Cleaner Production Demonstration Project at Bonlac Foods, Stanhope

Table of Contents

EXECUTIVE SUMMARY

1.0 REVIEW OF BONLAC OPERATIONS

2.0 PLANNING AND ORGANISATION OF THE BONLAC FOODS CLEANER PRODUCTION PROJECT
2.1 CLEANER PRODUCTION APPROACH USED AT BONLAC FOODS
2.2 CLEANER PRODUCTION OPPORTUNITIES
2.2. 1 CIP Chemicals Change Over
2.2.2 Diversion of Waste Water to Farmland
2.2.3 Solids Screening from Cheese Room Waste Water
2.2.4 Alternative Disposal of Soap Stock

cs_bon7.gif - 93.4 K 3.0 CLEANER PRODUCTION INITIATIVES
3.1 CIP CHEMICALS CHANGEOVER
3.1.1 Project Evaluation and Implementation
3.1.2 Results
3.2 DIVERSION OF WASTE WATER TO FARM IRRIGATION
3.2.1 Project Evaluation
3.2.2 Project Implementation
3.2.3 Results
3.3 SOLIDS SCREENING FROM CHEESE ROOM WASTE WATER
3.3.1 Project Evaluation
3.3.2 Project Implementation
3.3.3 Results
3.4 ALTERNATIVE DISPOSAL OF SOAP STOCK
3.4.1 Project Evaluation
3.4.2 Project Implementation
3.4.3 Results

4.0 REVIEW OF PROJECT

5.0 CONCLUDING REMARKS

6.0 BONLAC FOODS PERSPECTIVE

LIST OF TABLES
TABLE 1 DAILY MARGINAL COSTS ASSOCIATED WITH CHANGE OVER TO STABILON®

LIST OF FIGURES
FIGURE 1 VOLUME OF WASTE WATER DISCHARGE TO THE WASTE WATER TREATMENT FACILITY PER TONNE OF CHEESE PRODUCED FOR BOTH THE 1995/1996 SEASON AND THE 1994/1995 SEASON (kL OF WASTE WATER/TONNE OF CHEESE)

FIGURE 2 TONNE OF CHEESE PRODUCED PER KILOLITRE OF MILK INTAKE FOR BOTH THE 1995/1996 SEASON AND THE 1994/1995 SEASON (TONNE OF CHEESE/kL OF MILK INTAKE).

FIGURE 3 VOLUME OF EFFLUENT DISCHARGED TO THE WASTE WATER TREATMENT FACILITY BEFORE, DURING AND AFTER THE DIVERSION OF LOW IONIC WASTE STREAMS TO FARMLAND FOR IRRIGATION.

FIGURE 4 VOLUME OF EFFLUENT DISCHARGED TO THE WASTE WATER TREATMENT FACILITY PER TONNE OF CHEESE PRODUCED, BEFORE, DURING AND AFTER THE DIVERSION OF LOW IONIC WASTE STREAMS TO FARMLAND FOR IRRIGATION.

FIGURE 5 TOTAL SUSPENDED SOLIDS IN THE WASTE WATER DISCHARGE STREAM PER TONNE OF CHEESE PRODUCED FOR THE 1995/1996 CHEESE PRODUCTION SEASON.

FIGURE 6 TSS IN WASTEWATER PER TONNE OF CHEESE PRODUCED 1995/1996 SEASON (SCREENS INSTALLED NOVEMBER 1995)


EXECUTIVE SUMMARY

The Cleaner Production Demonstration Project (the Project) was an initiative of Environment Australia -The Environment Protection Group (EPG). The aim of the Project was to raise the awareness of Australian industry and actively promote cleaner production issues. This was to be achieved by conducting ten successful cleaner production demonstration projects in industry around Australia, documenting the benefits and experiences of the project, and publicising the results to wider industry. Dames & Moore, assisted by Energetics, were engaged as technical consultants on the project. The project commenced in June 1994, and ran for 27 months.

