Cleaner Production Demonstration Project at CSR Wood Panels
EXECUTIVE SUMMARY
1.0 REVIEW OF CSR WEATHERTEX OPERATIONS
2.0 PLANNING AND ORGANISATION OF CLEANER PRODUCTION PROJECT
2.1CLEANER PRODUCTION APPROACH USED AT CSR
2.2CLEANER PRODUCTION OPPORTUNITIES AT CSR WOOD PANELS
2.2.1Reduced Board Defects
2.2.2Improved Paint Application
2.2.3Board Thickness
2.2.4Sale of Wood Waste
2.2.5Sale of Brick Strips
2.2.6Reduced Effluent
2.2.7Increased Pack Sizes
2.2.8Irrigation of Forest Plantation
2.2.9Operating Procedures3.0 CLEANER PRODUCTION INITIATIVES
3.1REDUCTION IN BOARD REJECTS
3.1.1Detailed Evaluation of Opportunity
3.1.2Project Implementation
3.1.3Results
3.2REDUCED PAINT OVERSPRAY
3.2.1Detailed Evaluation of Opportunity
3.2.2Project Implementation
3.2.3Results
3.3BOARD THICKNESS CONTROL
3.3.1Project Evaluation and Implementation
3.3.2Results
3.4SALE OF SOLID WOOD WASTE
3.4.1Project Evaluation and Implementation
3.4.2Results
3.5SALE OF BRICK STRIPS
3.5.1Project Evaluation and Implementation
3.5.2Results
3.6REDUCED WASTE WATER
3.6.1Detailed Evaluation of Opportunity
3.6.2Project Implementation
3.6.3Results
3.7INCREASED PACK SIZES
3.7.1Detailed Evaluation of Opportunity
3.7.2Project Implementation
3.7.3Results
3.8IRRIGATION OF FOREST PLANTATION
3.8.1Project Evaluation and Implementation
3.8.2Results
LIST OF FIGURES
FIGURE 1 PAINT USAGE EXPERIMENTS
The Cleaner Production Demonstration Project is
an initiative of the Environment Australia - Environment Protection
Group. The aim of the Project was to raise the awareness of Australian
industry and actively promote cleaner production issues. This
was to be achieved by conducting ten successful cleaner production
demonstration projects in industry around Australia, documenting
the benefits and experiences of the project, and publicising the
results to wider industry. Dames & Moore, assisted by Energetics,
were engaged as technical consultants on the project. The project
commenced in June 1994, and ran for 27 months.
CSR Weathertex was selected as one of the ten
companies to participate in the project. This case study report
presents a record of the progress of the CSR Weathertex project,
from initial meeting to project completion, and details the results
of the project and any problems which may have been encountered.
CSR Weathertex is part of the CSR Timber Products
division. It produces "Weathertex" manufactured wood
paneling made from processed timber.
The plant has undergone a major and radical restructuring
and downsizing during the period of the cleaner production program.
Whilst the uncertainty created during this change initially halted
cleaner production work, the new "leaner" focus ultimately
produced far more impressive results than might otherwise have
been the case.
The workforce has been re-organised into teams
covering each production area. The teams have responsibility for
achieving production targets and identifying the reasons for any
shortfall. This has resulted in a rapid and very significant improvement
in productivity and quality, leading to a vastly improved financial
position.
Cleaner Production philosophies have been whole-heartedly
embraced in a bid to return the plant to profitability. The impetus
for this came from the Weathertex site personnel who recognised
the financial value of reducing the cost of waste and inefficient
practices. This approach has undoubtedly provided a rapid and
low cost means of securing significant savings on the site.
Economic imperatives have forced rapid changes
on the site and it was fortuitous that the project was running
during this time to record the changes made and provide some assistance
along the way. From a somewhat hesitant start, when it appeared
financial and human resources would limit what could be achieved,
the situation rapidly evolved to one where there were almost too
many projects to track and record.
This report identifies 8 separate cleaner production
opportunities:
Together these actions are saving and are expected
to save over $1.3 million per year for the plant and have significantly
contributed to the ongoing viability of the plant and the well
being of the local community.
