5,200 kL/year |
Gripper Rinser | 7,340 kL/year |
Bottle Washer | 2,000 kL/year |
This represents approximately 9% of sites total annual water usage.
As for the sand backwash water, there were opportunities to reuse this water as:
An alternative to recycling the water, optimising the amount of
water by putting a control valve in the line, was also considered.
Benefits : | The benefits of collecting and reusing this water are reduction in water usage and waste water volumes (total of 14,540 kL / year). |
Drawbacks: | It was considered that installation of the complicated piping required to access the capping machines, gripper rinser and bottle washer was not the most feasible method of reducing water consumption in these areas. |
Outcome: | It was decided that the collection and recycling system was not feasible at this stage. In order to reduce water wasted at the capping machines, the installation of throttle valves was proposed to control the rate of water flow. It was proposed that these valves be installed, at an estimated cost of $300. |
Jam Cooler Improvements
The water level high-control system at the J1 jam cooler appeared
to be working effectively. However, the recycling pumps in the
cooler were found to be "cavitating" due to a lack of
sufficient water, and throwing water out of the top of the cooler.
It was initially thought that the screens controlling water flow
may have been blocked, preventing water flow and thereby causing
pump cavitation. The screens were removed but cavitation continued.
The cause of the overflow was not determined.
Further possible jam cooler improvements were assessed qualitatively
by comparing aspects of the cooler with the fruitsnacks cooler,
which appeared to be operating with less waste of water. Further
investigation revealed that water was fed to the Fruitsnacks cooler
through an open-ended U-shaped pipe, which allowed water to enter
the system at 2 points, and thus made more efficient use of the
water available. Water is fed to the J1 jam cooler though one
outlet only. While the J1 system could have been altered to more
closely resemble the Fruitsnacks configuration, all fittings on
the J1 cooler are (and must be) made of stainless steel, which
is expensive to modify and difficult to weld.
Benefits : | It was difficult to measure the amount of water being wasted at the jam cooler, as overflows were periodic, and inefficiencies were difficult to quantify. |
Drawbacks: | It was decided that any saving resulting from improvement of the jam cooler would be small when compared to some of the other cleaner production opportunities. It was considered that there would be some implementation difficulties with any specific initiatives |
Outcome: | This project was not proceeded with as part of the cleaner production demonstration project, but may be followed up by Schweppes Cottee's at a later stage. |
Improving Container Wash Systems
Container wash systems in the fruit snacks, cordial and topping
plants waste significant quantities of water.
Fruit Snacks Container Wash
Clean water was being fed to the fruit snacks container wash system
at a rate of approximately 40 L per minute, which equates to a
water usage of 3,500 kL/year, which was eventually discharged
to sewer. Water was fed to the container wash system through
a series of 6 nozzles, which were similar to domestic "water-saving"
shower nozzles. The use of more water-efficient nozzles had the
potential to significantly reduce water usage. It was decided
to install alternative nozzles which deliver a flat spray, the
benefits of which are detailed in Section 3.3.1. These nozzles
were also to be installed in other sections of the various production
lines. Nozzles cost approximately $25 each plus plumbers' fees.
Cordial Line Container Wash Systems
There were three opportunities for reducing water being used and wasted in these systems.
Topping Plant Wash Tunnel (C4)
The amount of mains water being used in this wash system was measured
as 53 L/min, which equates to approximately 4,900 kL/year. This
is heated to increase the cleaning efficiency. At present, there
is little control over the water used in the wash tunnel. While
water saver nozzles are used in the wash tunnel, a recycling system
for the wash water, such as that used on the C1 line, could be
implemented.
Benefits : | Container Wash water consists of a approximately 8% of the total quantity of the total amount of water used on the site. The identified projects would decrease water usage and discharges to sewer. The recycling of Topping Line Wash Tunnel would also decrease energy usage. |
Drawbacks: | The optimising of the existing wash systems and the improved system control would require significant time from the main engineering manager on the site. New nozzles cost approximately $25 plus installation fees. Costs for the installation of the recycling wash water system on other cordial lines were estimated at $1,500. |
Outcome: | The Fruit Snacks Container Wash was implemented at an early stage and not directly as a result of this project. Projects (1) and (2) on the Cordial Lines Container Wash Systems were selected for implementation, with implementation of project (3) at a later stage. The optimising of the Topping Plant Wash Tunnel was to be investigated following further trials on the C1 wash tunnel. |
The cleaner production projects selected for implementation at the Schweppes Cottee's site were:
3.1.2 Project Implementation
Utilising Sand Filter Backwash Water
The sand filter backwash water is collected in a tank, and pumped
to Cooling Towers 1 and 2 to be used instead of mains water.