Bonlac Foods' Stanhope facility in Victoria was selected as one of the ten companies to participate in the project. This case study represents a record of progress of the Bonlac project, and any problems or lessons which may have been encountered. The case study demonstrates the application of Cleaner Production to the dairy foods processing industry.

Bonlac Foods, Australia's largest manufacturer of dairy products, is committed to producing high quality dairy products with minimal impacts to the environment. When producing cheese and milk powder, Bonlac is faced with the problem of preventing small particles of cheese entering its waste water drainage system. These particles represent a loss of product and add an unnecessary load onto the waste water treatment facility.

In addition, Bonlac must ensure that all process equipment, pipes and tanks are kept clean and free of unwanted micro-organisms. This is achieved with a periodic chemical flushing process called, Cleaning In Place (CIP), and involves the use of both alkaline solutions and acid detergents. These chemicals ultimately discharge to the waste water treatment facility and increase the load on the system.

The cleaner production demonstration projects that were initially identified were as follows:

Alternative CIP Cleaning Process/Solution

The use of Stabilon ® was expected to reduce the use of an acid cleaning solution in the dairy CIP process. It was also expected to reduce the total volume of waste water and phosphorous levels in the effluent being discharged to the waste water treatment facility. Change over to Stabilon®; detergent was found to reduce the cycle time of the CIP process, providing more time to produce cheese. This resulted in an income net benefit of about $310.00 per day.

Diversion of Waste water to Land Filtration

Some of the less contaminated waste water streams were to be diverted to a farm for spray irrigation thus reducing the biological and hydraulic load on the effluent treatment facility. The diversion to farm is limited to the drier months. Soil which is too wet cannot effectively handle the additional waste water.

Results of a ten day trial indicated a 30% reduction in the waste water volume discharged to the waste water treatment facility. The diversion will recommence on a regular basis in the next cheese production season.

Solids Screening, Cheese Room Waste water

Appreciable quantities of cheese solids are lost to the drain in the cheese room operations during normal production, daily wash down and the CIP process.

Bonlac aims to capture these solids and reduce the organic load on the waste water treatment facility. Two methods were proposed to deal with this issue. The first involves installing screens at the points where the large losses occur. The second method involves installing two large settling tanks in the whey room to capture cheese fines in the process rinse water. The impact of the project was to be assessed by monitoring the total suspended solids levels in waste water discharge from the cheese room.

Overall levels of suspended solids in the water was immediately noted as a results of the project implementation. The reduction was not as significant as expected but this is largely attributed to only one settling tank being commissioned. In addition, insufficient time was available to properly tune the tank to operate at optimum design conditions. This is believed to have reduced the effectiveness of the settling tank in removing the solids from in the waste water discharge. However, Bonlac will have both tanks operational and fully tuned for the next cheese production season. It is expected that the TSS level in the waste water discharge will show a significant reduction.

The total cost for the works to capture the cheese fine was about $30,500 The budget recovery of the fines was monitored by Bonlac Stanhope on a monthly basis. The recovery is expected to translate as $100,968 Therefore, the payback period for this project is less than 4 months.

Alternative Disposal of Soap Stock

Soap stock is a by-product of anhydrous milk fat production. It is basically a mixture of caustic soda and free fatty acids, and is approximately 5 % solids. It is normally disposed to landfill at a property owned by Bonlac. An opportunity was identified to sell the product to commercial soap manufacturers, however the natural composition of the soap stock was found to vary beyond the specifications imposed by the soap manufacturer and the project was postponed indefinitely.

A key lesson from this Cleaner Production demonstration project is that the process of compiling the environmental and process data in itself plays an important role in the identification of Cleaner Production initiatives. Other important lessons which emanated from demonstration project include the importance of commitment from management, ideas are encouraged in teams commissioned to assess specific parts of the operation, and that opportunities do not have to involve large capital costs.

Cleaner Production initiatives have been implemented at Bonlac Foods (Stanhope) with significant improvements. This has provided Bonlac with incentive for other Cleaner Production opportunities to be investigated and implemented.