The improvements are almost all related to the
change in work culture brought about by the change to the work
team environment. This has been coupled with an improved understanding
of the process through simple research and systematic monitoring
of process variables. Other than the capital cost of retraining
the work force, most of the projects have involved very little
capital cost. The exceptions are the effluent works which were
required to meet state EPA licence requirements. Improvements
to the paint system required capital expenditure of around $50,000.
The changes implemented on this site are a model
case study of what can be achieved through Cleaner Production
processes.
1.0 REVIEW OF CSR
WEATHERTEX OPERATIONS
The Weathertex plant at Raymond Terrace is a division
of CSR Timber Products. It produces manufactured timber board
designed for external use. The major uses are for house cladding
and signboards. The site also formerly produced "masonite"
products, but following a major company re-organisation midway
through 1995, the plant now produces "Weathertex" only.
In former years, the plant provided the main employment
for the township of Raymond Terrace, north of Newcastle. The size
of the workforce has reduced from 250 people down to 80 people
due to changes in technology and product mix, but the plant still
plays an important role in generating income for the town.
The process is based on the Mason gun, a technology
which uses high pressure steam to reduce wood chips to their constituent
parts before being reformed into the appropriate shaped board.
Operations at CSR Weathertex include:
Chipping: | A variety of hardwood species are chipped |
Mason Guns: | The chips are subjected to high pressure steam, which is suddenly released, causing the wood to break into its constituent parts. |
Stock Preparation
Board Making: | Mixing wood fibre into a slurry ready for forming. The wood slurry is then poured onto a forming mat and rolled to produce "wet lap". |
Pressing: | The wet lap is cut to length and subjected to high pressure and temperature. This removes all remaining water and cures the natural resins to bind the wood fibres together. |
Finishing: | The boards pass through a number of operations involving: |
|
Wastes generated at the site include wastewater, waste oil, solvents, liquid paints, turpentine, empty drums, solid paint, wood fibre, broken boards and offcuts, wood sludge, sawdust, logyard mulch and general garbage.
A structured approach was used to identify opportunities and implement Cleaner Production at CSR. The approach included:
1 | An initial "review" of the site, conducted by Dames & Moore and Energetics in close discussion with CSR personnel. The purpose of this audit was to provide preliminary information on the operation of the site, and identify general cleaner production opportunities. |
2 | Follow up site visits and meetings between Energetics, Dames & Moore and CSR, with the objective of reviewing site processes in more detail, and identifying specific cleaner production opportunities with potential to become cleaner production projects. |
3 | Evaluating the pros and cons associated with each of the potential cleaner production opportunities. |
4 | Selection of the opportunities to be implemented at the site (to be decided by Moore Business personnel in discussion with management). |
5 | Implementing the selected opportunities and conducting any monitoring required to demonstrate the benefits of the opportunities. |
From the outset, and throughout the course of the project, it
was envisaged that CSR were to be responsible for the day-to-day
running of the project. Dames & Moore and Energetics acted
as catalysts for ideas and were responsible for providing
technical back-up as required and documenting the results of the
project.
The incentive for implementing cleaner production at CSR Weathertex
has altered radically since the beginning of the project and this
has changed the focus for identifying suitable cleaner production
projects.
At the beginning of 1995 (and the commencement of site work for
the Cleaner Production program), the site was operating 7 days
per week with a workforce of over 250 people. At full production
rate, disposal of effluent from the process was looming as a significant
issue and one which, if not addressed, would have the potential
to close the plant down. Actions were already being taken to address
this, however, it was perceived the Cleaner Production process
would provide much needed assistance.
Midway through 1995, a deteriorating market place forced CSR to
re-organise its Timber Products division. For the Raymond Terrace
plant, this meant operating hours were reduced to 3 to 4 days
per week, the workforce was reduced to 80 people and the number
of different types of boards produced was also reduced. The threat
of total closure was imminent if financial performance did not
quickly and substantially improve.