The filter backwash water is pumped to a main collection tank
adjacent to the cooling towers by a pump which is pressure-activated.
Water is gravity fed from the tank to the cooling towers. Level
control in the cooling towers activates valves which open to allow
water to fill to the desired level in the towers. Mains water
is provided as a backup, should the filter backwash system fail
for some reason.
Equipment required included:
The equipment was installed by contract plumbers in June 1996,
and is to commence operation in July 1996. Capital and installation
costs associated with implementation of the project were $3,500.
Installing Throttle Valves On The Jam Line Capping Machine
The throttle valves were not installed during the course of the
project, however these will be installed at a later date.
Container Wash Nozzles
Water saving nozzles of the flat spraying variety were installed
by contract plumbers in the various wash systems as indicated
below:
Note:
Recycling Wash Water On The Cordial Line
The recycling system on C1 line collects water from
the final rinse, and uses it as "first-wash" water.
The system comprises a collection tank with level control, piping,
a pump, and a flowmeter which measures the amount of mains water
used in the wash system. The system was installed in 1994 by
site fitters and contract plumbers. Purchase and installation
of the equipment cost $1,500.
This system was to be used as a model, and installed
on other container wash systems, however was not extended to other
wash systems in the course of this project.
3.1.3 Results
Utilising Sand Filter Backwash Water
Total volume of water saved by implementing system | |
Unit cost for supply and disposal of water | |
Cost savings associated with water savings | |
Cost of purchasing and installing equipment | |
Payback period |
Container Wash Nozzles
The results of installing water-saving nozzles on the container
wash systems are summarised in Table 1. In summary:
Total volume of water saved by implementing system | |
Unit cost for supply and disposal of water | |
Cost savings associated with water savings | |
Cost of purchasing and installing equipment | |
Payback period |
Recycling Wash Water On The Cordial Line
The amount of mains water being used in the container wash system
on the cordial line was not monitored prior to the installation
of the recycling system. We estimate that the recycling system
halved the consumption of mains water. Following installation
of the system, the usage of mains water was monitored (by the
flowmeter) and found to be around 37 L/min, which equates to an
annual figure of 2,650 kL. The estimated savings associated with
the recycling system are:
Estimated water saving following installation of the recycling system | |
Unit cost for supply and disposal of water | |
Cost saving associated with water saving | |
Cost of supplying and installing equipment | |
Payback Period |
This demonstrates that significant savings are possible by recycling
wash water in other areas of the plant.
SUMMARY OF RESULTS OF WATER SAVING INITIATIVES
Schweppes Cotteeís will save over 14. 7 million litres
of water and $29, 560 each year as a result of their water savings
initiatives. The total cost of installing the water saving equipment
was $8390.
Amount of water consumed prior to installation of the nozzles (kL/year) | |||||
Amount of water consumed following installation of nozzles (kL/year) | |||||
Water savings (kL/year) | |||||
Unit cost for supply and disposal of water ($/kL) | |||||
Cost savings associated with water savings ($) | |||||
Cost of purchasing and installing nozzles ($) | |||||
Payback period (weeks) |
General
The consumption of mains water at the site is measured via a single flowmetre. Daily readings are taken, and summarised into a report which indicates the water usage for each 4 week period. To indicate the benefits of the cleaner production initiatives at the site in general terms, the production and water consumption figures for the first 20 weeks in 1995 and 1996 have been compared:
Production (in kgs and litres of product) | ||
Water consumption (kL) |
This information indicates that while production in 1996 was approximately
4% less than in 1995, water consumption was 13% less in 1996 than
it was in 1995. This water saving would translate to a roughly
equivalent reduction in wastewater being discharged from the site.