Table of Contents

1.0 REVIEW OF BONLAC OPERATIONS

Bonlac is Australia's largest manufacturer of dairy products, with an annual turnover of $1 billion. In addition, Bonlac has grown to become one of the largest processed food exporters in the country with markets in more than 50 countries. Bonlac processes whole milk obtained from local dairy suppliers to produce milk powders, anhydrous milk fat, demineralised whey and cheese. Butter, cream and processed cheese are other Bonlac products.
cs_bon7.gif - 93.4 K

The Stanhope facility processes whole milk transported by road tanker from some 780 local suppliers. The facility produces a variety of cheese, milk powders and anhydrous milk fat. The facility currently employs 241 people which includes seasonal workers during the peak milk intake period. Milk production peaks in December and January but declines during the winter months.

The manufacturing processes typically involve demineralisation, cheese making and spray drying.

In the cheese making plant, milk stored in silos is pasteurised prior to being churned within a network of stirred vats. The vats are heated with process water, and operate in batch mode. During the batch cycle, the milk is converted into a mixture of curd and whey. This mixture is fed into the "Alf-O-Matic" cheese maker which separates the whey, and converts the curd into cheese solids. The cheese is then salted to extract water held by the cheese prior to being transported into the "Wincanton Tower" cheese presses. The cheese solids are compacted in the towers to produce 25 kg cheese blocks which are packaged, labelled and dispatched off-site for further processing.

The other major operation at the Stanhope facility involves the production of milk powder. Milk from the storage silos is fed into a series of evaporators to produce a milk concentrate. The concentrate is then fed into one of two spray dryers from which fine milk powder is produced. The powder is subsequently packaged for sale off-site.

Maintaining clean process vessels and equipment is extremely important for Bonlac. This is achieved by periodic cleaning of the plants process facilities with detergents and other chemicals. The procedure is called Cleaning In Place (CIP), and involves the use of acids and alkaline solutions. This cleaning procedure, in addition to the normal process operations generates large volumes of waste water.

The site generates over 3.3 million litres of waste water each day. The waste water is directed to the plants waste water treatment facility. The treatment facility consist of a series of aeration ponds, anaerobic lagoons and staged settling lagoons. Treated effluent is then discharged into Deakin Drain, a canal which channels the waste water into the Murray River. Bonlac have an EPA licence which outlines conditions pertaining to this discharge.

In order to meet the demands of its customers and produce high quality dairy products, Bonlac performs its operations to an accredited Quality Management System (ISO 9002). Bonlac is also committed to producing high quality products with minimal impacts to the environment. The site is currently seeking accreditation for implementing and developing an Environmental Management System based on ISO 14001. In addition, Environmental Teams were established at Stanhope, to address environmental issues such as monitoring the plants performance in relation to waste water, reduction in the use of cleaning chemicals and reducing general waste generated during the manufacturing operations. Bonlac's philosophy is to minimise and reduce the impact of waste generated by the plant operations by improving the process efficiency. Through continuous improvement, Bonlac intend to increase the product recovery and simultaneously decrease the cost incurred with waste handling. Cleaner production was identified by Bonlac as a medium to facilitate the realisation of these goals.


2.0 PLANNING AND ORGANISATION OF THE BONLAC FOODS CLEANER PRODUCTION PROJECT

2.1 CLEANER PRODUCTION APPROACH USED AT BONLAC FOODS

Bonlac Stanhope have implemented Environment Teams dedicated to identifying target areas to improve environmental performance. One such group is the Cheese Waste Reduction Team. The main aim of this team is to develop strategies to reduce the use of cleaning detergents, waste water, and product and raw material wastage in the cheese plant. Work teams have also been established in the spray drying areas, milk receival and product packaging, all with a focus on continuous improvement and waste minimisation. The Environment Teams meet regularly to evaluate suggestions seen to benefit Bonlac through enhanced process efficiency, and benefit the surrounding environment through reduced discharge of waste.