The effect of this on the Project was two-fold. Firstly, the effluent
problem was largely solved due to the reduced operating hours
of the plant. Secondly, the plant had to identify ways to cut
costs with little or no capital expenditure.
As a result the cleaner production opportunities were developed
as part of the overall plant improvement. All employees were
encouraged to identify opportunities, especially the quality teams
on the site. The evaluation and implementation of the projects
was undertaken by CSR personnel with significant commitment from
senior site management.
2.2 CLEANER PRODUCTION OPPORTUNITIES AT CSR WOOD PANELS
The main cleaner production initiatives identified by CSR personnel
and the consultants involved:
These are discussed in more detail in the following sections.
Prior to the implementation of Cleaner Production methodology
to the site, the average net reject rate (after reworking) was
13.5% (6,750 tonnes/year). The cost of reject product for this
site was estimated to be $100,000 per 1%, so the total cost of
reject product was over $1.35 million per year. Reducing the reject
rate was therefore central to re-establishing financial control
of the site.
The high reject rate was due to a number of reasons. The most
important of these was the lack of control over the process and
insufficient understanding of the process variables. As there
was opportunity to reduce solid wastes and decrease overall costs,
the initiative to reduce board rejects was investigated as part
of this project.
2.2.2 Improved Paint Application
After pressing and planing, the board is cut into planks prior
to painting. Paint is applied using two spray guns. The site
consumed around 300,000 litres of paint and solvent each year,
at a cost of approximately $1.4M (based on the new, reduced production
requirements).
This operation was very inefficient and resulted in a great deal
of paint overspray. Waste paint built up rapidly inside the spray
booth, quickly blocking the filters exhausting air from the booth
and creating a significant housekeeping problem. Some of the
oversprayed paint was captured and recycled, but the recycling
process itself resulted in some waste also. Therefore, improved
paint spraying techniques would reduce air emissions and the amount
of waste paint and decrease operating costs. More efficient spray
systems were investigated as part of this project.
The thickness of the boards after pressing were not consistent. Boards over 10.5 mm thick were rejected, whilst boards less than 10.5 mm were accepted, but were planed to the correct thickness of
9.5 mm. Lost wood accounted for around 5% of total wood consumption,
or 1,800 tonnes per year.
This process resulted in waste of wood product and the generation
of dust which must be collected, stored and disposed of. By improving
control over board thickness, less wood would be wasted. This
opportunity was further investigated as part of this project.
Waste wood products are generated at various stages throughout
the process, they include:
Approximately 6,000 tonnes of wood waste are generated per year.
These were formerly disposed of to landfill, at a cost of around
$80,000 per year. There was an opportunity to identify a market
for the wastes and sell them, which was investigated during this
project.
The site has a large backlog of reject product. This is potentially
expensive to dispose of and is a demoralising reminder of previous
quality control problems. Converting this reject pile into saleable
product (ëbrick stripsí) will:
This opportunity was investigated as part of this project.
The board making process requires large volumes of water and results
in high effluent flow rate. Whilst it is possible to install
filtration equipment to recycle the effluent back to the process,
this would be expensive and could not be justified on this site
at the present time.
Two low cost opportunities were identified to reduce water waste,
however, as follows:
Broke Tank Overflows
The 'Broke Tank' is a central holding point for water flow in
the board making process. It is a relatively small tank (approximately
10,000 L) but has a very high flowrate through it.
This tank was found to overflow from time to time resulting in
a large loss of water. It was estimated that water lost through
overflow was in the region of 4.5 megalitres (ML) per annum.
The reasons for the overflow were investigated.
Boiler Feedwater Pump Cooling
Steam is used extensively on the site and this is supplied by
coal-fired boilers. The boilers are supplied with feedwater by
two feedwater pumps. Cooling water is supplied to the pumps to
prevent them overheating and this was largely being discharged
to the effluent plant. Approximately 5 ML per year of water is
used for pump cooling. There was an opportunity to collect and
recycle this cooling water, which was investigated during this
project.
Most of the finished product is transported from site in 1 tonne
'packs'. A 'pack' consists of a hardwood pallet and metal strapping.