3.2 MINIMISATION OF ENERGY USE
3.2.1 Detailed Evaluation of Opportunity
Hot Water Maker
Steam provided to heat the hot water tank was found to be controlled
by a pneumatic control valve. The control valve is regulated
via an input to pressure (I to P) converter, which receives signals
from the thermocouple inside the tank and delivers a varying air
pressure to the control valve to increase or decrease the steam
rate as required. Water was found to be present in the compressed
air at the site, a problem which is fairly common across industry,
and was damaging the I to P converter.
The solution to this problem is to replace the control mechanism
with a mechanically controlled steam valve, eliminating the need
for compressed air in the control system.
Benefits : | By addressing this problem, the hot water temperature can be controlled more accurately, preventing the wastage of steam and energy. The economic benefits are difficult to quantify as the hot water heater is a small part of a complicated steam network, and it is not possible to directly measure the steam being wasted |
Drawbacks: | There were no perceived drawbacks from this project. |
Outcome: | This project was therefore implemented. |
Steam Traps and Steam Isolation Valves
The Schweppes Cottee's site has close to 100 steam traps, within
the numerous plants on site. Based on experience from other plants
it could be expected that 5-10 % of these steam traps would be
not working or not working effectively. This would lead to wasted
steam and higher output of the boiler. At the Schweppes Cottee's
plant there appeared to be live steam returning with the condensate,
suggesting that some, or many of the steam traps were not working
effectively.
Two initiatives were considered to address this problem. The
first involved the implementing of a planned inspection and maintenance
procedure for the steam traps on the site so as to ensure that
the steam traps were operating as required. The second involved
putting steam and condensate isolation valves in the steam system
such that individual plant areas could be isolated so that any
energy losses from the steam system for individual plants would
not occur when the individual plant was not operating and so as
to allow easier maintenance of steam traps within the plants.
Benefits : | If 5 - 10% steam traps are not working effectively this could represent a significant energy loss. Other organisations who have implemented a steam system as outlined above receive significant energy savings. This leads to lower energy costs, with the environmental benefits of decrease greenhouse gas emissions, reduced NOx emissions and reduced resource usage. |
Drawbacks: | The present steam system has been the result of numerous additions to the site over many years. No integrated steam system presently exists and only limited information is available on steam piping routes and takeoffs. A reasonable amount of time and cost would be required to identify all steam pipelines and traps and some work and costs would be associated with the redirecting of steam lines in some areas and the installation of isolation valves to allow for the isolation of the steam system to individual plants. |
Outcome: | As there was a significant amount of work to be done for this initiative, the project did not go ahead within the timeframe of the Project. Schweppes Cottee's plan to proceed with the initiative in the near future. |
Alternative to Compressed Air on Cap-Dryers
Air is used to dry bottles and jars prior to labelling and ink
marking. At about 36 places compressed air is used for this purpose.
The air is directed onto the bottles by air knife or by squashing
the end of copper tubing and using this as a nozzle. The use
of compressed air for this purpose is an inefficient use of energy
used to compress the air.
The initiative proposed was to replace areas where compressed
air is used by a fan and a dedicated air knife.
Benefits : | The proposed system would result in a decrease in energy usage associated with the compressed air. The cost benefit associated with this is difficult to determine. |
Drawbacks: | The proposed initiative would require capital costs associated with the provision of blowers and associated air knife jets. In some cases new electrical connections would also be required. |
Outcome: | As there was a significant amount of work to be done for this initiative, the project did not go ahead within the timeframe of the Project. Schweppes Cottee's plan to proceed with the initiative in the near future. |
Revised Energy Management Structure
At present, individual plants are not accountable for the energy used at the plant, e.g. compressed air, steam and electricity. The accountability structure does not provide for an incentive to plant managers and engineers to set targets for energy usage and minimisation of energy for the plant.
The initiative here was to set up energy metering equipment on
each plant to allow tracking of energy usage within the site as
a first step to implementing a management structure that allows
energy usage to managed and minimised.