At the outset of the Demonstration Project, Bonlac Foods realised that the concept of Cleaner Production would help facilitate some of the areas identified by the Environment Teams. An initial meeting was held between senior staff at Bonlac, and Dames & Moore, to discuss some of the options and ideas available for the Cleaner Production Demonstration Project. Dames & Moore facilitated those meetings, and assisted with evaluating the advantages and disadvantages of various projects. However, the final selection decision was made by Bonlac based on areas which were perceived as having greatest potential in terms of returned benefit to the company and the environment.

The key personnel involved in the Bonlac Cleaner Production Demonstration Project team were:

Throughout the duration of this project, regular meetings were held between Bonlac and Dames & Moore. Dames & Moore provided technical advice as required, and documented the results of the project. Bonlac was responsible for the implementation and development of the projects.

2.2 CLEANER PRODUCTION OPPORTUNITIES

A number of opportunities were identified by the Environment teams. The four projects selected were:

There were no formal criteria such as economic evaluation or a feasibility analysis, used to choose these projects. However, the projects were deemed by Bonlac to provide an excellent opportunity to demonstrate the benefits of cleaner production.

This section describes the four cleaner production projects that were identified.

2.2.1 CIP Chemicals Change Over

In order to protect human health, all food processing plant and equipment must be maintained in an extremely clean and hygienic condition. Bonlac must maintain clean conditions in all its process equipment and pipes which handle materials related to the cheese making process. The equipment surfaces are Cleaned In Place (CIP) with a combination of alkaline solution, acid detergents and hot water. The acid detergent normally used at Bonlac is a mixture of nitric and phosphoric acids.

Approximately 300L per day of spent acid and alkaline wastes are discharged to site waste water treatment ponds which eventually discharge to surface drains. Nitrates and phosphates in the waste are undesirable because these compounds increase the nutrient loading in the waste water, which enhances the risk of algae growth and eutrophication of the receiving waterways, in this case the Murray River.

An alternative to this acid mix is Stabilon®; detergent. Stabilon® is a combination of complex agents, wetting agents, anti-foam agents, cleaning activators and emulsifiers.

When used in conjunction with caustic soda, the need for a regular acid cleaning stage in dairy CIP systems can largely be eliminated.

The use of Stabilon® would reduce the nitrate and phosphate load in the waste water, but also reduce the total volume of effluent disposed to the waste water treatment facility. This is because Stabilon® has more effective cleaning properties compared with the traditional acid mixture and the large liquid volumes associated with the acid cycle is eliminated.

2.2.2 Diversion of Waste Water to Farmland

Total effluent to the waste water treatment facility is approximately 3,390 kL of waste water per day. There are three waste water streams which contribute a substantial volume to the waste water treatment facility. They are:

These streams are relatively clean, and free of significant quantities of suspended or dissolved solids. It was proposed to divert these streams away from the waste water treatment facility to nearby farmland for irrigation. If successful, the cost savings arising from the reduced volume of effluent to be handled by the sites waste water treatment facility would be significant.

2.2.3 Solids Screening from Cheese Room Waste Water

Cheese solids are lost to the drain in the cheese room during normal operations, daily wash down and the CIP process. The sources of cheese solid losses include the cheese vats, the Alfa-O-Matic cheese maker, the salting station and the Wincanton towers (used to press the cheese into blocks). It was proposed to capture these solids and reduce the amount of cheese solids in the waste water discharged to the waste water treatment facility.

2.2.4 Alternative Disposal of Soap Stock

Soap stock is a by-product of the anhydrous milk fat manufacturing process. It essentially consists of caustic soda and free fatty acids, and is approximately 5 per cent solids. The plant produces approximately 1200 tonnes of soapstock per year. At the outset of the project, the soap stock was currently land farmed at a property owned by Bonlac. Soapstock contains high salt levels which could possibly leach into the groundwater. An alternative to land disposal was identified. It was proposed to sell the soap stock to commercial soap makers. However, before potential buyers could be approached, it was necessary to conduct a thorough analysis of the soap stock.


