Snap-on Tools Recycling a Rinsewater Stream Using |
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Standard Industrial Classification (SIC) | Sheet Metal Fabrication/3444 | ||
Process | Electrodeposition of water based paints. | ||
Type of Waste | Ethylene glycol monobutyl ether (butyl cellusolve) | ||
Strategies | Process Modification - Ion Exchange Column Installation | ||
Background | Snap-on Tools is a hand tool and tool
storage rollaway manufacturer headquartered in Kenosha, Wisconsin. Snap-on employs over
1,300 in its Wisconsin operations and has gross revenues in excess of $900 million. Snap-on uses an electrocoating paint line with water based coatings. Snap-on Tools uses ultrafiltration to recover process paint from the rinse tanks' effluent. The ultrafiltration process produces concentrated paint for return to the paint bath, and permeate which is recycled to the rinse baths. The permeate composition is 97% water with 2-3% ethylene glycol monobutyl ether (butyl cellusolve) and a contaminant isopropyl amine present in amounts less than 1%. The recycle loop to the rinse could not be totally closed because the contaminant isopropyl amine would build up in the system and ruin the rinse bath. To prevent the build up of isopropyl amine, a purge stream was split from the recycle stream and drained to the Publicly-Owned Treatment Works (POTW). In 1989, Snap-on reported sewering over 190,000 pounds of the butyl cellusolve. The local POTW had no difficulty handling the extra strength wastewater loading. |
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Motivation | Snap-on Tools places a substantial value on its image as a good corporate citizen. As a result, Snap-on felt uncomfortable discharging the large amount of butyl cellusolve to the local POTW. The company felt that their disclosure of the discharge in SARA Title III reporting would taint their corporate image. | ||
Changes Implemented | Snap-on Tools decided to recover the
190,000 pounds of butyl cellusolve that was lost in the purge of the recycle stream and
discharged to the POTW. Snap-on Tools needed a method of removing the contaminant
isopropyl amine from the purge stream. Snap-on identified ion exchange as the most
attractive means of removing isopropyl amine. A two stage ion exchange resin system was installed to remove the isopropyl amine from the purge stream. The permeate from the ion exchange system (water and butyl cellusolve) can now returned to the rinse baths. The isopropyl amine that is trapped by the resin is stripped during the regeneration of the resin and is sewered. The ion exchange system has been very successful in removing the isopropyl amine. Only 3,500 pounds per year of butyl celluslove must now be purged and discharged to the POTW. Snap-on Tools now saves $54,900/year due to butyl cellusolve recovery, and at least $18,000/year on sewer fees. |
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Problems Encountered | It was critical that the ion exchange system be effective in removing isopropyl amine because the build up of the contaminant in the rinsewater could degrade the quality of the electocoating finish. Closing the wastewater loop entirely was contingent on complete removal of isopropyl amine. | ||
Material/Energy Balance | Original Process Feedstock Waste Disposal Pollution Prevention Approach Feedstock Waste |
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Economics | Capital Cost $150,000 (1989) Operating/Maintenance Cost Payback Period |
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Company Address | Snap-on Tools Corporation Kenosha, WI 53141-1410 |
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Contact Person | Mr. Hiram J. Buffington, Manager Environmental Engineering and Industrial Hygiene Phone: 414/656-5200 |
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Pollution Prevention Resources | University of Wisconsin Extension Solid and Hazardous Waste Education Center Milwaukee area: 414/475-2845 Remainder of state: 608/262-0385 Pollution Prevention
Clearinghouse |
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