There is a an opportunity to increase the standard pack size
to 2 tonnes, thereby reducing the amount of packaging required
per tonne of product.
This opportunity was investigated during the project.
2.2.8 Irrigation of Forest Plantation
The Weathertex plant produces around 1 ML of waste water each
production day. This is treated at an on-site effluent plant
to remove solids and neutralise the pH. It is then disposed of
by spray irrigation on surrounding land owned by CSR.
Some 6 ha of the 25 ha of irrigated land was purchased by the
NSW Roads and Traffic Authority for an upgrading of the nearby
Pacific Highway. If all the effluent had been irrigated on the
remaining 19 ha, this would have imposed an unacceptably high
biological oxygen demand (BOD) load on the soil and the company
would have been in breach of it's EPA licence conditions. An
alternative disposal point was therefore needed to secure the
viability of the plant and prevent environmental damage. This
opportunity was investigated further.
Many of the operational difficulties being encountered were due
to inadequate or incorrect procedures being followed. Whilst
written procedures were in place, these were often ignored.
A review of all procedures was required to assess them for correctness
and relevance to current operation. Adoption of a standard set
of procedures would then aid achieving uniformity in the process.
Progress was made toward preparing a standard set of procedures,
but these were not finalised during the course of the project.
3.0 CLEANER PRODUCTION INITIATIVES
A summary of the costs and benefits of the cleaner production
projects implemented is shown below.
3.1 REDUCTION IN BOARD REJECTS
3.1.1 Detailed Evaluation of Opportunity
The objective of this project was the reduction in the reject
rate of product through improved knowledge and control of all
stages of the process.
In keeping with the team driven approach, factors affecting product
quality and hence reject rate, were identified by teams representing
all stages of the process.
It was quickly realised that there was insufficient knowledge
on site of the important process variables to be controlled, but
that significant economic advantages could be achieved by better
understanding the process.
Therefore initiative resulted in a significant reduction in the
amount of rejects which resulted in significantly lower unit production
costs.
A methodical team approach was used to go through the board production
process to identify factors affecting product quality. Where
there was considered insufficient information, project team and
process operators investigated the impact on product quality and
identify the actions required to improve product quality.
One example of this, is the mix of tree species used to create
the wood pulp. Until reviewed by the team, the site had no detailed
understanding of the species that would enhance the performance
of the board making process and those that would detract from
it. Experimentation was conducted using a pilot plant on site
and this quickly identified the best species to use. An "Approved
Species" list has now been developed. Suppliers have been
trained to provide appropriate species, and logs are now branded
by a suitably trained contractor prior to collection.
Other process variables such as ëgun pressureí, ëwet
lapí thickness, and ëpressed boardí thickness
are now monitored continually, using chart recorders, manual measurements
and manual recorders.
An important and surprising result of the process was to reduce
the speed of the board machine from 32 ft/min to 28 ft/min; a
reduction of 12.5%. Process consistency and quality was improved
and output actually rose by some 17% as a result of this action.
Rejects are now monitored on a shift by shift basis by production
personnel from each area of the process. This allows rapid identification
of problem areas and allows response to the causes of rejects
as they occur, which is a major reason for the large reduction
in reject rate observed. Both gross and net rejects are monitored
to assess the quality of the production process and the ability
to recover from faults. Both measures provide an important pointer
to the performance of the plant.
Prior to targeting board reject rate as a high priority area for
improvement, net rejects were assessed on the basis of a monthly
stocktake. This method gave no indication of the gross reject
rate (ie: boards initially rejected and subsequently reworked)
and monthly reporting did not allow rapid response to developing
problems.
Gross reject rate from each stage of the process is now recorded
on a shift by shift basis by production personnel. They respond
to the causes of rejects as they occur and this is a major reason
for the very large reduction in reject rate observed.
A monthly summary of board rejects is still compiled, but this
details gross and net rejects from each production stage. This
allows much better analysis of any long-term trends in reject
rate.
Net rejects cost the plant approximately $100,000 per 1% of production.
As a result on the initiative, rejects have been reduced from
an average 13.5% (Jun 94 to May 95) to an average 6% (Nov ë95
to Apr ë96) representing an annual saving of some $750,000.