3.0 CLEANER PRODUCTION INITIATIVES

This section describes the implementation of each of the cleaner production projects, and the results. Detailed evaluation of each of the projects was not conducted prior to implementation. The projects were deemed by Bonlac to provide an excellent opportunity to demonstrate the benefits of cleaner production.

3.1 CIP CHEMICALS CHANGEOVER

3.1.1 Project Evaluation and Implementation

As noted in an earlier section, Bonlac decided that no detailed evaluation was required of the opportunity as the perceived economic and environmental benefits were well understood.

Implementation of the project was straight forward with a simple swap of the acid wash chemical from the existing nitric/phosphoric acid wash chemical to Stabilon®;. The swap required operators to be aware of the different water make-up required to use Stabilon® and its better-cleaning properties.

The impact of the Stabilon® project was to be assessed by monitoring the waste water quality and volume discharged from the facility.

3.1.2 Results

Bonlac made the change over to Stabilon® in their CIP process in September 1995.

Prior to change over to Stabilon® 200 litres of nitric/phosphoric acid was used each day in the CIP process. However, only 150 litres of Stabilon® is used to achieve the same level of cleaning. The need for less cleaning detergents also reduces the quantity cleaning water used, effluent produced and in electricity usage to power the cleaning pumps. Phosphorus and nitric levels in the waste water discharged to the waste water treatment facility are also expected to decrease.

The use of Stabilon® decreased the normal 6 hour CIP wash time by 25 %, to 4.5 hours. This effectively increased the available cheese making time by 1.5 hours per day. Bonlac continue to perform a full acid wash about once a week for control purposes. The introduction of Stabilon® to the CIP process increased the available time for the production of cheese by approximately 9 hours per week or 8%.

TABLE 1
DAILY MARGINAL COSTS ASSOCIATED WITH CHANGE OVER TO STABILON®  
  Cost ($/day)
Costs
    Stabilon® Consumption
-571.50
Savings
    Reduced Nitric/Phosphoric Acid Usage
220.00
    Extra Production - Cheese
382.50
    Extra Production - Whey
220.00
    Reduced Electricity Consumption
40.00
    Reduced Cleaning Water Consumption
20.80
NET BENEFIT $311.80

As illustrated in Table 1, change over to Stabilon®; yielded an overall net savings of $311.80 per day. The savings are expected to increase as the use of Stabilon® detergent is refined.

The expected reduction in the total quantity of waste water volume did not occur. However, cleaning with Stabilon® created additional time available for cheese production and therefore the volume of waste water increased accordingly. An attempt was made to relate the volume of waste water discharged to the waste water treatment facility, to the amount of cheese produced. The results were compared with data from the 1994/1995 production season to account for seasonal variation. The results are shown in Figure 1 and Figure 2.


Figure 1 indicates that in 1995/1996 season, despite the changeover to Stabilon®;, a clear reduction in effluent discharged per tonne of cheese produced was not obvious. The results display a general and gradual decline in waste water discharged from the cheese room per tonne of cheese produced. However, it is clear that the waste water generated was greater in December 1996 and January 1996, compared with the previous season. A reduction is evident in February and March 1995, but this is subsequently followed with another increase.


Figure 2 indicates that in the early stages of the 1995/1996 season, more milk was used to produce cheese relative to the 1994/1995 season. This was followed by a slight improvement between December 1995 and April 1996. This variation indicates that other factors have influenced the waste water volumes discharged from the facility. Although this study did not demonstrate a reduction in waste water discharge, it is expected that the volume of waste water will decrease during the next season as the use of Stabilon®; is refined.

Although the expected reduction in waste water did not eventuate, two main benefits from the use of Stabilon® were observed. Firstly, Bonlac have increased their cheese production rate without major capital works or plant expansion. Secondly, because Stabilon®; replaces the use of nitric and phosphoric acids, the nitrogen and phosphorus nutrient loading in the waste water released to the waste water treatment facility is expected to decreased. Such reductions in the environmental nutrient loading will decrease the risk of algal growth and eutrophication of the receiving waterways.