Benefits : | The initiative would allow Schweppes Cottee's to monitor and manage energy usage around the site. An understanding of where energy is used would provide the first essential step in this process. The energy savings possible through this process are considered to be substantial, possible over 15%. If this was achieved Schweppes Cotteeís would save 1425 MW-hours of electricity and 10, 970 m3 of gas. This equates to 1400 tonnnes of CO2 per year for the electricity saving and 22 tonnes per year for the gas saving. |
Drawbacks: | To implement the initiative significant time and cost would be required to track down compressed air, steam and electricity lines. Further time and cost would be required to redirect lines and install metering equipment. The initiative requires a change in responsibility to plant managers. This would require consultation and training with them to enable the revised energy management system to be implemented effectively. |
Outcome: | As there was a significant amount of work to be done for this initiative, the project did not go ahead within the timeframe of the Cleaner Production Demonstration Project. However, it is recognised that significant advantages could be obtained through this process. As a result, Schweppes Cottee's plan to proceed the initiative with respect to steam usage in the near future. |
Following evaluation, Schweppes Cottees decided to proceed with
the replacement of the controller on the hot water maker to conserve
energy.
3.2.2 Project Implementation
The implementation of this initiative was straight forward with
the installation of a mechanically controlled steam valve to regulate
steam to heat the hot water maker.
3.2.2 Results
No specific details are available on the energy and costs savings
associated with this initiative.
3.3 BOD5 AND OIL AND
GREASE REDUCTION
3.3.1 Detailed Evaluation of Opportunity
Prevent Spillage and/or Collect and Recycle Cordial Spilt at the Filling Machine
There were opportunities to reduce BOD5 in the wastewater (and minimise product wastage) by reducing the amount of cordial spilt at the cordial filler. The causes of cordial spillage at the filler appear to be:
Spillage from the filler drains onto the floor and to the site
sewer.
The alternative to reducing waste was to collect and recycle the
spilt cordial. Line lube is used on the conveyor carrying the
empty bottles to the filler. Thus, to collect and recycle spilt
cordial, line lube would have to be eliminated from those conveyors
feeding the filler so that the recycled cordial is not contaminated
with impurities.
The possibility of not using line-lube on conveyors transporting
empty bottles to the filler was discussed with operational personnel.
The line supervisor reported that, on occasions where for some
reason the line-lube system failed and lube was not applied to
the conveyor, the bottles fall over and will not pass through
the sorter efficiently.
Although the amounts of cordial produced and bottled are recorded
at the site, these figures have a wastage factor built into them.
Therefore, it was not possible to determine exactly how much
cordial was being wasted at the filler.
Benefits : | The proposed system would reduce product wastage and decrease BOD levels in discharges to sewer. This would result in increased productivity and decrease in wastewater discharge costs. The economic benefits were such that a 20% decrease in BOD level would result in a 10% decrease in wastewater charges (c/kL). |
Drawbacks: | Schweppes Cottee's advised that the filler had been recently upgraded, and the subject of a number of studies, and did not think that further improvement in the performance of the filler was possible. There were some operability concerns. |
Outcome: | As the perceived benefits of the potential project were difficult to accurately determine, and the solution to the problem appeared to be complicated, this project was not implemented. |
Optimising Line-lube Sprayers
The primary source of oil and grease in the wastewater system
is associated with line lube chemical in the wastewater. Minimising
the amount of line lube on the conveyors has the potential to
decrease the amount of oil and grease disposed of to sewer.
Benefits : | Approximately $45,000 is spent annually on 13,000 litres of line lube. Collecting and recycling line lube would reduce costs, wastewater volumes and water usage. Line lube has high concentrations of oil and grease. By reducing the amount of line lube used, concentrations of oil and grease in the wastewater would be reduced. The financial benefits in decreasing oil and grease in the wastewater are not great as the contribution of oil and grease to the total wastewater costs is about 1%. |
Drawbacks: | During the timeframe of the cleaner production project, independent changes were being made to one of the jam lines, the changes included re-organisation and improvements in the line lube system on this line. Controlling line lube to co-ordinate with conveyor movement was seen to be a relatively complicated project. Management preferred to wait until the new system was installed, determine whether any lessons could be learnt from this system, and apply any improvements to the rest of the lines at a later stage. Discussions with line-lube suppliers and other manufacturers revealed that the collection and recycling of line lube may not be feasible, as the recycled line lube would have to be filtered and re-dosed prior to reuse. |
Outcome: | The improvement of the line-lube system was not completed as part of this project. As part of the jam line improvements being independently implemented, the type of line-lube product used was changed. The benefits of this changeover are documented in Section 3.3.3. |
3.3.2 Project Implementation
Separate to the initiatives undertaken as part of this project,
the line lube system on the cordial and jam production lines has
been improved,. The improvements were completed by line-lube
suppliers, Diversey, at no cost, and involved:
Equipment installed as part of the improvements remains the property
of Diversey.