The primary cost to achieve this was in retraining the work force
to operate as self-directed work teams and establishing the management
systems to support this. The total cost of this was difficult
to quantify and the effect is spread over all operations of the
plant. A reasonable estimate of this cost is $100,000. Capital
cost for equipment was nil.
COSTS: | $100,000 |
SAVINGS: | $750,000 per year |
PAYBACK PERIOD: | less than 2 months |
3.2.1 Detailed Evaluation of Opportunity
Once the boards have been cut to the correct width, they are sprayed
with primer paint. This operation was very inefficient with a
great deal of paint overspray resulting in waste and a poor working
environment.
The objectives of this project were:
A team was assembled from production workers in this area to address
the problem. They contacted several suppliers of alternative equipment
and conducted trials of the existing system against potential
new systems. The key to reducing the overspray was the use of
appropriate spray nozzles.
A controlled experiment was conducted to determine the reduction
in paint overspray possible by improved equipment and set up methods.
A record was kept of paint consumption and board production rate
for a set period of time using the existing paint gun system.
A similar record was then kept using a new spray gun system. This
process allowed paint consumption and cost per square metre of
board to be identified for each system.
Two important results came out of this work. Firstly, it was found
that the existing estimates of paint consumption were inaccurate,
and secondly, it was found that the new system was much more economical
to use. Figure 1 demonstrates the results of these experiments.
Average paint use expressed as Litres/Plank has decreased by
approximately 25% as a result of the implementation of the new
paint spray system. The economic savings associated with the
initiative are shown below.
COSTS | Approximately $20,000 for new guns and tips and $30,000 to upgrade the paint filtration system | |
SAVINGS (Paint) | 170 mm board | 3 cents/plank |
213,000 planks per year | ||
$6,390 per year | ||
200 mm board | 23 cents/plank | |
888,000 planks per year | ||
$204,240 per year | ||
300 mm board | 27 cents/plank | |
360,000 planks per year | ||
$97,200 per year | ||
TOTAL | $307,830 per year | |
SAVINGS (Housekeeping) | Savings will also result through reduced clean-up time and reduced use of air and paint filters. These savings have not yet been quantified. | |
PAYBACK | Less than 2 months. |
Whilst this project requires capital expenditure of some $50,000,
the savings made will provide a payback period of less than 2
months.
The project resulted in improved paint coverage, reduced waste,
and a vastly cleaner spray booth.
3.3.1 Project Evaluation and Implementation
The objective of this project was to improve the consistency of
board thickness, thus reducing wood waste.
The reduction in the variation in board thickness was achieved
through improved selection of wood species, and some minor fine-tuning
of the process.
The improvement in board quality control has seen the variation
in thickness reduced by half, resulting in less raw material being
used, less planing required, and better housekeeping. Thickness
variations of up to 1 mm has now been reduced to a maximum of
0.5 mm, improving the yield from the timber input.
Average variation in board thickness was reduced from 0.5 mm (5%)
to 0.25 mm (2.5%), thereby saving 2.5% on raw material and producing
less dust from planing. The savings associated with this opportunity
are outlined below.
COSTS | Nil |
SAVINGS | 2.5% x 36,000 tonnes of wood (annual consumption) |
900 tonnes of wood per year | |
$35,000 per year | |
PAYBACK | Immediate |
3.4.1 Project Evaluation and Implementation
Waste wood products are generated at various points in the process
from the wood yard through to the finishing plant. While some
this waste was sold on an adhoc basis to surrounding nurseries,
most of the wood waste was sent to landfill.
The objective of this project was to reduce costs associated with
wood waste disposal.
The wood waste products are now sold for potting mix rather than
being sent to land fill.
This is a particularly impressive project as it emanated from
a former CSR employee made redundant by the downsizing in mid
1995. The employee was keen to remain working at the Weathertex
site and identified the potential for selling the wood wastes.
He now operates this activity as a business.
The project has led to a decrease in the quantity of solid waste
sent to landfill and identified an effective use of what was once
considered a waste from the site. The economic benefits of the
initiative are outlined below.