3.2 DIVERSION OF WASTE WATER TO FARM IRRIGATION

3.2.1 Project Evaluation

As with other cleaner production initiatives identified at the Bonlac Stanhope no quantitative economic or environmental evaluation was made of the diversion of wastewater to farm irrigation.

Economic benefits of the initiative were perceived as decreased costs associated with the wastewater treatment plant and sales of the crop grown on the irrigated land.

Environmental benefits were perceived as a decrease in hydraulic load to and from the wastewater treatment plant, leading to a more efficient wastewater treatment plant and a decrease in the impact of the receiving waterways.

3.2.2 Project Implementation

To implement the project an irrigation system needed to be installed so the proposed diversion system could be trialled.

The wastewater can only be diverted for farm irrigation when there is sufficient capacity for the irrigated land to sustainably absorb the wastewater. Therefore, the capacity of the land to accept the wastewater depends on the season and the amount of rainfall.

The diversion of waste water to farm was scheduled to commence in December 1995. The farmland is owned by Bonlac.

3.2.3 Results

Diversion of the three low ionic waste water streams from the whey room, demineralisation plant, and evaporators to nearby farmland was initially delayed whilst the land was prepared for irrigation and subsequently commenced in February 1996.

A ten day trail was performed to commission the irrigation facilities installed, as well as demonstrate the potential reduction in waste water transported to the waste water treatment facility. The results of the trial are represented in Figure 3 and Figure 4.


Figure 3



Figure 4

Before diversion commenced, a total of about 3,390 kL of waste water was sent to the waste water treatment facility each day. During the diversion, the flow reduced to an average of 2,390 kL per day, representing an approximate 30 % reduction of effluent discharged into Deakin Drain, and ultimately into the Murray River. Figure 4 illustrates the waste water discharged to the waste treatment facility per tonne of cheese produced. This was done to demonstrate that the effluent reduction was due to the diversion trials, rather than changes in the production rate.

The diversion will occur continuously commencing in the next cheese production season. The scheduling of the diversion process will strongly depend on seasonal climatic patterns including rainfall, relative humidity and temperature. However, the savings obtained during the optimum weather conditions will greatly reduce the loading on the existing waste treatment facility.

Bonlac intend to grow millet grass on the irrigated farmland, and sell it as fodder for cattle.

In summary, the major benefit of the project is a significant reduction in the volume of waste water processed by the waste water treatment facility and an increase in the efficiency of the facility. This reduction translates into a decrease in the hydraulic loading of waste water entering the Deakin Drain directing water to the Murray River. The secondary benefit is the expected earnings from the millet grass to be grown on the farmland.

3.3 SOLIDS SCREENING FROM CHEESE ROOM WASTE WATER

3.3.1 Project Evaluation

No detailed quantitative evaluation was undertaken of the cleaner production initiative prior to implementation.

The economic benefits of the initiative were identified as a decrease in lost cheese, thereby effectively increasing plant productivity, and a decrease in wastewater treatment costs.

The environmental benefits were perceived as a more efficient use of resources and a decrease in suspended solid and organic load to the wastewater treatment plant and the local receiving waterway.

3.3.2 Project Implementation

Two methods were proposed for reducing the quantity of suspended solids in the cheese room wastewater.

One method proposed to capture solids from the cheese room waste water involved installing screens in the cheese room waste water outlet, thereby reducing the organic load on the waste water treatment facility. The recovered solids were to be re-processed if free of contamination. Installation of the screens was scheduled for December 1995.

In addition to the screens, Bonlac proposed to install two large settling tanks in the whey room, with the intent of removing cheese solids from the process rinse water. This system was considered less likely to result in microbial contamination of the cheese. Again the recovered solids could be re-used in the cheese making process and the wastewater from cheese making plant would have lower suspended solids. The settling tanks were to be installed and operational by the beginning of February 1996.

To monitor the impact of the cheese solids removal project, a sampling and testing program was set up to monitor total suspended solids (TSS) in the effluent streams leaving the cheese room.