3.3.3 Results
Improvements to the line-lube system have resulted in:
Other benefits which are though to be attributed to the new line-lube
system are:
4.0 REVIEW OF PROJECT
Many cleaner production opportunities were identified at the Schweppes
Cottee's site. The projects which were implemented during the
timeframe of the Demonstration Project were mostly of a small
scale, and successful. The projects focussed on water minimisation
and reduction of energy usage. All of the projects had a payback
period of less than 5 months.
While the project was a success at Schweppes Cottee's, there was
scope for increasing the benefits of the project. Achievements
at Schweppes Cottee's were mainly limited by the fact that the
various projects were to be implemented by one person at the site,
who was extremely busy, and there were no personnel made available
to which aspects of the projects could be delegated.
The implementation and day-to-day monitoring of the project was
the responsibility of one engineer. The project may have been
more successful had more of Schweppes Cottee's personnel been
involved to share the workload. As a result, actual implementation
of the various projects was slower to start, and took longer,
than expected, mainly due to lack of resources.
During the course of the project, Schweppes Cottee's advised that
corporate management had placed a restriction on capital expenditure
at the site, which would affect the commitment of finances to
the project. This restriction was shortly lifted, and did not
have an adverse impact on the success of the project.
Actual costs and benefits of implementing the projects were largely
as anticipated.
There appears to be some commitment to continue investigating
and implementing the other opportunities for cleaner production
identified at the site. Cleaner production initiatives have been
implemented at the site independent of this project, with significant
benefits.
5.0 CONCLUDING REMARKS
Based on the experience of implementing a Cleaner Production Program
at Schweppes Cottee's, significant environmental and economic
savings can be expected form the application of Cleaner Production
to the food industry.
A key lesson from this case study is that the process of compiling
environmental and process data in itself plays an important role
in the identification of Cleaner Production initiatives. Furthermore
old sites, which have had processes added to or modified, are
likely to have the potential to significantly improve utility
efficiency with resulting environmental and economic benefits
through Cleaner Production initiatives.
The other key lessons identified in the case study that the once
the initiatives have been identified, organisation have can have
significant flexibility in the implementation of the initiatives,
especially when the initiatives are relatively simple and have
low capital cost.
6.0 SCHWEPPES COTTEE'S PERSPECTIVE
"The Cleaner Production Demonstration Project highlighted
a number of benefits to our company.
We were able to reduce water and energy consumption in a number
of areas of our factory and therefore save money. Another benefit
was to gain a greater understanding of our factory as far as where
the energy and other resources were used. Prior to this project,
we only had rough numbers or numbers that covered the entire site
with respect to water and energy use. Following the project we
are able to break down into specific areas water and energy consumption
to easily measure any improvements.
Early on in the project a number of possible opportunities were
identified. Most of these required a lot of investigation to
see if they are viable. At the time we were extremely busy with
production, one line in particular was operating 24 hours per
day, 6 days per week which made it difficult to work on the project.
Tradesmen were also busy supporting production and largely unavailable
for project work.
None of the opportunities identified had any large dollar savings,
that is enough to justify extra resources which would have had
to come from outside the company. For us to justify extra resources,
we needed to identify the savings that would have come as part
of the project. We could not do this while we were gathering
the information to see if the project was viable.
We will continue to work on all the initiatives identified in
the report. I will be happy to give details to the EPA. As the
cost of water and energy continues to rise, some of the projects
become more viable.
Other similar demonstration projects would be beneficial to industry
if it can show them that you can do things better or in a way
that saves you time, money or resources. We should always be
looking at ways of doing things better as technology is changing
all the time. If you are not prepared to change you will be left
behind. We have proved that we can do things better on our site
and save money and resources at the same time, so it is possible
to do similar things at other companies."
David Fox
Engineering Manager