COST: | No capital cost |
$100,000 per year contracting and administration cost | |
SAVINGS: | Avoided land fill costs of $80,000 per year |
Generating revenue of $200,000 per year | |
Providing employment (under contract) for 1 person | |
Net improvement of $180,000 per year | |
PAYBACK: | Immediate |
3.5.1 Project Evaluation and Implementation
To dispose of reject boards the past practice was to cut the boards
into chips for boiler fuel or into packing strips for the brick
industry, or "brick strips". Both options are relatively
labour-intensive and detracted from the main production process
- hence the accumulated stockpile.
The objective of this project was to use old stockpiles of reject product to produce saleable product.
Two former employees now work as full-time contractors to convert
the reject boards into brick strips.
This arrangement has ensured:
The economic benefits of the initiative are outlined below.
COST: | No capital cost |
$100,000 per year contracting cost | |
SAVINGS: | Generating revenue of $150,000 per year |
Providing employment (under contract) for 2 persons | |
Net improvement of $50,000 per year, until the stockpiles are all sold | |
PAYBACK: | Immediate |
3.6.1 Detailed Evaluation of Opportunity
As discussed in Section 2, the early cleaner production work on
the site was directed toward reducing the impact of effluent from
the site. Part of this work included a water audit to identify
areas to reduce wastewater.
Following the change in emphasis for the cleaner production work,
much of this information was put aside. However, two areas had
been identified as wasting water and it was decided to proceed
with rectifying these.
Broke Tank Overflows
The first area, "broke tank" overflows was not only
responsible for wasting water but also halting production whilst
the reason for the overflow was identified and corrected.
A number of reasons for the overflows were identified and these
included:
These problems were solved by:
Savings of some 4.5 megalitres per year will result.
Boiler Feedwater Pump Cooling
Water used for cooling the boiler feedwater pumps is presently
discharged to a drain and disposed of through the effluent system.
This water will be redirected to a holding tank supplying fresh
water to the process, saving approximately 5 ML of water per year.
Measures to reduce wastewater, by preventing overflows and directing
cooling water back to the board making process, resulted in a
water saving of approximately 9.5 ML/yr. The economic benefits
of the initiative are outlined below.
COST: | $5,000 |
SAVING: | 9.5 ML per year |
Note:
Water is taken from on site bores and disposed of on site so cost of water is minimal.
Indicative savings for this project in a metropolitan location
at $1.50/kL = $14,250 per year
3.7.1 Detailed Evaluation of Opportunity
The objective of this initiative was to reduce the amount of packaging
required per tonne of product. The finished boards are loaded
onto pallets in packs of 1 tonne and shipped to distribution centres.
An opportunity was identified to increase the size of the pack
to 2 tonnes and thereby reduce the amount of packaging material,
and hence the cost. Converting 70% of 1 tonne packs to 2 tonne
packs saves $20 per 2 tonne pack.
This project was not implemented.
Negotiations are still proceeding on this project, but it is expected
a 2 tonne pack will soon be introduced for around 70% of the product
dispatched.
The expected economic benefits of the initiative are outlined
below.
COSTS: | Nil |
SAVINGS: | $28,000 per year |
PAYBACK: | Immediate |
3.8 IRRIGATION OF FOREST PLANTATION
3.8.1 Project Evaluation and Implementation
As discussed in Section 2, the irrigation system was considered
to be the major area in need of improvement, due to increasingly
stringent licence requirements.
Accordingly capital works were undertaken to upgrade the effluent
treatment plant (principally clarification and neutralisation)
and to develop an irrigation network for neighbouring pine and
hardwood plantation forests.
The irrigation system resulted in:
The proposed initiative has led to more sustainable irrigation
practices and a more sustainable use of the forest resources.
Savings will accrue from improved forest yield but cannot be assessed
as yet. The costs and benefits of the initiative are summarised
below.
COST | $2 Million (including upgrade of water treatment plant) |
BENEFITS |
|
4.0 REVIEW OF PROJECT
Following the re-organisation, there was a rapid change in priorities.