3.3.3 Results

Screens to capture solids in the cheese room effluent discharge, were installed in December 1995. Total suspended solids (TSS) in the discharge is plotted in Figure 5 and TSS as a function of cheese production is plotted in Figure 6. A significant decrease was noted in the first month of operation, both in absolute terms and as a function of the tonnage of cheese produced. A gradual increase is clearly evident beyond January 1996. The cause of this increase has yet to be determined, but the TSS levels are still markedly lower than the concentration of suspended solids in the waste water prior to the installation of the screens.

The settling tanks were installed in late February 1996 although, because of time constraints, only one tank was commissioned. Bonlac personnel reported that the optimum operating conditions for the tank were still being investigated. This could explain the reduced effectiveness of the settling tank in removing the solids loading in the waste water discharge and the gradual but eventual increase in the solids content of the waste water. However, both tanks will be operational and fully optimised for the next cheese production season. It is expected that the TSS in the waste water discharge will decrease during the next season.


Figure 5



Figure 6
The estimated breakdown of costs associated with the capture of cheese solids from the whey leaving the cheese room follows:

Tank rework for normal and salt curd fines $11,000
Kason screens upgrade and pipework $4,500
Rearranging pipework on settling tanks $15,000
TOTAL COST$30,500

The initiative is expected to decrease the amount of solids being sent to the wastewater treatment plant and an increase in cheese production of over 17,700 kgs/year or approximately 1% of production. This equates to production of approximately $100,000 of product. The payback period is less than four months.

In summary, the installation of the screens and settling tanks in the cheese plant reduced the overall level of suspended solids in the waste water. The major benefit to the environment is from the reduced organic loading on the receiving waterways. Bonlac expect to convert the captured solids into product available for sale.

Bonlac is now using product that was previously lost in the waste water and is saving on raw materials - milk.

3.4 ALTERNATIVE DISPOSAL OF SOAP STOCK

3.4.1 Project Evaluation

The cleaner production initiative identified involved finding a viable use for what is at presently considered a waste.

The economic benefits of the initiative include reducing waste disposal costs and producing an additional income source. The environmental benefits included a decreased impact on local soil, groundwater and surface water and improved use of resources.

3.4.2 Project Implementation

To assist in the evaluating potential uses of the soap stock, Bonlac carried out tests which included an assessment of the free fatty acids content in the soap stock. The information was used to determine whether the soap stock composition is sufficiently consistent during the production season for potential use in the soap manufacturing process.

3.4.3 Results

A number of samples of the soap stock were taken and analysed. The soap stock composition was found to vary significantly during the season and was influenced by factors such as the type of cream stabilisers used in the anhydrous milk fat manufacturing process. For instance, whey cream was found to increase the amount of solids in the waste because it contained high levels of free fatty acids.

A number of commercial soap manufacturers were approached with the analysis results. All manufacturers indicated that they required consistent quality and composition if the purchase of soap stock was to be viable. In addition, the manufactures specified concentrations of caustic soda greater than 40 %. Neither of these criteria could be guaranteed by Bonlac and therefore the material was not attractive to any of the soap manufacturers contacted.

In summary, selling the soap stock to commercial soap manufacturers did not eventuate because the soap manufacturers demanded strict quality control and consistency in the soap stock composition, which is currently beyond Bonlac's capacity to supply. In the meantime Bonlac will continue to land farm the soap stock waste. However, the exercise has yielded a better understanding of the soap stock composition which will form the basis for seeking other re-use options in future.


4.0 REVIEW OF PROJECT

The initiatives which constitute the cleaner production demonstration program at Bonlac required monitoring through sampling, and analysis of the waste water quality and quantity. Monitoring stations were set up at a number of effluent interceptor pits throughout the plant. Each point was used to measure the total volumetric flow of effluent, as well as parameters such as chemical oxygen demand (COD) and total suspended solids.

The information gathered was important in evaluating the outcome of the initiatives of the cleaner production demonstration program. Bonlac will continue to monitor the quality of their effluent beyond the completion of this program and use the data to identify other areas in which to focus cleaner production projects. This will be used to provide evidence of Bonlacís commitment to continual improvement in their efforts to minimise any impact on the environment.

Importantly the cleaner production demonstration program has resulted in quantifiable benefits for Bonlac as indicated in the previous section. In addition, the comprehensive monitoring infra-structure established for continuous monitoring of the effluent will assist Bonlac in their commitment towards minimising the impact its operations on the environment.

While the project was a success at Bonlac Foods, there is scope for increasing the benefits resulting from the cleaner production scheme. Achievements were limited because the process modifications and monitoring equipment took longer than expected to implement. These delays coupled with the fact that the dairy production has defined seasonal cycles meant that the effective time available to implement the projects was reduced.

The implementation and day-to-day monitoring of the projects was the responsibility of one person. As a result some projects took longer to initiate than others, whilst some only ran for short periods, enough to demonstrate the benefits. The scheduling was not due to the person responsible, but rather the lack of resources made available to them. During the project, other unforseen issues took higher priority, including quality audits and a change in production demands.

Actual costs and benefits of implementing the projects were largely as anticipated.

There is strong commitment from Bonlac to continue to develop the projects further. Bonlac is also committed to the ongoing investigation of other opportunities for cleaner production. The company is committed to operating a certified Environmental Management System (ISO 14001), through which continuous improvement and cleaner production will proceed.


5.0 CONCLUDING REMARKS

Based on the experience of implementing a Cleaner Production Program at Bonlac Foods (Stanhope), significant environmental and economic benefits can be expected from the application of Cleaner Production in the dairy food industry.

There are many cleaner production opportunities for the Bonlac site. The projects which were implemented during the time frame of the Demonstration Project resulted in demonstrable savings for Bonlac and clear benefits for the environment. The projects focused on continuous improvement, reduction of waste water and recovery of product in the waste stream.

In this demonstration program, four projects were identified. Three projects resulted in benefits to Bonlac and the environment. By improving the process efficiency, the impact of discharges to the environment has been reduced. Replacing acid cleaning with a Stabilon® detergent resulted in greater production capacity and a reduced risk of environmental damage. Diverting waste water to farmland for irrigation of crops is a clean and profitable method for dealing with large volumes of effluent. Screens to capture cheese solids which are normally lost to the drains results in higher product recovery rates and reduce the organic loading on the environment. The soap stock project was not successful in identifying an alternative use rather than disposal to landfill, but a better understanding of the soap stack composition was gained.

A key lesson from this Cleaner Production demonstration project is that the process of compiling the environmental and process data in itself plays an important role in the identification of Cleaner Production initiatives. Other important lessons which emanated from demonstration project include the importance of commitment from management, ideas are encouraged in teams commissioned to assess specific parts of the operation, and that opportunities do not have to involve large capital costs.

Cleaner Production initiatives have been implemented at Bonlac Foods (Stanhope) with significant improvements. This has provided Bonlac with incentive for other Cleaner Production opportunities to be investigated and implemented.


6.0 BONLAC FOODS PERSPECTIVE

"The nature of process operations at Bonlac result in the generation of copious waste water. The Cleaner Production Demonstration project focussed on process improvements to minimise water usage and waste water generated, as well as recover product which has been discharged with the waste water. The Demonstration Project has successfully reduced the amount of waste and increased process efficiency through combining continuous improvement with cleaner production.

Bonlac believes that the project schedule, costs and benefits proceeded largely as expected. The overall benefits gained were significant.

In addition to the cost savings, the Program demonstrated the method and benefits associated with Cleaner Production concepts. These methods will be adopted to carry out other cleaner production opportunities at the Stanhope site and all other Bonlac facilities.

Bonlac will continue to provide additional details of the projects implemented where possible to the EPA. Bonlac is pleased to have participated in the EPA Cleaner Production Demonstration Project."


Llew Sandford

Technical Manager

 

 

ea_logo.gif