The effluent issue receded due to reduced operating hours of
the plant (7 days/week down to 3-4 days/week). The amount of effluent
to be discharged reduced proportionately. Reducing operating costs
became the prime objective and the plant was still under threat
of closure if a satisfactory financial performance could not be
achieved.
The radical re-organisation of the operation at CSR Weathertex
required a step change in the way management and the workforce
approached their responsibilities. The opportunity was taken
to implement a "team based" approach to manufacturing,
with management and technical resources available for support.
This re-organisation resulted in a fundamental change of attitude
amongst the workforce and is the basis for the rapid improvements
demonstrated.
The focus of the Cleaner Production activities for this site has
shifted over time. During the initial site visits in early 1995,
the plant was operating seven days per week and the market appeared
buoyant. Reject rates were a concern, but a team was already
addressing this issue and the prospect of action from the state
EPA due to effluent discharge was considered a greater priority.
Accordingly, water minimisation and effluent re-use strategies
were considered.
Within six months however, the building market had declined and
the financial performance of the plant was considered unacceptable.
For several months, Cleaner Production activities were halted
whilst the future shape of the site's operations were determined
and the workforce was reduced by two-thirds.
Teams have been formed for each process area and have been given
the tools to monitor the consistency and quality of the output
from their process. In most instances monitoring is through simple
manual graphing of important process variables.
The teams have participated in brainstorming sessions and followed
the methodology of CSR's 'BIQ' or Building in Quality Program.
This places a strong emphasis on identifying an area for improvement,
stating a vision, measuring performance and systematically identifying
the key areas to address.
The teams have had strong and clear leadership from their "team
leader", Bill Gissane, who is also the site manager. The
site has shown a very high level of autonomy in pursuing their
identified goals and managing the various changes required to
improve performance.
To say there have been no problems during the Cleaner Production
Project would be to trivialise the extensive and somewhat traumatic
changes wrought on the company, brought about by a stagnant market
and unsustainable financial performance. The response however,
has been an outstanding demonstration of what can be achieved
by a motivated workforce.
A summary of the costs and benefits of cleaner production initiatives
is shown below:
Reduced Reject Rate | 100,000 refer to discussion. | 2,700 tonnes wood
37 tonnes wax 22,000 litres paint and solvent 200,000 kWh Electricity 450 tonnes coal 194 tonnes of greenhouse gas | less than 2 months | |
Reduced Paint overspray | 50,000 | 80,000 litres paint | less than 2 months | |
Improved board thickness control | Nil | 900 tonnes wood per year | Immediate | |
Sale of waste wood products | Refer to discussion. | 6,000 tonnes per year
Work for 1 person | Immediate | |
Sale of Brick Strips | Refer to discussion. | 120,000 m2/year
Work for 2 people | Immediate | |
Reduced waste water | 5,000 | 9.5 ML per year | ||
Increased Pack Sizes | Nil | 15,000 kg packing material | ||
Irrigation system | 2,000,000 | Improved forest yield
Reduced water loading on soil |
5.0 CONCLUDING REMARKS
It is fair to say that Cleaner Production principles became the
guiding light for the plant. This was not however, an initiative
imposed from outside, but a recognition of the need to substantially
reduce waste in order to become competitive.
The greatest potential obstacles to the program - a massive reduction
in workforce and output, and threatened closure - thus became
the greatest impetus to achieve change.
The major changes made relate to improvements in board quality
and a reduction in paint wasted in the finishing section. These
improvements account for over 80% of the total financial improvement.
6.0 CSR'S PERSPECTIVE
"In the timber processing business, we are acutely aware
of environmental concerns. We are privileged to have access to
a great resource and it is fundamental that we are careful and
wise with its use. There is no commercial or moral justification
for wasting any resource, particularly native Australian
timber. The Cleaner Production Project has been a magnificent
opportunity for us to learn how to husband our resources more
effectively. We have profited from the Project and if all Australian
Industry can learn something from us we will have been happy to
make a contribution".
Bill Gissane
CSR Wood Panels